HL incident on 2025-10-07 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200
Incident datetime
2025-10-07 09:20
Report number
Location
OK
Narrative
Oneok technician arrived on site for semi-annual valve inspection and discovered a stem packing leak. Technician notified local supervisor of the situation. Osro was dispatched to assist with clean-up efforts. Operations injected additional valve packing to stop the packing leak. The entire valve was removed and replaced with a new valve setting with a stainless-steel stem. The nickel-plated carbon steel stems are a known problem due to holidays in the nickel plating on the carbon steel stems allowing corrosion to occur resulting in stem packing damage. There are currently ongoing mitigation efforts to replace all similar valves.
Detailed record list
Report Received Date
2025-11-06 00:00:00
Iyear
2025
Report Number
20250256
Supplemental Number
41554
Report Type
Original Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2025-10-07 09:20:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2.29
Recovered Bbls
1.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2025-10-07 09:20:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Routine Shutdown
Communication State Fed Ind
No
On Site Datetime
2025-10-07 09:20:00
Confirmed Discovery Datetime
2025-10-07 09:20:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2025-10-07 07:30:00
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2025-10-07 07:30:00
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2025-10-07 09:25:00
Osro Arrived On Site Dt
10/7/2025 13:50
Num Pub Evacuated
0
Pipe Fac Name
East Houston- El Paso
Segment Name
Line Id 6645
Onshore State Abbreviation
Tx
Onshore Postal Code
76936
Onshore City Name
Eldorado
Onshore County Name
Schleicher
Designated Location
Milepost
Designated Name
347
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Mj 303
Installation Year
2012
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Nickel Plated Carbon Steel Stems
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
200
Est Cost Emergency
10000
Est Cost Environmental
30000
Est Cost Other
0
Prpty
40220
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
107
Mop Psig
953
Mop Cfr Section
Mop Cfr Section Details
Longhorn Mitigation Plan Submission
Maop Established Date
2017-05-07 00:00:00
Maop Reversal Flow Ind
Yes
Surge Analysis Date
2024-10-29 00:00:00
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
153665
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No controller actions took place prior to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Additional Defect Ind
Yes
Preparer Name
G*** C*********
Preparer Title
Regulatory Compliance Specialist Ii
Preparer Email
G**************@o****.com
Preparer Telephone
9183818066
Prepared Date
2025-11-06 00:00:00
Local Contact Name
G*** C*********
Local Contact Email
G**************@o****.com
Local Contact Telephone
9183818066
Authorizer Name
R*** M****
Authorizer Telephone
9183818066
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
G**************@o****.com
Narrative
Oneok technician arrived on site for semi-annual valve inspection and discovered a stem packing leak. Technician notified local supervisor of the situation. Osro was dispatched to assist with clean-up efforts. Operations injected additional valve packing to stop the packing leak. The entire valve was removed and replaced with a new valve setting with a stainless-steel stem. The nickel-plated carbon steel stems are a known problem due to holidays in the nickel plating on the carbon steel stems allowing corrosion to occur resulting in stem packing damage. There are currently ongoing mitigation efforts to replace all similar valves.
Report Received Date 2025-11-06 00:00:00
Iyear 2025
Report Number 20250256
Supplemental Number 41554
Report Type Original Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2025-10-07 09:20:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 30.855313 Google Maps OpenStreetMap
Location Longitude -100.658147 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2.29
Recovered Bbls 1.9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2025-10-07 09:20:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Routine Shutdown
Communication State Fed Ind No
On Site Datetime 2025-10-07 09:20:00
Confirmed Discovery Datetime 2025-10-07 09:20:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2025-10-07 07:30:00
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2025-10-07 07:30:00
Downstream Valve Type Ind Remotely Controlled
Notify Qualified Indiv Ind No
Oil Spill Removal Org Ind Yes
Osro Activated Datetime 2025-10-07 09:25:00
Osro Arrived On Site Dt 10/7/2025 13:50
Num Pub Evacuated 0
Pipe Fac Name East Houston- El Paso
Segment Name Line Id 6645
Onshore State Abbreviation Tx
Onshore Postal Code 76936
Onshore City Name Eldorado
Onshore County Name Schleicher
Designated Location Milepost
Designated Name 347
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Mj 303
Installation Year 2012
Manufactured Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Nickel Plated Carbon Steel Stems
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 200
Est Cost Emergency 10000
Est Cost Environmental 30000
Est Cost Other 0
Prpty 40220
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 107
Mop Psig 953
Mop Cfr Section Other View CFR 49 §192
Mop Cfr Section Details Longhorn Mitigation Plan Submission
Maop Established Date 2017-05-07 00:00:00
Maop Reversal Flow Ind Yes
Surge Analysis Date 2024-10-29 00:00:00
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 153665
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No controller actions took place prior to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Additional Defect Ind Yes
Preparer Name G*** C*********
Preparer Title Regulatory Compliance Specialist Ii
Preparer Email G**************@o****.com
Preparer Telephone 9183818066
Prepared Date 2025-11-06 00:00:00
Local Contact Name G*** C*********
Local Contact Email G**************@o****.com
Local Contact Telephone 9183818066
Authorizer Name R*** M****
Authorizer Telephone 9183818066
Authorizer Title Regulatory Compliance Manager
Authorizer Email G**************@o****.com
Narrative Oneok technician arrived on site for semi-annual valve inspection and discovered a stem packing leak. Technician notified local supervisor of the situation. Osro was dispatched to assist with clean-up efforts. Operations injected additional valve packing to stop the packing leak. The entire valve was removed and replaced with a new valve setting with a stainless-steel stem. The nickel-plated carbon steel stems are a known problem due to holidays in the nickel plating on the carbon steel stems allowing corrosion to occur resulting in stem packing damage. There are currently ongoing mitigation efforts to replace all similar valves.

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