GTG incident on 2025-10-22 — TX

Operator
Energy Transfer Company
Cause
Other Incident Cause
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$880,026
Incident datetime
2025-10-22 09:37
Report number
Location
TX
Narrative
On october 22, 2025, at 6:30 a.M. While investigating line shut-ins and compressor shutdowns due to high o2 issues an operations (ops) tech observed that the headlee discharge line had 40 psig when the normal operating pressure is 1250 pisig. The employee notified the ops supervisor who then verified the line pressure with another ops tech located at the lupin station. At 6:40 a.M. The ops team began a leak investigation on the 7406642 - lupin to headlee. At 09:37 a.M. Field personnel pinpoint the location the leak. The line was shut in and field personnel began to investigate the severity of the leak. At 11:15 a.M. Operations made an initial determination that the leak may exceed the reportable threshold and notified DOT compliance. The nrc notification was made at 12:06 p.M. Txrrc notification was made at 12:15 p.M. The investigation is ongoing.
Detailed record list
Report Received Date
2025-11-20 00:00:00
Iyear
2025
Report Number
20250128
Supplemental Number
41611
Report Type
Original
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2025-10-22 06:30:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2025-10-22 12:06:00
Additional Nrc Report Numbers
1446170
Commodity Released Type
Natural Gas
Unintentional Release
7784
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2025-10-22 10:15:00
Restart Datetime
2025-10-26 02:00:00
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2025-10-22 10:15:00
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2025-10-22 10:00:00
Num Pub Evacuated
0
Incident Identified Datetime
2025-10-22 09:37:00
On Site Datetime
2025-10-22 09:37:00
Confirmed Discovery Datetime
2025-10-22 21:39:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Odessa
Onshore County Name
Midland
Designated Location
Not Applicable
Pipe Fac Name
7406642 � Lupin To Headlee
Segment Name
7406642
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
12.75
Pipe Wall Thickness
0.25
Pipe Smys
52000
Pipe Specification
X-52
Pipe Seam Type
Longitudinal Erw - Unknown Frequency
Pipe Manufacturer
Womble
Pipe Coating Type
Epoxy
Coating Applied Ind
No
Installation Year
2022
Manufactured Year
2022
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Length
216
Rupture Width
9
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
660
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
26855
Est Cost Intentional Release
0
Est Cost Prop Damage
880026
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
3.45
Prpty
906881
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
1250
Gas Flow In Pipe In Mcf
13500
Mop Psig
1440
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2022-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
44697
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Type C Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status
Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Incident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Still Under Investigation, Cause Of Incident To Be Determined* (*supplemental Report Required)
Preparer Name
T*** P******
Preparer Title
Sr. Specialist Dot Compliance
Preparer Email
T***********@e*************.com
Preparer Telephone
4322656810
Local Contact Name
T*** P******
Local Contact Email
T***********@e*************.com
Local Contact Telephone
4322656810
Authorizer Name
J***** D*******
Authorizer Title
Manager Dot Compliance
Authorizer Telephone
7139895231
Authorizer Email
J**************@e*************.com
Narrative
On october 22, 2025, at 6:30 a.M. While investigating line shut-ins and compressor shutdowns due to high o2 issues an operations (ops) tech observed that the headlee discharge line had 40 psig when the normal operating pressure is 1250 pisig. The employee notified the ops supervisor who then verified the line pressure with another ops tech located at the lupin station. At 6:40 a.M. The ops team began a leak investigation on the 7406642 - lupin to headlee. At 09:37 a.M. Field personnel pinpoint the location the leak. The line was shut in and field personnel began to investigate the severity of the leak. At 11:15 a.M. Operations made an initial determination that the leak may exceed the reportable threshold and notified DOT compliance. The nrc notification was made at 12:06 p.M. Txrrc notification was made at 12:15 p.M. The investigation is ongoing.
Report Received Date 2025-11-20 00:00:00
Iyear 2025
Report Number 20250128
Supplemental Number 41611
Report Type Original
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2025-10-22 06:30:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 31.759878 Google Maps OpenStreetMap
Location Longitude -102.259267 Google Maps OpenStreetMap
Nrc Rpt Num 1446101 NRC Report How to search
Nrc Rpt Datetime 2025-10-22 12:06:00
Additional Nrc Report Numbers 1446170
Commodity Released Type Natural Gas
Unintentional Release 7784
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2025-10-22 10:15:00
Restart Datetime 2025-10-26 02:00:00
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2025-10-22 10:15:00
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2025-10-22 10:00:00
Num Pub Evacuated 0
Incident Identified Datetime 2025-10-22 09:37:00
On Site Datetime 2025-10-22 09:37:00
Confirmed Discovery Datetime 2025-10-22 21:39:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 79706
Onshore City Name Odessa
Onshore County Name Midland
Designated Location Not Applicable
Pipe Fac Name 7406642 � Lupin To Headlee
Segment Name 7406642
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Other Underground Facilities No
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 12.75
Pipe Wall Thickness 0.25
Pipe Smys 52000
Pipe Specification X-52
Pipe Seam Type Longitudinal Erw - Unknown Frequency
Pipe Manufacturer Womble
Pipe Coating Type Epoxy
Coating Applied Ind No
Installation Year 2022
Manufactured Year 2022
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Length 216
Rupture Width 9
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 660
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 26855
Est Cost Intentional Release 0
Est Cost Prop Damage 880026
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 3.45
Prpty 906881
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 1250
Gas Flow In Pipe In Mcf 13500
Mop Psig 1440
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 2022-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 44697
Internal Inspection Ind Yes
Operation Complications Ind Yes
Low Flow Ind Yes
Pipeline Function Type C Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Incident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Still Under Investigation, Cause Of Incident To Be Determined* (*supplemental Report Required)
Preparer Name T*** P******
Preparer Title Sr. Specialist Dot Compliance
Preparer Email T***********@e*************.com
Preparer Telephone 4322656810
Local Contact Name T*** P******
Local Contact Email T***********@e*************.com
Local Contact Telephone 4322656810
Authorizer Name J***** D*******
Authorizer Title Manager Dot Compliance
Authorizer Telephone 7139895231
Authorizer Email J**************@e*************.com
Narrative On october 22, 2025, at 6:30 a.M. While investigating line shut-ins and compressor shutdowns due to high o2 issues an operations (ops) tech observed that the headlee discharge line had 40 psig when the normal operating pressure is 1250 pisig. The employee notified the ops supervisor who then verified the line pressure with another ops tech located at the lupin station. At 6:40 a.M. The ops team began a leak investigation on the 7406642 - lupin to headlee. At 09:37 a.M. Field personnel pinpoint the location the leak. The line was shut in and field personnel began to investigate the severity of the leak. At 11:15 a.M. Operations made an initial determination that the leak may exceed the reportable threshold and notified DOT compliance. The nrc notification was made at 12:06 p.M. Txrrc notification was made at 12:15 p.M. The investigation is ongoing.

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