Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2025-04-25 — OH
Operator
Marathon Pipe Line Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$17,720
Incident datetime
2025-04-25 00:00 UTC
Report number
Location
OH
Narrative
On april 1, an isolation gasket failed while commissioning a new meter at benedum station. Benedum station was down at the time of release due to the commissioning and controls work. Piping section was immediately isolated and subsequently de-pressured. Reportable criteria were determined to have been met at 14:35 on april 2nd after volume calculations were completed. The released commodity was a nitrogen/ngl mixture that was predominately nitrogen. The failed gasket was installed during construction and is to be replaced. Supplemental update: internal investigation revealed that the design did not identify the need for support of the valve in the the interim period until the future connection would be made. The valve has been reinstalled with appropriate support.
Detailed record list
Report Received Date
2025-04-25 00:00:00
Iyear
2025
Report Number
20250105
Supplemental Number
40993
Report Type
Supplemental Final
Operator Id
32147
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
31.3730523
Location Longitude
-101.7862002
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
2
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Post-Construction Commissioning
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Orla Junction - Sweeny 24"-20" Products (Bangl)
Segment Name
Benedum Station
Onshore State Abbreviation
Tx
Onshore Postal Code
79755
Onshore City Name
Not Within A Municipality
Onshore County Name
Upton
Designated Location
Survey Station No.
Designated Name
Benedum
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
2025
Manufactured Year
2024
Material Involved
Material Other Than Carbon Steel
Material Details
Lamons Dfs Insulation Gasket
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
57
Est Cost Prop Damage
17720
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
17777
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
420
Mop Psig
1461
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2025-02-18 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
No
Scada Functional Ind
No
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room had no impact on release
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Support Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Design
Preparer Name
Z*** C*********
Preparer Title
Compliance Specialist
Preparer Email
Z***********@m****************.com
Preparer Telephone
4196726607
Prepared Date
2025-06-05 00:00:00
Authorizer Name
M****** G***
Authorizer Telephone
4194214505
Authorizer Title
Ess And Compliance Director
Authorizer Email
M*****@m****************.com
Narrative
On april 1, an isolation gasket failed while commissioning a new meter at benedum station. Benedum station was down at the time of release due to the commissioning and controls work. Piping section was immediately isolated and subsequently de-pressured. Reportable criteria were determined to have been met at 14:35 on april 2nd after volume calculations were completed. The released commodity was a nitrogen/ngl mixture that was predominately nitrogen. The failed gasket was installed during construction and is to be replaced. Supplemental update: internal investigation revealed that the design did not identify the need for support of the valve in the the interim period until the future connection would be made. The valve has been reinstalled with appropriate support.
Report Received Date | 2025-04-25 00:00:00 |
---|---|
Iyear | 2025 |
Report Number | 20250105 |
Supplemental Number | 40993 |
Report Type | Supplemental Final |
Operator Id | 32147 PHMSA Enforcement |
Name | Marathon Pipe Line Llc |
Operator Street Address | 539 South Main Street |
Operator City Name | Findlay |
Operator State Abbreviation | OH |
Operator Postal Code | 45840 |
Time Zone | Central |
Daylight Savings Ind | No |
Location Latitude | 31.3730523 Google Maps OpenStreetMap |
Location Longitude | -101.7862002 Google Maps OpenStreetMap |
Commodity Released Type | Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions |
Commodity Subtype | Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid) |
Unintentional Release Bbls | 2 |
Intentional Release Bbls | 0 |
Recovered Bbls | 0 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Pump/meter Station Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Post-Construction Commissioning |
Communication State Fed Ind | No |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Orla Junction - Sweeny 24"-20" Products (Bangl) |
Segment Name | Benedum Station |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 79755 |
Onshore City Name | Not Within A Municipality |
Onshore County Name | Upton |
Designated Location | Survey Station No. |
Designated Name | Benedum |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Intrastate |
Item Involved | Flange Assembly |
Installation Year | 2025 |
Manufactured Year | 2024 |
Material Involved | Material Other Than Carbon Steel |
Material Details | Lamons Dfs Insulation Gasket |
Release Type | Leak |
Leak Type | Connection Failure |
Wildlife Impact Ind | No |
Soil Contamination | No |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 57 |
Est Cost Prop Damage | 17720 |
Est Cost Emergency | 0 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 17777 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 420 |
Mop Psig | 1461 |
Mop Cfr Section | Internal Design Pressure �195.406(A)(1) View CFR 49 §192 |
Maop Established Date | 2025-02-18 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | No |
Scada Functional Ind | No |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Control room had no impact on release |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Equipment Failure |
Cause Details | Non-Threaded Connection Failure |
Eq Failure Type | Non-Threaded Connection Failure |
Other Non Threaded Ind | Gasket |
Additional Support Ind | Yes |
Eq Additional Other Ind | Yes |
Eq Additional Other Details | Design |
Preparer Name | Z*** C********* |
Preparer Title | Compliance Specialist |
Preparer Email | Z***********@m****************.com |
Preparer Telephone | 4196726607 |
Prepared Date | 2025-06-05 00:00:00 |
Authorizer Name | M****** G*** |
Authorizer Telephone | 4194214505 |
Authorizer Title | Ess And Compliance Director |
Authorizer Email | M*****@m****************.com |
Narrative | On april 1, an isolation gasket failed while commissioning a new meter at benedum station. Benedum station was down at the time of release due to the commissioning and controls work. Piping section was immediately isolated and subsequently de-pressured. Reportable criteria were determined to have been met at 14:35 on april 2nd after volume calculations were completed. The released commodity was a nitrogen/ngl mixture that was predominately nitrogen. The failed gasket was installed during construction and is to be replaced. Supplemental update: internal investigation revealed that the design did not identify the need for support of the valve in the the interim period until the future connection would be made. The valve has been reinstalled with appropriate support. |
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