HL incident on 2025-09-25 — TX

Operator
West Texas Gulf Pipeline Co
Cause
Other Accident Cause
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$55,000
Incident datetime
2025-09-25 10:24
Report number
Location
TX
Narrative
On 09/25/25 at approximately 10:24, contractors working for the company punctured the 21002.01 - 26inch nederland to trinity line causing crude oil to release. Operations was immediately notified and dispatched to the location. The line was isolated because the line was already shut down for a project. Approximately 25 barrels of crude oil was released to the soil with 5 gallons migrating into lnva canal. An osro cleaned up released product and contaminated soil. The leak was repaired by installing a mechanical clamp. The line was restarted on 09/26/25 at approximately 09:00. The cause of the accident is still under investigation. A supplemental report will be submitted once complete.
Detailed record list
Report Received Date
2025-10-21 00:00:00
Iyear
2025
Report Number
20250245
Supplemental Number
41495
Report Type
Original
Operator Id
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2025-09-25 10:24:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
25
Recovered Bbls
25
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2025-09-25 10:24:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Routine Shutdown
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2025-09-25 12:30:00
On Site Datetime
2025-09-25 10:50:00
Confirmed Discovery Datetime
2025-09-25 10:50:00
Nrc Rpt Datetime
2025-09-25 12:09:00
Nrc Rpt Num
Additional Nrc Report Numbers
1443851
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2025-09-25 12:30:00
Upstream Valve Type Ind
Manual
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
Valve Was Already Closed
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2025-09-25 11:00:00
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2025-09-25 12:10:00
Osro Arrived On Site Dt
9/25/2025 17:00
Num Pub Evacuated
0
Pipe Fac Name
West Texas Gulf Pipeline
Segment Name
21002.01 - 26 Inch Nederland To Trinity
Onshore State Abbreviation
Tx
Onshore Postal Code
77713
Onshore City Name
Not Within A Municipality
Onshore County Name
Jefferson
Designated Location
Survey Station No.
Designated Name
961334.5
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
26
Pipe Wall Thickness
0.37
Pipe Smys
52000
Pipe Specification
Api 5l
Pipe Seam Type
Flash Welded
Pipe Manufacturer
A.o. Smith
Pipe Coating Type
Coal Tar
Coating Applied Ind
No
Installation Year
1953
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
1.4
Puncture Circum
1.4
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
0.12
Rel Water Name
Lower Neches Valley Authority Canal
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
140000
Est Cost Gas Released
1500
Est Cost Prop Damage
55000
Est Cost Emergency
735000
Est Cost Environmental
400000
Est Cost Other
0
Prpty
1331500
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
45
Mop Psig
655
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2013-01-04 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required)
Preparer Name
T*** N*******
Preparer Title
Director - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2025-10-21 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 09/25/25 at approximately 10:24, contractors working for the company punctured the 21002.01 - 26inch nederland to trinity line causing crude oil to release. Operations was immediately notified and dispatched to the location. The line was isolated because the line was already shut down for a project. Approximately 25 barrels of crude oil was released to the soil with 5 gallons migrating into lnva canal. An osro cleaned up released product and contaminated soil. The leak was repaired by installing a mechanical clamp. The line was restarted on 09/26/25 at approximately 09:00. The cause of the accident is still under investigation. A supplemental report will be submitted once complete.
Report Received Date 2025-10-21 00:00:00
Iyear 2025
Report Number 20250245
Supplemental Number 41495
Report Type Original
Operator Id 22442 PHMSA Enforcement
Name West Texas Gulf Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2025-09-25 10:24:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 30.100855 Google Maps OpenStreetMap
Location Longitude -94.246006 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 25
Recovered Bbls 25
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2025-09-25 10:24:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Routine Shutdown
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2025-09-25 12:30:00
On Site Datetime 2025-09-25 10:50:00
Confirmed Discovery Datetime 2025-09-25 10:50:00
Nrc Rpt Datetime 2025-09-25 12:09:00
Nrc Rpt Num 1443760 NRC Report How to search
Additional Nrc Report Numbers 1443851
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2025-09-25 12:30:00
Upstream Valve Type Ind Manual
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail Valve Was Already Closed
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2025-09-25 11:00:00
Oil Spill Removal Org Ind Yes
Osro Activated Datetime 2025-09-25 12:10:00
Osro Arrived On Site Dt 9/25/2025 17:00
Num Pub Evacuated 0
Pipe Fac Name West Texas Gulf Pipeline
Segment Name 21002.01 - 26 Inch Nederland To Trinity
Onshore State Abbreviation Tx
Onshore Postal Code 77713
Onshore City Name Not Within A Municipality
Onshore County Name Jefferson
Designated Location Survey Station No.
Designated Name 961334.5
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 26
Pipe Wall Thickness 0.37
Pipe Smys 52000
Pipe Specification Api 5l
Pipe Seam Type Flash Welded
Pipe Manufacturer A.o. Smith
Pipe Coating Type Coal Tar
Coating Applied Ind No
Installation Year 1953
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 1.4
Puncture Circum 1.4
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 0.12
Rel Water Name Lower Neches Valley Authority Canal
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 140000
Est Cost Gas Released 1500
Est Cost Prop Damage 55000
Est Cost Emergency 735000
Est Cost Environmental 400000
Est Cost Other 0
Prpty 1331500
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 45
Mop Psig 655
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 2013-01-04 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required)
Preparer Name T*** N*******
Preparer Title Director - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Prepared Date 2025-10-21 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Director - Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 09/25/25 at approximately 10:24, contractors working for the company punctured the 21002.01 - 26inch nederland to trinity line causing crude oil to release. Operations was immediately notified and dispatched to the location. The line was isolated because the line was already shut down for a project. Approximately 25 barrels of crude oil was released to the soil with 5 gallons migrating into lnva canal. An osro cleaned up released product and contaminated soil. The leak was repaired by installing a mechanical clamp. The line was restarted on 09/26/25 at approximately 09:00. The cause of the accident is still under investigation. A supplemental report will be submitted once complete.

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