HL incident on 2025-09-16 — TX

Operator
Plains Pipeline, L.p.
Cause
Other Accident Cause
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$17,500
Incident datetime
2025-09-16 12:42
Report number
Location
TX
Narrative
Approximately 67 barrels of crude oil were released from the wink s to monahans 10" pipeline. The date and time of the release (part a q4) is indicative of the earliest possible time the release could have started based on pipeline movements. The cause and associated preventative measure will be provided in a supplemental report pending further investigation into the cause of the release.
Detailed record list
Report Received Date
2025-10-16 00:00:00
Iyear
2025
Report Number
20250242
Supplemental Number
41471
Report Type
Original
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2025-09-16 01:21:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
-103.1347222
Commodity Released Type
Crude Oil
Unintentional Release Bbls
67
Recovered Bbls
67
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2025-09-16 12:42:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2025-09-16 13:12:00
Restart Datetime
2025-09-16 19:25:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2025-09-16 13:27:00
On Site Datetime
2025-09-16 12:48:00
Confirmed Discovery Datetime
2025-09-16 19:25:00
Nrc Rpt Datetime
2025-09-18 12:40:00
Nrc Rpt Num
Additional Nrc Report Numbers
1443234
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2025-09-16 13:12:00
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2025-09-16 12:48:00
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2025-09-16 12:47:00
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wink S To Monahans 10inch
Segment Name
Wink S To Monahans 10inch
Onshore State Abbreviation
Tx
Onshore Postal Code
79789
Onshore City Name
Wink
Onshore County Name
Winkler
Designated Location
Milepost
Designated Name
0+2.15mi
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
54
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
10
Pipe Wall Thickness
0.25
Pipe Smys
46000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Coating Applied Ind
Yes
Installation Year
1991
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
3500
Est Cost Gas Released
4000
Est Cost Prop Damage
17500
Est Cost Emergency
354097
Est Cost Environmental
0
Est Cost Other
0
Prpty
379097
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
44
Mop Psig
1440
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2018-06-18 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
27456
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required)
Preparer Name
N****** A G******* N****** A G*******
Preparer Title
Hse Regulatory Compliance Supervisor
Preparer Email
N***************@p*****.com
Preparer Telephone
7136464376
Prepared Date
2025-10-16 00:00:00
Local Contact Name
N****** A G******* N****** A G*******
Local Contact Email
N***************@p*****.com
Local Contact Telephone
7136464376
Authorizer Name
N****** A G*******
Authorizer Telephone
7136464376
Authorizer Title
Hse Regulatory Compliance Supervisor
Authorizer Email
N***************@p*****.com
Narrative
Approximately 67 barrels of crude oil were released from the wink s to monahans 10" pipeline. The date and time of the release (part a q4) is indicative of the earliest possible time the release could have started based on pipeline movements. The cause and associated preventative measure will be provided in a supplemental report pending further investigation into the cause of the release.
Report Received Date 2025-10-16 00:00:00
Iyear 2025
Report Number 20250242
Supplemental Number 41471
Report Type Original
Operator Id 300 PHMSA Enforcement
Name Plains Pipeline, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2025-09-16 01:21:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 31.7510556 Google Maps OpenStreetMap
Location Longitude -103.1347222 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 67
Recovered Bbls 67
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2025-09-16 12:42:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2025-09-16 13:12:00
Restart Datetime 2025-09-16 19:25:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2025-09-16 13:27:00
On Site Datetime 2025-09-16 12:48:00
Confirmed Discovery Datetime 2025-09-16 19:25:00
Nrc Rpt Datetime 2025-09-18 12:40:00
Nrc Rpt Num 1443070 NRC Report How to search
Additional Nrc Report Numbers 1443234
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2025-09-16 13:12:00
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2025-09-16 12:48:00
Downstream Valve Type Ind Remotely Controlled
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2025-09-16 12:47:00
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Wink S To Monahans 10inch
Segment Name Wink S To Monahans 10inch
Onshore State Abbreviation Tx
Onshore Postal Code 79789
Onshore City Name Wink
Onshore County Name Winkler
Designated Location Milepost
Designated Name 0+2.15mi
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 54
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 10
Pipe Wall Thickness 0.25
Pipe Smys 46000
Pipe Specification Api 5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Coating Applied Ind Yes
Installation Year 1991
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 3500
Est Cost Gas Released 4000
Est Cost Prop Damage 17500
Est Cost Emergency 354097
Est Cost Environmental 0
Est Cost Other 0
Prpty 379097
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 44
Mop Psig 1440
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2018-06-18 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 27456
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required)
Preparer Name N****** A G******* N****** A G*******
Preparer Title Hse Regulatory Compliance Supervisor
Preparer Email N***************@p*****.com
Preparer Telephone 7136464376
Prepared Date 2025-10-16 00:00:00
Local Contact Name N****** A G******* N****** A G*******
Local Contact Email N***************@p*****.com
Local Contact Telephone 7136464376
Authorizer Name N****** A G*******
Authorizer Telephone 7136464376
Authorizer Title Hse Regulatory Compliance Supervisor
Authorizer Email N***************@p*****.com
Narrative Approximately 67 barrels of crude oil were released from the wink s to monahans 10" pipeline. The date and time of the release (part a q4) is indicative of the earliest possible time the release could have started based on pipeline movements. The cause and associated preventative measure will be provided in a supplemental report pending further investigation into the cause of the release.

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