Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2025-04-22 — TX
Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$150,000
Incident datetime
2025-04-22 00:00 UTC
Report number
Location
TX
Narrative
On 3/24/2025 at 16:00 cdt enterprise pipeline technician received a notification, from a third-party producer, of a crude release on lid c14. The affected pipeline segment was immediately isolated, and dispatched pipeline operator confirmed the release of crude. Metallurgical analysis determined that the failure occurred due to internal corrosion present along the bottom of the pipe. The affected pipeline segment was replaced, and the pipeline was returned into service.
Detailed record list
Report Received Date
2025-04-22 00:00:00
Iyear
2025
Report Number
20250100
Supplemental Number
41235
Report Type
Supplemental Final
Operator Id
30829
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
32.4513
Location Longitude
-102.8111
Commodity Released Type
Crude Oil
Unintentional Release Bbls
267
Recovered Bbls
160
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Producer
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
1426769
Additional Nrc Report Numbers
1426884
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
3/25/2025 7:00
Num Pub Evacuated
0
Pipe Fac Name
C14
Segment Name
Hobbs To Midland
Onshore State Abbreviation
Tx
Onshore Postal Code
79714
Onshore City Name
Not Within A Municipality
Onshore County Name
Andrews
Designated Location
Milepost
Designated Name
24
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
8
Pipe Wall Thickness
0.188
Pipe Smys
52000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Republic Steel
Pipe Coating Type
Coal Tar
Coating Applied Ind
Unknown
Installation Year
1980
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
2500
Est Cost Gas Released
18453
Est Cost Prop Damage
150000
Est Cost Emergency
42000
Est Cost Environmental
76000
Est Cost Other
0
Prpty
288953
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
200
Mop Psig
730
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
1980-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
42240
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Not applicable to this release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Under Deposit Corrosion
Int Metallurgical Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
Bottom Of Pipe. Pipe Segment Was At Level With No Obvious Low Point At Location Of The Leak.
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2024
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Axial Previous Year
2019
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
High Resolution
Geometry Recent Year
2024
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
No Cups
Geometry Previous Year
2019
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
No Cups
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2008
Hydrtst Most Rcnt Pressure
934
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
Y******* B**
Preparer Title
Pipeline Compliance Engineer
Preparer Email
Y***@e****.com
Preparer Telephone
713-381-5650
Prepared Date
2025-08-08 00:00:00
Local Contact Name
Y******* B**
Local Contact Email
Y***@e****.com
Local Contact Telephone
713-381-5650
Authorizer Name
Y******* B**
Authorizer Telephone
713-381-5650
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
Y***@e****.com
Narrative
On 3/24/2025 at 16:00 cdt enterprise pipeline technician received a notification, from a third-party producer, of a crude release on lid c14. The affected pipeline segment was immediately isolated, and dispatched pipeline operator confirmed the release of crude. Metallurgical analysis determined that the failure occurred due to internal corrosion present along the bottom of the pipe. The affected pipeline segment was replaced, and the pipeline was returned into service.
Report Received Date | 2025-04-22 00:00:00 |
---|---|
Iyear | 2025 |
Report Number | 20250100 |
Supplemental Number | 41235 |
Report Type | Supplemental Final |
Operator Id | 30829 PHMSA Enforcement |
Name | Enterprise Crude Pipeline Llc |
Operator Street Address | 1100 Louisiana Street |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 32.4513 Google Maps OpenStreetMap |
Location Longitude | -102.8111 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 267 |
Recovered Bbls | 160 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Other |
Accident Details | Third Party Producer |
System Part Involved | Onshore Pipeline, Including Valve Sites |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | No |
Nrc Rpt Num | 1426769 NRC Report How to search |
Additional Nrc Report Numbers | 1426884 |
Ignite Ind | No |
Upstream Action Taken | Valve Closure |
Upstream Valve Type Ind | Manual |
Downstream Action Taken | Valve Closure |
Downstream Valve Type Ind | Manual |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | Yes |
Osro Arrived On Site Dt | 3/25/2025 7:00 |
Num Pub Evacuated | 0 |
Pipe Fac Name | C14 |
Segment Name | Hobbs To Midland |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 79714 |
Onshore City Name | Not Within A Municipality |
Onshore County Name | Andrews |
Designated Location | Milepost |
Designated Name | 24 |
Federal | No |
Location Type | Pipeline Right-Of-Way |
Incident Area Type | Underground |
Incident Area Subtype | Under Soil |
Depth Of Cover | 60 |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Pipe |
Pipe Type | Pipe Body |
Puddle Weld Ind | No |
Pipe Diameter | 8 |
Pipe Wall Thickness | 0.188 |
Pipe Smys | 52000 |
Pipe Specification | Api 5l |
Pipe Seam Type | Erw - High Frequency |
Pipe Manufacturer | Republic Steel |
Pipe Coating Type | Coal Tar |
Coating Applied Ind | Unknown |
Installation Year | 1980 |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Pinhole |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | Yes |
Soil Remed Ind | Yes |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 2500 |
Est Cost Gas Released | 18453 |
Est Cost Prop Damage | 150000 |
Est Cost Emergency | 42000 |
Est Cost Environmental | 76000 |
Est Cost Other | 0 |
Prpty | 288953 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 200 |
Mop Psig | 730 |
Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
Maop Established Date | 1980-01-01 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Length Segment Isolated | 42240 |
Internal Inspection Ind | Yes |
Operation Complications Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Not applicable to this release. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Corrosion Failure |
Cause Details | Internal Corrosion |
Internal External | Internal Corrosion |
Int Visual Exam Results | Localized Pitting |
Int Other Corrosion Ind | Yes |
Int Corrosion Type Details | Under Deposit Corrosion |
Int Metallurgical Basis Ind | Yes |
Int Other Loc Ind | Yes |
Corrosion Location Details | Bottom Of Pipe. Pipe Segment Was At Level With No Obvious Low Point At Location Of The Leak. |
Corrosion Inhibitors | Yes |
Corrosion Lining | No |
Cleaning Dewatering | Yes |
Corrosion Coupons | Yes |
Collected Data Ind | Yes |
Axial Magnetic Flx Lkg Ind | Yes |
Geometry Deformation Ind | Yes |
Axial Recent Year | 2024 |
Axial Rcnt Propul Method | Free Swimming |
Axial Rcnt Attuned Detect | Metal Loss |
Axial Rcnt Atnd Dtct Metal | High Resolution |
Axial Previous Year | 2019 |
Axial Prev Propul Method | Free Swimming |
Axial Prev Attuned Detect | Metal Loss |
Axial Prev Atnd Dtct Metal | High Resolution |
Geometry Recent Year | 2024 |
Geometry Rcnt Propul Method | Free Swimming |
Geometry Rcnt Resolution | High Resolution |
Geometrt Rcnt Measur Cups | No Cups |
Geometry Previous Year | 2019 |
Geometry Prev Propul Method | Free Swimming |
Geometry Prev Resolution | High Resolution |
Geometrt Prev Measur Cups | No Cups |
Has Hydrtst Conduc Before Ind | Yes |
Hydrtst Most Rcnt Year | 2008 |
Hydrtst Most Rcnt Pressure | 934 |
Direct Asmnt Conducted | No |
Non Destructive Exam Ind | No |
Preparer Name | Y******* B** |
Preparer Title | Pipeline Compliance Engineer |
Preparer Email | Y***@e****.com |
Preparer Telephone | 713-381-5650 |
Prepared Date | 2025-08-08 00:00:00 |
Local Contact Name | Y******* B** |
Local Contact Email | Y***@e****.com |
Local Contact Telephone | 713-381-5650 |
Authorizer Name | Y******* B** |
Authorizer Telephone | 713-381-5650 |
Authorizer Title | Pipeline Compliance Engineer |
Authorizer Email | Y***@e****.com |
Narrative | On 3/24/2025 at 16:00 cdt enterprise pipeline technician received a notification, from a third-party producer, of a crude release on lid c14. The affected pipeline segment was immediately isolated, and dispatched pipeline operator confirmed the release of crude. Metallurgical analysis determined that the failure occurred due to internal corrosion present along the bottom of the pipe. The affected pipeline segment was replaced, and the pipeline was returned into service. |
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