HL incident on 2025-05-16 — TX

Operator
Nustar Pipeline Operating Partnership L.p.
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2025-05-16 00:00 UTC
Report number
Location
TX
Narrative
At approximately 20:00 on 08may25, sunoco / nustar local personnel received a call from a landowner that they smelled ammonia anhydrous. Local personnel dispatched to the site, arriving at approximately 21:05 to begin walking the line and looking for a leak. The leak was confirmed at 21:32 with a call to ammonia system leadership. Sunoco / nustar pipeline safety personnel were notified of the release at 22:01 to begin the notification process with the national response center (nrc). A call was placed and received by the nrc at 22:19. Mr. Davis took the call and provided incident number 1430608. A follow-up call was received by region 6 epa at 23:06 requesting an update on the incident and an offer to provide assistance, if needed. A small vapor stream was identified coming from the upstream side of valve 3-27. Control center personnel were notified of the release and asked to shut down the pipeline (22:15). Local personnel were dispatched to close the upstream valve (3-25) and the downstream valve (3-27). Local personnel provided overnight air monitoring of the site. Visqueen was used to cover the leak and keep the vapors down. There was no danger to local residents and no notifications were made to local authorities. Sunoco / nustar maintenance personnel were called and dispatched to the site for repairs. Upon excavation of the valve site, a small crack was discovered on the side seam weld of a stopple tee. Repairs were completed and the line was returned to service at 18:45 on 09may25.
Detailed record list
Report Received Date
2025-05-16 00:00:00
Iyear
2025
Report Number
20250124
Supplemental Number
40896
Report Type
Original
Operator Id
Name
Nustar Pipeline Operating Partnership L.p.
Operator Street Address
8111 Westchester Drive
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75225
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
1
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Additional Nrc Report Numbers
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Automatic
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Nustar Ammonia System - Cabot Sta. To Floral Sta.
Segment Name
Cabot Station - 10" To Floral Station
Onshore State Abbreviation
Ar
Onshore Postal Code
72176
Onshore City Name
Not Within A Municipality
Onshore County Name
Lonoke
Designated Location
Milepost
Designated Name
146
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year
1997
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
60
Est Cost Prop Damage
10000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
10060
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
700
Mop Psig
1340
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
1969-04-12 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
36700
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The crack in the pipe was small enough it rendered the leak un-detectable by the control room (scada/cpm).
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Stopple Control Fitting Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Side Seam Weld On Stopple Tee.
Preparer Name
D*** S*****
Preparer Title
Manager - Pipeline Safety
Preparer Email
D**********@s*****.com
Preparer Telephone
3162459695
Prepared Date
2025-05-16 00:00:00
Local Contact Name
D*** S*****
Local Contact Email
D**********@s*****.com
Local Contact Telephone
3162459695
Authorizer Name
D*** S*****
Authorizer Telephone
3162459695
Authorizer Title
Manager - Pipeline Safety
Authorizer Email
D**********@s*****.com
Narrative
At approximately 20:00 on 08may25, sunoco / nustar local personnel received a call from a landowner that they smelled ammonia anhydrous. Local personnel dispatched to the site, arriving at approximately 21:05 to begin walking the line and looking for a leak. The leak was confirmed at 21:32 with a call to ammonia system leadership. Sunoco / nustar pipeline safety personnel were notified of the release at 22:01 to begin the notification process with the national response center (nrc). A call was placed and received by the nrc at 22:19. Mr. Davis took the call and provided incident number 1430608. A follow-up call was received by region 6 epa at 23:06 requesting an update on the incident and an offer to provide assistance, if needed. A small vapor stream was identified coming from the upstream side of valve 3-27. Control center personnel were notified of the release and asked to shut down the pipeline (22:15). Local personnel were dispatched to close the upstream valve (3-25) and the downstream valve (3-27). Local personnel provided overnight air monitoring of the site. Visqueen was used to cover the leak and keep the vapors down. There was no danger to local residents and no notifications were made to local authorities. Sunoco / nustar maintenance personnel were called and dispatched to the site for repairs. Upon excavation of the valve site, a small crack was discovered on the side seam weld of a stopple tee. Repairs were completed and the line was returned to service at 18:45 on 09may25.
Report Received Date 2025-05-16 00:00:00
Iyear 2025
Report Number 20250124
Supplemental Number 40896
Report Type Original
Operator Id 10012 PHMSA Enforcement
Name Nustar Pipeline Operating Partnership L.p.
Operator Street Address 8111 Westchester Drive
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75225
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 35.0248 Google Maps OpenStreetMap
Location Longitude -91.9321 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Anhydrous Ammonia
Unintentional Release Bbls 1
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num 1430608 NRC Report How to search
Additional Nrc Report Numbers No
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Automatic
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Nustar Ammonia System - Cabot Sta. To Floral Sta.
Segment Name Cabot Station - 10" To Floral Station
Onshore State Abbreviation Ar
Onshore Postal Code 72176
Onshore City Name Not Within A Municipality
Onshore County Name Lonoke
Designated Location Milepost
Designated Name 146
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year 1997
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 60
Est Cost Prop Damage 10000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 10060
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 700
Mop Psig 1340
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 1969-04-12 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 36700
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The crack in the pipe was small enough it rendered the leak un-detectable by the control room (scada/cpm).
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Stopple Control Fitting Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Side Seam Weld On Stopple Tee.
Preparer Name D*** S*****
Preparer Title Manager - Pipeline Safety
Preparer Email D**********@s*****.com
Preparer Telephone 3162459695
Prepared Date 2025-05-16 00:00:00
Local Contact Name D*** S*****
Local Contact Email D**********@s*****.com
Local Contact Telephone 3162459695
Authorizer Name D*** S*****
Authorizer Telephone 3162459695
Authorizer Title Manager - Pipeline Safety
Authorizer Email D**********@s*****.com
Narrative At approximately 20:00 on 08may25, sunoco / nustar local personnel received a call from a landowner that they smelled ammonia anhydrous. Local personnel dispatched to the site, arriving at approximately 21:05 to begin walking the line and looking for a leak. The leak was confirmed at 21:32 with a call to ammonia system leadership. Sunoco / nustar pipeline safety personnel were notified of the release at 22:01 to begin the notification process with the national response center (nrc). A call was placed and received by the nrc at 22:19. Mr. Davis took the call and provided incident number 1430608. A follow-up call was received by region 6 epa at 23:06 requesting an update on the incident and an offer to provide assistance, if needed. A small vapor stream was identified coming from the upstream side of valve 3-27. Control center personnel were notified of the release and asked to shut down the pipeline (22:15). Local personnel were dispatched to close the upstream valve (3-25) and the downstream valve (3-27). Local personnel provided overnight air monitoring of the site. Visqueen was used to cover the leak and keep the vapors down. There was no danger to local residents and no notifications were made to local authorities. Sunoco / nustar maintenance personnel were called and dispatched to the site for repairs. Upon excavation of the valve site, a small crack was discovered on the side seam weld of a stopple tee. Repairs were completed and the line was returned to service at 18:45 on 09may25.

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