Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2025-08-22 — TX
Operator
Oryx Delaware Oil Transport Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$2,500
Incident datetime
2025-08-22 00:00 UTC
Report number
Location
TX
Narrative
Approximately 91 barrels of crude oil were released from a sump at oryx state line station. The date and time of the release (part a q4) are indicative of the earliest possible time the release could have started based on when a lightning storm caused a power outage at the station. The cause of the release is attributed to a valve misalignment following a severe thunderstorm (power outage) which prevented the pipeline from relieving to tankage. To prevent future incidents, the valve position was corrected and the individual was re-trained.
Detailed record list
Report Received Date
2025-08-22 00:00:00
Iyear
2025
Report Number
20250196
Supplemental Number
41292
Report Type
Original Final
Operator Id
39654
Name
Oryx Delaware Oil Transport Llc
Operator Street Address
333 Clay St. Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
31.967744
Location Longitude
-103.738853
Commodity Released Type
Crude Oil
Unintentional Release Bbls
91
Recovered Bbls
91
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oryx State Line
Segment Name
Sump
Onshore State Abbreviation
Tx
Onshore Postal Code
79754
Onshore City Name
Mentone
Onshore County Name
Loving
Designated Location
Milepost
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
2017
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
350
Est Cost Prop Damage
2500
Est Cost Emergency
20000
Est Cost Environmental
0
Est Cost Other
0
Prpty
22850
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1200
Mop Psig
285
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2017-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Nf Lightning Ind
Yes
Preparer Name
N****** G*******
Preparer Title
Hse Regulatory Compliance Supervisor
Preparer Email
N***************@p*****.com
Preparer Telephone
7136464376
Prepared Date
2025-08-22 00:00:00
Local Contact Name
N****** A G*******
Local Contact Email
N***************@p*****.com
Local Contact Telephone
7136464376
Authorizer Name
N****** A G*******
Authorizer Telephone
7136464376
Authorizer Email
N***************@p*****.com
Narrative
Approximately 91 barrels of crude oil were released from a sump at oryx state line station. The date and time of the release (part a q4) are indicative of the earliest possible time the release could have started based on when a lightning storm caused a power outage at the station. The cause of the release is attributed to a valve misalignment following a severe thunderstorm (power outage) which prevented the pipeline from relieving to tankage. To prevent future incidents, the valve position was corrected and the individual was re-trained.
Report Received Date | 2025-08-22 00:00:00 |
---|---|
Iyear | 2025 |
Report Number | 20250196 |
Supplemental Number | 41292 |
Report Type | Original Final |
Operator Id | 39654 PHMSA Enforcement |
Name | Oryx Delaware Oil Transport Llc |
Operator Street Address | 333 Clay St. Suite 1900 |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 31.967744 Google Maps OpenStreetMap |
Location Longitude | -103.738853 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 91 |
Recovered Bbls | 91 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Oryx State Line |
Segment Name | Sump |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 79754 |
Onshore City Name | Mentone |
Onshore County Name | Loving |
Designated Location | Milepost |
Designated Name | 0+00 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Sump |
Installation Year | 2017 |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Overfill Or Overflow |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 350 |
Est Cost Prop Damage | 2500 |
Est Cost Emergency | 20000 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 22850 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 1200 |
Mop Psig | 285 |
Mop Cfr Section | Component Design Pressure �195.406(A)(2) View CFR 49 §192 |
Maop Established Date | 2017-01-01 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Exceeded 110% Of Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | Yes, specify investigation result(s): (select all that apply) |
Invest Schedule Ind | Yes |
Invest No Control Room Ind | Yes |
Invest No Controller Ind | Yes |
Employee Drug Test Ind | Yes |
Contractor Drug Test Ind | No |
Num Employees Tested | 1 |
Num Employees Failed | 0 |
Cause | Incorrect Operation |
Cause Details | Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow |
Operation Type | Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow |
Overflow Other Ind | Valve Misalignment |
Related Failure Follow Ind | Yes |
Category Type | Other Maintenance |
Operator Qualification Ind | Yes |
Qualified Individuals | Yes, They Were Qualified For The Task(S) |
Nf Lightning Ind | Yes |
Preparer Name | N****** G******* |
Preparer Title | Hse Regulatory Compliance Supervisor |
Preparer Email | N***************@p*****.com |
Preparer Telephone | 7136464376 |
Prepared Date | 2025-08-22 00:00:00 |
Local Contact Name | N****** A G******* |
Local Contact Email | N***************@p*****.com |
Local Contact Telephone | 7136464376 |
Authorizer Name | N****** A G******* |
Authorizer Telephone | 7136464376 |
Authorizer Email | N***************@p*****.com |
Narrative | Approximately 91 barrels of crude oil were released from a sump at oryx state line station. The date and time of the release (part a q4) are indicative of the earliest possible time the release could have started based on when a lightning storm caused a power outage at the station. The cause of the release is attributed to a valve misalignment following a severe thunderstorm (power outage) which prevented the pipeline from relieving to tankage. To prevent future incidents, the valve position was corrected and the individual was re-trained. |
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