HL incident on 2025-09-01 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Other Accident Cause
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2025-09-01 08:00
Report number
Location
TX
Narrative
On 9/1/2025 at 8:00 am cst enterprise pipeline operator discovered a crude release on facility piping at echo station. The leak was immediately isolated. Approximately 0.1 barrels of crude oil was released with remediation completed. The section of facility pipe has been disconnected and blinded off.
Detailed record list
Report Received Date
2025-09-29 00:00:00
Iyear
2025
Report Number
20250233
Supplemental Number
41413
Report Type
Original Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2025-09-01 08:00:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.1
Recovered Bbls
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2025-09-01 08:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2025-09-01 08:02:00
Restart Datetime
2025-09-09 10:50:00
Communication State Fed Ind
No
On Site Datetime
2025-09-01 08:00:00
Confirmed Discovery Datetime
2025-09-01 08:00:00
Nrc Rpt Datetime
2025-09-03 13:30:00
Nrc Rpt Num
Additional Nrc Report Numbers
1441835
Ignite Ind
No
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2025-09-01 08:05:00
Osro Arrived On Site Dt
9/1/2025 8:30
Num Pub Evacuated
0
Pipe Fac Name
Echo Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
77034
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost
Designated Name
0+0.00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
2015
Manufactured Year
2015
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
60
Est Cost Prop Damage
0
Est Cost Emergency
65000
Est Cost Environmental
20000
Est Cost Other
0
Prpty
85060
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
85
Mop Psig
1440
Mop Cfr Section
Four Hour Test Or Operation �195.406(A)(5)
Maop Established Date
2015-01-15 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release caused by pinhole leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Investigation Complete, Cause Of Accident Unknown
Incident Unknown Comments
Section Of The Facility Pipe Has Been Cut Out And Disconnected.
Preparer Name
M****** K********
Preparer Title
Pipeline Compliance Engineer
Preparer Email
M*********@e****.com
Preparer Telephone
713-376-9799
Prepared Date
2025-09-29 00:00:00
Local Contact Name
M****** K********
Local Contact Email
M*********@e****.com
Local Contact Telephone
713-376-9799
Authorizer Name
S**** D****
Authorizer Telephone
713-381-5585
Authorizer Title
Senior Manager Compliance
Authorizer Email
S******@e****.com
Narrative
On 9/1/2025 at 8:00 am cst enterprise pipeline operator discovered a crude release on facility piping at echo station. The leak was immediately isolated. Approximately 0.1 barrels of crude oil was released with remediation completed. The section of facility pipe has been disconnected and blinded off.
Report Received Date 2025-09-29 00:00:00
Iyear 2025
Report Number 20250233
Supplemental Number 41413
Report Type Original Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2025-09-01 08:00:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.61354 Google Maps OpenStreetMap
Location Longitude -95.18478 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.1
Recovered Bbls 0.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2025-09-01 08:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2025-09-01 08:02:00
Restart Datetime 2025-09-09 10:50:00
Communication State Fed Ind No
On Site Datetime 2025-09-01 08:00:00
Confirmed Discovery Datetime 2025-09-01 08:00:00
Nrc Rpt Datetime 2025-09-03 13:30:00
Nrc Rpt Num 1441660 NRC Report How to search
Additional Nrc Report Numbers 1441835
Ignite Ind No
Notify Qualified Indiv Ind No
Oil Spill Removal Org Ind Yes
Osro Activated Datetime 2025-09-01 08:05:00
Osro Arrived On Site Dt 9/1/2025 8:30
Num Pub Evacuated 0
Pipe Fac Name Echo Terminal
Onshore State Abbreviation Tx
Onshore Postal Code 77034
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost
Designated Name 0+0.00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing No
Pipe Facility Type Interstate
Item Involved Sump
Installation Year 2015
Manufactured Year 2015
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 60
Est Cost Prop Damage 0
Est Cost Emergency 65000
Est Cost Environmental 20000
Est Cost Other 0
Prpty 85060
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 85
Mop Psig 1440
Mop Cfr Section Four Hour Test Or Operation �195.406(A)(5) View CFR 49 §192
Maop Established Date 2015-01-15 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release caused by pinhole leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Investigation Complete, Cause Of Accident Unknown
Incident Unknown Comments Section Of The Facility Pipe Has Been Cut Out And Disconnected.
Preparer Name M****** K********
Preparer Title Pipeline Compliance Engineer
Preparer Email M*********@e****.com
Preparer Telephone 713-376-9799
Prepared Date 2025-09-29 00:00:00
Local Contact Name M****** K********
Local Contact Email M*********@e****.com
Local Contact Telephone 713-376-9799
Authorizer Name S**** D****
Authorizer Telephone 713-381-5585
Authorizer Title Senior Manager Compliance
Authorizer Email S******@e****.com
Narrative On 9/1/2025 at 8:00 am cst enterprise pipeline operator discovered a crude release on facility piping at echo station. The leak was immediately isolated. Approximately 0.1 barrels of crude oil was released with remediation completed. The section of facility pipe has been disconnected and blinded off.

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