HL incident on 2025-09-16 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$16,700
Incident datetime
2025-09-16 07:00
Report number
Location
TX
Narrative
On 9/16/2025 at 7:00 am cst enterprise pipeline operator discovered a crude oil release on manifold pipeline at sealy station. The leak was immediately isolated. Approximately 0.5 barrels of crude oil was released with remediation completed. The leaking line has been sent for metallurgical analysis. The line is out of service.
Detailed record list
Report Received Date
2025-10-15 00:00:00
Iyear
2025
Report Number
20250241
Supplemental Number
41464
Report Type
Original
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2025-09-16 07:00:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2025-09-16 07:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2025-09-16 07:05:00
Restart Datetime
2025-09-16 22:00:00
Communication State Fed Ind
No
On Site Datetime
2025-09-16 07:00:00
Confirmed Discovery Datetime
2025-09-16 07:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2025-09-17 07:00:00
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Sealy Station
Segment Name
C129 Manifold
Onshore State Abbreviation
Tx
Onshore Postal Code
77474
Onshore City Name
Sealy
Onshore County Name
Austin
Designated Location
Milepost
Designated Name
0+0.00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
24
Pipe Wall Thickness
0.5
Pipe Smys
70000
Pipe Specification
Api-5ls
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Coating Applied Ind
No
Installation Year
2017
Manufactured Year
2017
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
35
Est Cost Prop Damage
16700
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
16735
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
14
Mop Psig
285
Mop Cfr Section
Four Hour Test Or Operation �195.406(A)(5)
Maop Established Date
2017-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release caused by internal corrosion.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Corrosive Commodity Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Intrnl Cor Corrosive Cmdty Ind
Yes
Preparer Name
M****** K********
Preparer Title
Pipeline Compliance Engineer
Preparer Email
M*********@e****.com
Preparer Telephone
713-376-9799
Prepared Date
2025-10-15 00:00:00
Local Contact Name
M****** K********
Local Contact Email
M*********@e****.com
Local Contact Telephone
713-376-9799
Authorizer Name
S**** D****
Authorizer Telephone
713-381-5585
Authorizer Title
Senior Manager Compliance
Authorizer Email
S******@e****.com
Narrative
On 9/16/2025 at 7:00 am cst enterprise pipeline operator discovered a crude oil release on manifold pipeline at sealy station. The leak was immediately isolated. Approximately 0.5 barrels of crude oil was released with remediation completed. The leaking line has been sent for metallurgical analysis. The line is out of service.
Report Received Date 2025-10-15 00:00:00
Iyear 2025
Report Number 20250241
Supplemental Number 41464
Report Type Original
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2025-09-16 07:00:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.75895 Google Maps OpenStreetMap
Location Longitude -96.148369 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.5
Recovered Bbls 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2025-09-16 07:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2025-09-16 07:05:00
Restart Datetime 2025-09-16 22:00:00
Communication State Fed Ind No
On Site Datetime 2025-09-16 07:00:00
Confirmed Discovery Datetime 2025-09-16 07:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2025-09-17 07:00:00
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Sealy Station
Segment Name C129 Manifold
Onshore State Abbreviation Tx
Onshore Postal Code 77474
Onshore City Name Sealy
Onshore County Name Austin
Designated Location Milepost
Designated Name 0+0.00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 24
Pipe Wall Thickness 0.5
Pipe Smys 70000
Pipe Specification Api-5ls
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Coating Applied Ind No
Installation Year 2017
Manufactured Year 2017
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 35
Est Cost Prop Damage 16700
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 16735
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 14
Mop Psig 285
Mop Cfr Section Four Hour Test Or Operation �195.406(A)(5) View CFR 49 §192
Maop Established Date 2017-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release caused by internal corrosion.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Corrosive Commodity Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Intrnl Cor Corrosive Cmdty Ind Yes
Preparer Name M****** K********
Preparer Title Pipeline Compliance Engineer
Preparer Email M*********@e****.com
Preparer Telephone 713-376-9799
Prepared Date 2025-10-15 00:00:00
Local Contact Name M****** K********
Local Contact Email M*********@e****.com
Local Contact Telephone 713-376-9799
Authorizer Name S**** D****
Authorizer Telephone 713-381-5585
Authorizer Title Senior Manager Compliance
Authorizer Email S******@e****.com
Narrative On 9/16/2025 at 7:00 am cst enterprise pipeline operator discovered a crude oil release on manifold pipeline at sealy station. The leak was immediately isolated. Approximately 0.5 barrels of crude oil was released with remediation completed. The leaking line has been sent for metallurgical analysis. The line is out of service.

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