GTG incident on 2025-10-05 — TX

Operator
Energy Transfer Company
Cause
Other Incident Cause
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$125,000
Incident datetime
2025-10-05 12:10
Report number
Location
TX
Narrative
On october 5th, 2025 at 12:10 p.M. Gas control received a call from a landowner reporting a leak in an et row. Operations was dispatched at 12:15pm and confirmed at 2:31 p.M. That the line was our 1090 sugar valley pipeline. The line was isolated by valve closure by 3:56 p.M. The next morning october 6th 2025 at 11:22 a.M. Calculations confirmed the incident to be reportable, due to the gas loss exceeding the reporting threshold. Permanent repairs (pipe replacement) were completed by october 10th 2025. The line was returned to service on october 24th, 2025 at 2:00 p.M. The pipe has been sent to a lab where the cause is pending the results of the metallurgical analysis.
Detailed record list
Report Received Date
2025-11-03 00:00:00
Iyear
2025
Report Number
20250122
Supplemental Number
41541
Report Type
Original
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2025-10-05 12:10:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2025-10-06 11:30:00
Additional Nrc Report Numbers
1444937
Commodity Released Type
Natural Gas
Unintentional Release
8964
Intentional Release
110
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2025-10-05 15:56:00
Restart Datetime
2025-10-24 14:00:00
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2025-10-05 15:56:00
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2025-10-05 15:56:00
Num Pub Evacuated
0
Incident Identified Datetime
2025-10-05 12:10:00
On Site Datetime
2025-10-05 14:31:00
Confirmed Discovery Datetime
2025-10-06 11:22:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
77414
Onshore City Name
Bay City
Onshore County Name
Matagorda
Designated Location
Survey Station No.
Designated Name
123+53
Pipe Fac Name
1090 Sugar Valley
Segment Name
1090 Sugar Valley
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Loss Of Cover
Depth Of Cover
42
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12.75
Puddle Weld Ind
No
Pipe Wall Thickness
0.25
Pipe Smys
24000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Coating Applied Ind
No
Installation Year
1953
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Length
40
Rupture Width
34
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
660
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
7500
Est Cost Unintentional Release
33884
Est Cost Intentional Release
416
Est Cost Prop Damage
125000
Est Cost Emergency
2000
Est Cost Other
0
Gas Cost In Mcf
3.78
Prpty
168800
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
467
Gas Flow In Pipe In Mcf
3700
Mop Psig
500
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2011-07-28 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Gas Odorized Ind
Yes
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
39847
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Other
Accident Details
Notification From Land Owner
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No fatigue or drug/alcohol indications, no issues with controllers response to event
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Incident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Still Under Investigation, Cause Of Incident To Be Determined* (*supplemental Report Required)
Preparer Name
J***** S*****
Preparer Title
Sr. Specialist- Dot Compliance
Preparer Email
J************@e*************.com
Preparer Telephone
832-324-1027
Authorizer Name
J***** D*******
Authorizer Title
Manager Dot Compliance
Authorizer Telephone
7139895231
Authorizer Email
J**************@e*************.com
Narrative
On october 5th, 2025 at 12:10 p.M. Gas control received a call from a landowner reporting a leak in an et row. Operations was dispatched at 12:15pm and confirmed at 2:31 p.M. That the line was our 1090 sugar valley pipeline. The line was isolated by valve closure by 3:56 p.M. The next morning october 6th 2025 at 11:22 a.M. Calculations confirmed the incident to be reportable, due to the gas loss exceeding the reporting threshold. Permanent repairs (pipe replacement) were completed by october 10th 2025. The line was returned to service on october 24th, 2025 at 2:00 p.M. The pipe has been sent to a lab where the cause is pending the results of the metallurgical analysis.
Report Received Date 2025-11-03 00:00:00
Iyear 2025
Report Number 20250122
Supplemental Number 41541
Report Type Original
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2025-10-05 12:10:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 28.94264 Google Maps OpenStreetMap
Location Longitude -95.85557 Google Maps OpenStreetMap
Nrc Rpt Num 1444735 NRC Report How to search
Nrc Rpt Datetime 2025-10-06 11:30:00
Additional Nrc Report Numbers 1444937
Commodity Released Type Natural Gas
Unintentional Release 8964
Intentional Release 110
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2025-10-05 15:56:00
Restart Datetime 2025-10-24 14:00:00
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2025-10-05 15:56:00
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2025-10-05 15:56:00
Num Pub Evacuated 0
Incident Identified Datetime 2025-10-05 12:10:00
On Site Datetime 2025-10-05 14:31:00
Confirmed Discovery Datetime 2025-10-06 11:22:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 77414
Onshore City Name Bay City
Onshore County Name Matagorda
Designated Location Survey Station No.
Designated Name 123+53
Pipe Fac Name 1090 Sugar Valley
Segment Name 1090 Sugar Valley
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Loss Of Cover
Depth Of Cover 42
Other Underground Facilities No
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12.75
Puddle Weld Ind No
Pipe Wall Thickness 0.25
Pipe Smys 24000
Pipe Specification Api 5l
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Coating Applied Ind No
Installation Year 1953
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Length 40
Rupture Width 34
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 660
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 7500
Est Cost Unintentional Release 33884
Est Cost Intentional Release 416
Est Cost Prop Damage 125000
Est Cost Emergency 2000
Est Cost Other 0
Gas Cost In Mcf 3.78
Prpty 168800
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 467
Gas Flow In Pipe In Mcf 3700
Mop Psig 500
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 2011-07-28 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Gas Odorized Ind Yes
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 39847
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Other
Accident Details Notification From Land Owner
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No fatigue or drug/alcohol indications, no issues with controllers response to event
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Incident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Still Under Investigation, Cause Of Incident To Be Determined* (*supplemental Report Required)
Preparer Name J***** S*****
Preparer Title Sr. Specialist- Dot Compliance
Preparer Email J************@e*************.com
Preparer Telephone 832-324-1027
Authorizer Name J***** D*******
Authorizer Title Manager Dot Compliance
Authorizer Telephone 7139895231
Authorizer Email J**************@e*************.com
Narrative On october 5th, 2025 at 12:10 p.M. Gas control received a call from a landowner reporting a leak in an et row. Operations was dispatched at 12:15pm and confirmed at 2:31 p.M. That the line was our 1090 sugar valley pipeline. The line was isolated by valve closure by 3:56 p.M. The next morning october 6th 2025 at 11:22 a.M. Calculations confirmed the incident to be reportable, due to the gas loss exceeding the reporting threshold. Permanent repairs (pipe replacement) were completed by october 10th 2025. The line was returned to service on october 24th, 2025 at 2:00 p.M. The pipe has been sent to a lab where the cause is pending the results of the metallurgical analysis.

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