HL incident on 2025-06-03 — TX

Operator
Enterprise Products Operating Llc
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$250,000
Incident datetime
2025-06-03 00:00 UTC
Report number
Location
TX
Narrative
On 5/4/2025 at approximately 9:24 am mst, a local landowner notified enterprise of a potential leak on the rocky mountain line (lid 702). The line was isolated and shutdown. Amount released is estimated to be 80 barrels. Nrc reportable based on the cost of remediation. Cause of leak was due to stray current interference resulting from a loose negative connection in the junction box. The damaged pipe was cutout, replaced and put back in service. After investigation of the junction box, it was discovered the local livestock used the equipment as a scratching post resulting in the connection to fail. Box will be protected from this in the future.
Detailed record list
Report Received Date
2025-06-03 00:00:00
Iyear
2025
Report Number
20250137
Supplemental Number
41097
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Mountain
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
80
Recovered Bbls
80
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Additional Nrc Report Numbers
1430437
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Rocky Mountain
Segment Name
Four Corners Lateral Loop
Onshore State Abbreviation
Nm
Onshore Postal Code
88260
Onshore City Name
Not Within A Municipality
Onshore County Name
Lea
Designated Location
Milepost
Designated Name
34
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
12.75
Pipe Wall Thickness
0.225
Pipe Smys
65000
Pipe Specification
Api-5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
American Steel
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Coating Applied Ind
Unknown
Installation Year
1996
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
15000
Est Cost Gas Released
12000
Est Cost Prop Damage
250000
Est Cost Emergency
25000
Est Cost Environmental
50000
Est Cost Other
0
Prpty
352000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
760
Mop Psig
1607
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
1980-10-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
58080
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No issues with control room that warranted an investigation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Stray Current Corrosion Ind
Yes
Stray Current Type
Direct Current
Stray Current Details
Junction Box Was Loose (Negative Connection)
Field Exam Basis Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1996
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2024
Close Interval Survey Year
2025
Other Cp Survey Details
Cp Survey And Close Interval Survey After Release In May 2025.
Prior Damage
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2022
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
Standard Resolution
Axial Previous Year
2011
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
Standard Resolution
Geometry Recent Year
2022
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
Standard Resolution
Geometrt Rcnt Measur Cups
No Cups
Geometry Previous Year
2011
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
Standard Resolution
Geometrt Prev Measur Cups
No Cups
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
A***** A******** I*
Preparer Title
Pipeline Engineer
Preparer Email
A***********@e****.com
Preparer Telephone
713-3813659
Prepared Date
2025-07-01 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713-381-5585
Authorizer Title
Sr. Compliance Manager
Authorizer Email
S******@e****.com
Narrative
On 5/4/2025 at approximately 9:24 am mst, a local landowner notified enterprise of a potential leak on the rocky mountain line (lid 702). The line was isolated and shutdown. Amount released is estimated to be 80 barrels. Nrc reportable based on the cost of remediation. Cause of leak was due to stray current interference resulting from a loose negative connection in the junction box. The damaged pipe was cutout, replaced and put back in service. After investigation of the junction box, it was discovered the local livestock used the equipment as a scratching post resulting in the connection to fail. Box will be protected from this in the future.
Report Received Date 2025-06-03 00:00:00
Iyear 2025
Report Number 20250137
Supplemental Number 41097
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Mountain
Daylight Savings Ind Yes
Location Latitude 33.09021 Google Maps OpenStreetMap
Location Longitude -103.40893 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 80
Recovered Bbls 80
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num 1430176 NRC Report How to search
Additional Nrc Report Numbers 1430437
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Remotely Controlled
Notify Qualified Indiv Ind No
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Rocky Mountain
Segment Name Four Corners Lateral Loop
Onshore State Abbreviation Nm
Onshore Postal Code 88260
Onshore City Name Not Within A Municipality
Onshore County Name Lea
Designated Location Milepost
Designated Name 34
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 12.75
Pipe Wall Thickness 0.225
Pipe Smys 65000
Pipe Specification Api-5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer American Steel
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Coating Applied Ind Unknown
Installation Year 1996
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 15000
Est Cost Gas Released 12000
Est Cost Prop Damage 250000
Est Cost Emergency 25000
Est Cost Environmental 50000
Est Cost Other 0
Prpty 352000
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 760
Mop Psig 1607
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 1980-10-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 58080
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No issues with control room that warranted an investigation.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Stray Current Corrosion Ind Yes
Stray Current Type Direct Current
Stray Current Details Junction Box Was Loose (Negative Connection)
Field Exam Basis Ind Yes
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1996
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2024
Close Interval Survey Year 2025
Other Cp Survey Details Cp Survey And Close Interval Survey After Release In May 2025.
Prior Damage Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2022
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal Standard Resolution
Axial Previous Year 2011
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal Standard Resolution
Geometry Recent Year 2022
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution Standard Resolution
Geometrt Rcnt Measur Cups No Cups
Geometry Previous Year 2011
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution Standard Resolution
Geometrt Prev Measur Cups No Cups
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name A***** A******** I*
Preparer Title Pipeline Engineer
Preparer Email A***********@e****.com
Preparer Telephone 713-3813659
Prepared Date 2025-07-01 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 713-381-5585
Authorizer Title Sr. Compliance Manager
Authorizer Email S******@e****.com
Narrative On 5/4/2025 at approximately 9:24 am mst, a local landowner notified enterprise of a potential leak on the rocky mountain line (lid 702). The line was isolated and shutdown. Amount released is estimated to be 80 barrels. Nrc reportable based on the cost of remediation. Cause of leak was due to stray current interference resulting from a loose negative connection in the junction box. The damaged pipe was cutout, replaced and put back in service. After investigation of the junction box, it was discovered the local livestock used the equipment as a scratching post resulting in the connection to fail. Box will be protected from this in the future.

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