HL incident on 2025-07-17 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2025-07-17 00:00 UTC
Report number
Location
TX
Narrative
On 6/17/2025 at 6:45 am cst enterprise pipeline operator discovered a crude oil release on pipeline fitting at echo station. The leak was immediately isolated. Approximately 0.24 barrels of crude oil was released. Upon further investigation, it was determined that improper installation of fitting connection caused the crude oil release. The line has been isolated and removed from service.
Detailed record list
Report Received Date
2025-07-17 00:00:00
Iyear
2025
Report Number
20250170
Supplemental Number
41153
Report Type
Original Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.24
Recovered Bbls
0.24
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
6/17/2025 7:15
Num Pub Evacuated
0
Pipe Fac Name
Echo Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
77034
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost
Designated Name
0+0.00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Tubing Material
Carbon Steel
Tubing Type
Rigid
Installation Year
2019
Manufactured Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
0
Est Cost Emergency
42000
Est Cost Environmental
0
Est Cost Other
0
Prpty
42020
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
0
Mop Psig
275
Mop Cfr Section
Four Hour Test Or Operation �195.406(A)(5)
Maop Established Date
2019-01-14 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Improper installation of the tubing on pressure control valve.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Io Not Installed Properly Ind
Yes
Preparer Name
M****** K********
Preparer Title
Pipeline Compliance Engineer
Preparer Email
M*********@e****.com
Preparer Telephone
713-376-9799
Prepared Date
2025-07-17 00:00:00
Local Contact Name
M****** K********
Local Contact Email
M*********@e****.com
Local Contact Telephone
713-376-9799
Authorizer Name
S**** D****
Authorizer Telephone
713-381-5585
Authorizer Title
Senior Manager Compliance
Authorizer Email
S******@e****.com
Narrative
On 6/17/2025 at 6:45 am cst enterprise pipeline operator discovered a crude oil release on pipeline fitting at echo station. The leak was immediately isolated. Approximately 0.24 barrels of crude oil was released. Upon further investigation, it was determined that improper installation of fitting connection caused the crude oil release. The line has been isolated and removed from service.
Report Received Date 2025-07-17 00:00:00
Iyear 2025
Report Number 20250170
Supplemental Number 41153
Report Type Original Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.612389 Google Maps OpenStreetMap
Location Longitude -95.182861 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.24
Recovered Bbls 0.24
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind No
Oil Spill Removal Org Ind Yes
Osro Arrived On Site Dt 6/17/2025 7:15
Num Pub Evacuated 0
Pipe Fac Name Echo Terminal
Onshore State Abbreviation Tx
Onshore Postal Code 77034
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost
Designated Name 0+0.00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Tubing Material Carbon Steel
Tubing Type Rigid
Installation Year 2019
Manufactured Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 0
Est Cost Emergency 42000
Est Cost Environmental 0
Est Cost Other 0
Prpty 42020
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 0
Mop Psig 275
Mop Cfr Section Four Hour Test Or Operation �195.406(A)(5) View CFR 49 §192
Maop Established Date 2019-01-14 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Improper installation of the tubing on pressure control valve.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Failure Follow Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Io Not Installed Properly Ind Yes
Preparer Name M****** K********
Preparer Title Pipeline Compliance Engineer
Preparer Email M*********@e****.com
Preparer Telephone 713-376-9799
Prepared Date 2025-07-17 00:00:00
Local Contact Name M****** K********
Local Contact Email M*********@e****.com
Local Contact Telephone 713-376-9799
Authorizer Name S**** D****
Authorizer Telephone 713-381-5585
Authorizer Title Senior Manager Compliance
Authorizer Email S******@e****.com
Narrative On 6/17/2025 at 6:45 am cst enterprise pipeline operator discovered a crude oil release on pipeline fitting at echo station. The leak was immediately isolated. Approximately 0.24 barrels of crude oil was released. Upon further investigation, it was determined that improper installation of fitting connection caused the crude oil release. The line has been isolated and removed from service.

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