Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2025-07-02 — TX
Operator
Capturepoint Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$21,000
Incident datetime
2025-07-02 00:00 UTC
Report number
Location
TX
Narrative
On june 2, 2025 at approximately 12:00 p.M. Cdt, a landowner notified austen pitts that there was a leak on the 4.5" texok CO2 pipeline row downstream of mlv8 at mp37.25. Mr. Pitts proceeded to the location to confirm the line failure at approximately 1:00 p.M. Cdt. The failed section of pipeline was isolated and the beaver county, oklahoma sherrif's office was notified of the plan to blowdown the failed section at 1:20 p.M. Cdt on 6/2/25. The planned blowdown was completed at 4:40 p.M. Cdt. Removed 13' of 4.5" pipe on 6/4/25 and welded in-place replacement section of pipe on 6/5/25. The line resumed operations on 6/12/25 at 5:00 p.M. Cdt. There were no injuries reported and no evacuations or public notification was necessary. Metallurgical engineering services, inc. (mes) performed a failure analysis which stated: "based on the comprehensive failure analysis conducted on the subject four-inch nominal pipe, the primary root cause of the failure was identified as weld defects within the circumferential girth weld, which were preferentially corroded from the inner diameter through the weld heat affected zone (haz) until the joint was compromised." based on their failure analysis, mes identified the primary root cause of the failure as, "...Weld defects within the girth weld haz, specifically undercuts, incomplete penetration due to poor alignment, and slag inclusions. These defects led to preferential corrosion attack, exacerbated by the presence of chalcogens, which resulted in the through hole failure. All relevant test outcomes supported these findings, confirming that the failure originated from weld-related issues rather than the base metal composition or mechanical properties."
Detailed record list
Report Received Date
2025-07-02 00:00:00
Iyear
2025
Report Number
20250163
Supplemental Number
41260
Report Type
Supplemental Final
Operator Id
39754
Name
Capturepoint Llc
Operator Street Address
1101 Central Expressway, South Suite 150
Operator City Name
Allen
Operator State Abbreviation
TX
Operator Postal Code
75013
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
36.764489
Location Longitude
-100.590862
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
34
Intentional Release Bbls
786
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Landowner Reported
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
1432910
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Texok Co2
Segment Name
Texok Co2 (F2193)
Onshore State Abbreviation
Ok
Onshore Postal Code
73932
Onshore City Name
Not Within A Municipality
Onshore County Name
Beaver
Designated Location
Milepost
Designated Name
Mp37.25
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
96
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
4.5
Pipe Wall Thickness
0.125
Pipe Smys
42000
Pipe Specification
Api5l X42
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Seah
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Coating Applied Ind
No
Weld Subtype
Pipe Girth Weld
Different Girth Weld Ind
No
Installation Year
2015
Manufactured Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
Yes
Vegetation Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1200
Est Cost Prop Damage
21000
Est Cost Emergency
1000
Est Cost Environmental
0
Est Cost Other
1000
Est Cost Other Details
Working With Landowner To Determine Remediation Needed For Landowner's Property.
Prpty
24200
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1175
Mop Psig
1677
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2015-09-06 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
44880
Internal Inspection Ind
No
Tight Mitered Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pressure and temperature transmitters did not indicate a leak and the controllers did not see any changes in pressure or temperature to indicate a leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Significant Undercuts At The Toe Of Gw, Adjacent To Ds Side Of Weld Cap
Pwf Addl Misalignment Ind
Yes
Pwf Additional Other Ind
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2015
Hydrtst Most Rcnt Pressure
2170
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Extrnl Cor Galvanic Ind
Yes
Pwf Installation Ind
Yes
Preparer Name
H***** U*****
Preparer Title
Regulatory Consultant
Preparer Email
H************@e*********.com
Preparer Telephone
9364476100
Prepared Date
2025-08-15 00:00:00
Local Contact Name
P*** A*******
Local Contact Email
P********@c******.com
Local Contact Telephone
5012695215
Authorizer Name
T***** C******
Authorizer Telephone
9187280133
Authorizer Title
Director
Authorizer Email
T*******@c**************.com
Narrative
On june 2, 2025 at approximately 12:00 p.M. Cdt, a landowner notified austen pitts that there was a leak on the 4.5" texok CO2 pipeline row downstream of mlv8 at mp37.25. Mr. Pitts proceeded to the location to confirm the line failure at approximately 1:00 p.M. Cdt. The failed section of pipeline was isolated and the beaver county, oklahoma sherrif's office was notified of the plan to blowdown the failed section at 1:20 p.M. Cdt on 6/2/25. The planned blowdown was completed at 4:40 p.M. Cdt. Removed 13' of 4.5" pipe on 6/4/25 and welded in-place replacement section of pipe on 6/5/25. The line resumed operations on 6/12/25 at 5:00 p.M. Cdt. There were no injuries reported and no evacuations or public notification was necessary. Metallurgical engineering services, inc. (mes) performed a failure analysis which stated: "based on the comprehensive failure analysis conducted on the subject four-inch nominal pipe, the primary root cause of the failure was identified as weld defects within the circumferential girth weld, which were preferentially corroded from the inner diameter through the weld heat affected zone (haz) until the joint was compromised." based on their failure analysis, mes identified the primary root cause of the failure as, "...Weld defects within the girth weld haz, specifically undercuts, incomplete penetration due to poor alignment, and slag inclusions. These defects led to preferential corrosion attack, exacerbated by the presence of chalcogens, which resulted in the through hole failure. All relevant test outcomes supported these findings, confirming that the failure originated from weld-related issues rather than the base metal composition or mechanical properties."
Report Received Date | 2025-07-02 00:00:00 |
---|---|
Iyear | 2025 |
Report Number | 20250163 |
Supplemental Number | 41260 |
Report Type | Supplemental Final |
Operator Id | 39754 PHMSA Enforcement |
Name | Capturepoint Llc |
Operator Street Address | 1101 Central Expressway, South Suite 150 |
Operator City Name | Allen |
Operator State Abbreviation | TX |
Operator Postal Code | 75013 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 36.764489 Google Maps OpenStreetMap |
Location Longitude | -100.590862 Google Maps OpenStreetMap |
Commodity Released Type | Co2 (Carbon Dioxide) |
Unintentional Release Bbls | 34 |
Intentional Release Bbls | 786 |
Recovered Bbls | 0 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Other |
Accident Details | Landowner Reported |
System Part Involved | Onshore Pipeline, Including Valve Sites |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | 1432910 NRC Report How to search |
Ignite Ind | No |
Upstream Action Taken | Valve Closure |
Upstream Valve Type Ind | Manual |
Downstream Action Taken | Valve Closure |
Downstream Valve Type Ind | Manual |
Num Pub Evacuated | 0 |
Pipe Fac Name | Texok Co2 |
Segment Name | Texok Co2 (F2193) |
Onshore State Abbreviation | Ok |
Onshore Postal Code | 73932 |
Onshore City Name | Not Within A Municipality |
Onshore County Name | Beaver |
Designated Location | Milepost |
Designated Name | Mp37.25 |
Federal | No |
Location Type | Pipeline Right-Of-Way |
Incident Area Type | Underground |
Incident Area Subtype | Under Soil |
Depth Of Cover | 96 |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Weld, Including Heat-Affected Zone |
Pipe Diameter | 4.5 |
Pipe Wall Thickness | 0.125 |
Pipe Smys | 42000 |
Pipe Specification | Api5l X42 |
Pipe Seam Type | Erw - High Frequency |
Pipe Manufacturer | Seah |
Pipe Coating Type | Fusion Bonded Epoxy(Fbe) |
Coating Applied Ind | No |
Weld Subtype | Pipe Girth Weld |
Different Girth Weld Ind | No |
Installation Year | 2015 |
Manufactured Year | 2014 |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Pinhole |
Wildlife Impact Ind | No |
Soil Contamination | No |
Long Term Assessment | No |
Remediation Ind | Yes |
Vegetation Remed Ind | Yes |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 1200 |
Est Cost Prop Damage | 21000 |
Est Cost Emergency | 1000 |
Est Cost Environmental | 0 |
Est Cost Other | 1000 |
Est Cost Other Details | Working With Landowner To Determine Remediation Needed For Landowner's Property. |
Prpty | 24200 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 1175 |
Mop Psig | 1677 |
Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
Maop Established Date | 2015-09-06 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Length Segment Isolated | 44880 |
Internal Inspection Ind | No |
Tight Mitered Ind | Yes |
Operation Complications Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Pressure and temperature transmitters did not indicate a leak and the controllers did not see any changes in pressure or temperature to indicate a leak. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Material Failure Of Pipe Or Weld |
Cause Details | Design-, Construction-, Installation-, Or Fabrication-Related |
Field Exam Ind | Yes |
Metallurgical Ind | Yes |
Failure Type | Design-, Construction-, Installation-, Or Fabrication-Related |
Other Factor | Yes |
Other Factor Details | Significant Undercuts At The Toe Of Gw, Adjacent To Ds Side Of Weld Cap |
Pwf Addl Misalignment Ind | Yes |
Pwf Additional Other Ind | Yes |
Collected Data Ind | No |
Has Hydrtst Conduc Before Ind | Yes |
Hydrtst Most Rcnt Year | 2015 |
Hydrtst Most Rcnt Pressure | 2170 |
Direct Asmnt Conducted | No |
Non Destructive Exam Ind | No |
Extrnl Cor Galvanic Ind | Yes |
Pwf Installation Ind | Yes |
Preparer Name | H***** U***** |
Preparer Title | Regulatory Consultant |
Preparer Email | H************@e*********.com |
Preparer Telephone | 9364476100 |
Prepared Date | 2025-08-15 00:00:00 |
Local Contact Name | P*** A******* |
Local Contact Email | P********@c******.com |
Local Contact Telephone | 5012695215 |
Authorizer Name | T***** C****** |
Authorizer Telephone | 9187280133 |
Authorizer Title | Director |
Authorizer Email | T*******@c**************.com |
Narrative | On june 2, 2025 at approximately 12:00 p.M. Cdt, a landowner notified austen pitts that there was a leak on the 4.5" texok CO2 pipeline row downstream of mlv8 at mp37.25. Mr. Pitts proceeded to the location to confirm the line failure at approximately 1:00 p.M. Cdt. The failed section of pipeline was isolated and the beaver county, oklahoma sherrif's office was notified of the plan to blowdown the failed section at 1:20 p.M. Cdt on 6/2/25. The planned blowdown was completed at 4:40 p.M. Cdt. Removed 13' of 4.5" pipe on 6/4/25 and welded in-place replacement section of pipe on 6/5/25. The line resumed operations on 6/12/25 at 5:00 p.M. Cdt. There were no injuries reported and no evacuations or public notification was necessary. Metallurgical engineering services, inc. (mes) performed a failure analysis which stated: "based on the comprehensive failure analysis conducted on the subject four-inch nominal pipe, the primary root cause of the failure was identified as weld defects within the circumferential girth weld, which were preferentially corroded from the inner diameter through the weld heat affected zone (haz) until the joint was compromised." based on their failure analysis, mes identified the primary root cause of the failure as, "...Weld defects within the girth weld haz, specifically undercuts, incomplete penetration due to poor alignment, and slag inclusions. These defects led to preferential corrosion attack, exacerbated by the presence of chalcogens, which resulted in the through hole failure. All relevant test outcomes supported these findings, confirming that the failure originated from weld-related issues rather than the base metal composition or mechanical properties." |
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