HL incident on 2025-06-05 — TX

Operator
Permian Express Partners Llc
Cause
Other Accident Cause
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000,000
Incident datetime
2025-06-05 00:00 UTC
Report number
Location
TX
Narrative
On 05/05/2025 at approximately 06:23, the control center received scada indications of a release on the keller to midlothian segment of the 16-inch ringgold to corsicana system. The line was shutdown and upstream and downstream valves closed to isolate the segment. Operations personnel were dispatched and began field investigations to locate a potential release. On 05/06/2025 at approximately 14:10, field personnel discovered crude oil on the ground near mp 90.82 in the arlington/ft. Worth area. Once excavated, both crude oil and sewer water were discovered in the excavation. The location of the leak was where a 48-inch city of fort worth sewer line crossed under the keller to midlothian segment. Investigation in the ditch found the concrete sewer line appeared to have failed and was expelling sewage into the the immediate area in and around the keller to midlothian pipeline. Approximately 6,600 barrels of crude oil was released. The majority of the released crude traveled through the failed sewer pipe to a water treatment facility approximately 4 miles to the northeast. Cleanup contractors were mobilized to cleanup product and remove impacted soil at the failure site. Pep coordinated cleanup efforts at the water treatment facility with the city. The line was restarted on 5/9/25 at 22:00 by affecting a stopple and bypass around the failed section. After the pipeline was restarted the failed section was cold cut and removed from the ground, prepped and shipped to a 3rd party laboratory for analysis. The cause of the accident is still under investigation. A supplemental report will be submitted once complete.
Detailed record list
Report Received Date
2025-06-05 00:00:00
Iyear
2025
Report Number
20250139
Supplemental Number
40994
Report Type
Original
Operator Id
Name
Permian Express Partners Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
6600
Recovered Bbls
6600
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Additional Nrc Report Numbers
1430457
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
5/6/2025 18:00
Num Pub Evacuated
0
Pipe Fac Name
Ringgold To Corsicana
Segment Name
22002.01 - 16inch Corsicana To Keller
Onshore State Abbreviation
Tx
Onshore Postal Code
76013
Onshore City Name
Arlington
Onshore County Name
Tarrant
Designated Location
Milepost
Designated Name
90.82
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
64
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
16
Pipe Wall Thickness
0.25
Pipe Smys
42000
Pipe Specification
Api-5l X-42
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Coating Applied Ind
Unknown
Installation Year
1953
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Still Under Investigation
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
7600000
Est Cost Gas Released
0
Est Cost Prop Damage
1000000
Est Cost Emergency
100000
Est Cost Environmental
2000
Est Cost Other
0
Prpty
8702000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
773
Mop Psig
811
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
1998-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
120331
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required)
Preparer Name
T*** N*******
Preparer Title
Director - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2025-06-05 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 05/05/2025 at approximately 06:23, the control center received scada indications of a release on the keller to midlothian segment of the 16-inch ringgold to corsicana system. The line was shutdown and upstream and downstream valves closed to isolate the segment. Operations personnel were dispatched and began field investigations to locate a potential release. On 05/06/2025 at approximately 14:10, field personnel discovered crude oil on the ground near mp 90.82 in the arlington/ft. Worth area. Once excavated, both crude oil and sewer water were discovered in the excavation. The location of the leak was where a 48-inch city of fort worth sewer line crossed under the keller to midlothian segment. Investigation in the ditch found the concrete sewer line appeared to have failed and was expelling sewage into the the immediate area in and around the keller to midlothian pipeline. Approximately 6,600 barrels of crude oil was released. The majority of the released crude traveled through the failed sewer pipe to a water treatment facility approximately 4 miles to the northeast. Cleanup contractors were mobilized to cleanup product and remove impacted soil at the failure site. Pep coordinated cleanup efforts at the water treatment facility with the city. The line was restarted on 5/9/25 at 22:00 by affecting a stopple and bypass around the failed section. After the pipeline was restarted the failed section was cold cut and removed from the ground, prepped and shipped to a 3rd party laboratory for analysis. The cause of the accident is still under investigation. A supplemental report will be submitted once complete.
Report Received Date 2025-06-05 00:00:00
Iyear 2025
Report Number 20250139
Supplemental Number 40994
Report Type Original
Operator Id 39596 PHMSA Enforcement
Name Permian Express Partners Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 32.728841 Google Maps OpenStreetMap
Location Longitude -97.189752 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 6600
Recovered Bbls 6600
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num 1430396 NRC Report How to search
Additional Nrc Report Numbers 1430457
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Remotely Controlled
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind Yes
Osro Arrived On Site Dt 5/6/2025 18:00
Num Pub Evacuated 0
Pipe Fac Name Ringgold To Corsicana
Segment Name 22002.01 - 16inch Corsicana To Keller
Onshore State Abbreviation Tx
Onshore Postal Code 76013
Onshore City Name Arlington
Onshore County Name Tarrant
Designated Location Milepost
Designated Name 90.82
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 64
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 16
Pipe Wall Thickness 0.25
Pipe Smys 42000
Pipe Specification Api-5l X-42
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Coating Applied Ind Unknown
Installation Year 1953
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Still Under Investigation
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 7600000
Est Cost Gas Released 0
Est Cost Prop Damage 1000000
Est Cost Emergency 100000
Est Cost Environmental 2000
Est Cost Other 0
Prpty 8702000
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 773
Mop Psig 811
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 1998-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 120331
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required)
Preparer Name T*** N*******
Preparer Title Director - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Prepared Date 2025-06-05 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Director - Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 05/05/2025 at approximately 06:23, the control center received scada indications of a release on the keller to midlothian segment of the 16-inch ringgold to corsicana system. The line was shutdown and upstream and downstream valves closed to isolate the segment. Operations personnel were dispatched and began field investigations to locate a potential release. On 05/06/2025 at approximately 14:10, field personnel discovered crude oil on the ground near mp 90.82 in the arlington/ft. Worth area. Once excavated, both crude oil and sewer water were discovered in the excavation. The location of the leak was where a 48-inch city of fort worth sewer line crossed under the keller to midlothian segment. Investigation in the ditch found the concrete sewer line appeared to have failed and was expelling sewage into the the immediate area in and around the keller to midlothian pipeline. Approximately 6,600 barrels of crude oil was released. The majority of the released crude traveled through the failed sewer pipe to a water treatment facility approximately 4 miles to the northeast. Cleanup contractors were mobilized to cleanup product and remove impacted soil at the failure site. Pep coordinated cleanup efforts at the water treatment facility with the city. The line was restarted on 5/9/25 at 22:00 by affecting a stopple and bypass around the failed section. After the pipeline was restarted the failed section was cold cut and removed from the ground, prepped and shipped to a 3rd party laboratory for analysis. The cause of the accident is still under investigation. A supplemental report will be submitted once complete.

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