Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2025-06-18 — TX
Operator
Energy Transfer Company
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2025-06-18 00:00 UTC
Report number
Location
TX
Narrative
On 05/23/25 at approximately 07:58, a local operator employee closed mov 6001 causing the 24inch midland mesa c20017 line to overpressure, which led to a release of crude oil onto the ground. The line was immediately shutdown and isolated. The leak was discovered to be coming from a flange. Flanges were retorqued to stop leak, the line was inspected visually and was returned to service. Approximately 1 barrel of crude oil was released. Cleanup contractors removed product and remediated impacted soil. The cause of the accident is still under investigation. A supplemental report will be submitted once complete. Supplemental & final: the investigation determined the cause of the accident was due to incorrect operation leading to an overpressure. The field operator did not properly communicate with the control center prior to operating valves. To prevent reoccurrence, the delivery/receipt operating procedure has been updated to include valves in use and expanded communication guidance. The field operator's associated covered task qualifications were suspended and the individual was retrained and qualifications reinstated.
Detailed record list
Report Received Date
2025-06-18 00:00:00
Iyear
2025
Report Number
20250151
Supplemental Number
41206
Report Type
Supplemental Final
Operator Id
32099
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
32.00959
Location Longitude
-102.03685
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Midland Tank Farm
Segment Name
24inch Midland Mesa C20017
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Not Within A Municipality
Onshore County Name
Midland
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
2012
Manufactured Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
33
Est Cost Prop Damage
0
Est Cost Emergency
1955
Est Cost Environmental
183
Est Cost Other
0
Prpty
2171
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
420
Mop Psig
285
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2012-05-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Pipeline Or Equipment Overpressured
Operation Type
Pipeline Or Equipment Overpressured
Related Inadequate Proc Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
T*** N*******
Preparer Title
Director - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2025-08-01 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 05/23/25 at approximately 07:58, a local operator employee closed mov 6001 causing the 24inch midland mesa c20017 line to overpressure, which led to a release of crude oil onto the ground. The line was immediately shutdown and isolated. The leak was discovered to be coming from a flange. Flanges were retorqued to stop leak, the line was inspected visually and was returned to service. Approximately 1 barrel of crude oil was released. Cleanup contractors removed product and remediated impacted soil. The cause of the accident is still under investigation. A supplemental report will be submitted once complete. Supplemental & final: the investigation determined the cause of the accident was due to incorrect operation leading to an overpressure. The field operator did not properly communicate with the control center prior to operating valves. To prevent reoccurrence, the delivery/receipt operating procedure has been updated to include valves in use and expanded communication guidance. The field operator's associated covered task qualifications were suspended and the individual was retrained and qualifications reinstated.
Report Received Date | 2025-06-18 00:00:00 |
---|---|
Iyear | 2025 |
Report Number | 20250151 |
Supplemental Number | 41206 |
Report Type | Supplemental Final |
Operator Id | 32099 PHMSA Enforcement |
Name | Energy Transfer Company |
Operator Street Address | 1300 Main Street |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 32.00959 Google Maps OpenStreetMap |
Location Longitude | -102.03685 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 1 |
Recovered Bbls | 1 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Notify Qualified Indiv Ind | No |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Midland Tank Farm |
Segment Name | 24inch Midland Mesa C20017 |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 79706 |
Onshore City Name | Not Within A Municipality |
Onshore County Name | Midland |
Designated Location | Survey Station No. |
Designated Name | 0+00 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Intrastate |
Item Involved | Flange Assembly |
Installation Year | 2012 |
Manufactured Year | 2012 |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Seal Or Packing |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | Yes |
Soil Remed Ind | Yes |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 33 |
Est Cost Prop Damage | 0 |
Est Cost Emergency | 1955 |
Est Cost Environmental | 183 |
Est Cost Other | 0 |
Prpty | 2171 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 420 |
Mop Psig | 285 |
Mop Cfr Section | Component Design Pressure �195.406(A)(2) View CFR 49 §192 |
Maop Established Date | 2012-05-01 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Exceeded 110% Of Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | A review of the accident determined that there were no control room actions that contributed to the event. |
Employee Drug Test Ind | Yes |
Contractor Drug Test Ind | No |
Num Employees Tested | 1 |
Num Employees Failed | 0 |
Cause | Incorrect Operation |
Cause Details | Pipeline Or Equipment Overpressured |
Operation Type | Pipeline Or Equipment Overpressured |
Related Inadequate Proc Ind | Yes |
Category Type | Normal Operating Conditions |
Operator Qualification Ind | Yes |
Qualified Individuals | Yes, They Were Qualified For The Task(S) |
Preparer Name | T*** N******* |
Preparer Title | Director - Dot Compliance |
Preparer Email | T************@e*************.com |
Preparer Telephone | 713-989-7126 |
Prepared Date | 2025-08-01 00:00:00 |
Authorizer Name | T*** N******* |
Authorizer Telephone | 713-989-7126 |
Authorizer Title | Director - Dot Compliance |
Authorizer Email | T************@e*************.com |
Narrative | On 05/23/25 at approximately 07:58, a local operator employee closed mov 6001 causing the 24inch midland mesa c20017 line to overpressure, which led to a release of crude oil onto the ground. The line was immediately shutdown and isolated. The leak was discovered to be coming from a flange. Flanges were retorqued to stop leak, the line was inspected visually and was returned to service. Approximately 1 barrel of crude oil was released. Cleanup contractors removed product and remediated impacted soil. The cause of the accident is still under investigation. A supplemental report will be submitted once complete. Supplemental & final: the investigation determined the cause of the accident was due to incorrect operation leading to an overpressure. The field operator did not properly communicate with the control center prior to operating valves. To prevent reoccurrence, the delivery/receipt operating procedure has been updated to include valves in use and expanded communication guidance. The field operator's associated covered task qualifications were suspended and the individual was retrained and qualifications reinstated. |
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