Incident details
Operator, cause, commodity and consequences with raw source fields.
GTG incident on 2025-08-21 — TX
Operator
Sea Robin Pipeline Co
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$350,000
Incident datetime
2025-08-21 00:00 UTC
Report number
Location
TX
Narrative
While conducting an overflight, at approximately 15:30 on 08/02/25 bubbles were spotted near our sea robin 716-10-1 lateral in eugene island 330 (ei 330). Nrc (#1438692) was called reporting the bubbles in ei 330. The leak was confirmed to be sea robin and the 48hr update (#1438805) was made. The dsv was deployed on 08/02/25. The leak was located and a clamp was install on 08/05/25 at 07:10.
Detailed record list
Report Received Date
2025-08-21 00:00:00
Iyear
2025
Report Number
20250092
Supplemental Number
41287
Report Type
Original
Operator Id
18152
Name
Sea Robin Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
28.245986
Location Longitude
-91.705189
Nrc Rpt Num
1438692
Additional Nrc Report Numbers
1438805
Commodity Released Type
Natural Gas
Unintentional Release
229
Intentional Release
527853
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Still Shutdown Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Ignite Ind
No
Upstream Action Taken
Valve Closure
Downstream Action Taken
Valve Closure
Num Pub Evacuated
0
On Off Shore
Offshore
Pipe Fac Name
Sea Robin
Segment Name
Line 716-10-1
Off Water Depth
260
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Ocs Type
Ocs-Gulf Of America
Off Ocs Area
Eugene Island
Off Ocs Block
330
Off Area Accident Type
Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type
Interstate
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Puddle Weld Ind
No
Pipe Wall Thickness
0.41
Pipe Smys
24000
Pipe Specification
Api 5l X-52
Pipe Seam Type
Other
Pipe Seam Details
Unknown
Pipe Manufacturer
Unknown
Pipe Coating Type
Other
Pipe Coating Details
Mastec & Concrete
Coating Applied Ind
Yes
Installation Year
1973
Manufactured Year
1973
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
215
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
563
Est Cost Intentional Release
1298518
Est Cost Prop Damage
350000
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
2.46
Prpty
1649081
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
906
Gas Flow In Pipe In Mcf
3000
Mop Psig
1306
Mop Cfr Section
192.619(A)(1)
Maop Established Date
1977-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
31680
Internal Inspection Ind
No
Tight Mitered Ind
Yes
Operation Complications Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Other
Accident Details
Notified By Producer
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak was too small for scada to detect
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Corrosive Commodity Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
P*** W***
Preparer Title
Manager Dot Compliance
Preparer Email
P*********@e*************.com
Preparer Telephone
3187291832
Local Contact Name
P**** W***
Local Contact Email
P*********@e*************.com
Local Contact Telephone
4093823918
Authorizer Name
P**** W***
Authorizer Title
Manager Dot Compliance
Authorizer Telephone
3187291832
Authorizer Email
P*********@e*************.com
Narrative
While conducting an overflight, at approximately 15:30 on 08/02/25 bubbles were spotted near our sea robin 716-10-1 lateral in eugene island 330 (ei 330). Nrc (#1438692) was called reporting the bubbles in ei 330. The leak was confirmed to be sea robin and the 48hr update (#1438805) was made. The dsv was deployed on 08/02/25. The leak was located and a clamp was install on 08/05/25 at 07:10.
Report Received Date | 2025-08-21 00:00:00 |
---|---|
Iyear | 2025 |
Report Number | 20250092 |
Supplemental Number | 41287 |
Report Type | Original |
Operator Id | 18152 PHMSA Enforcement |
Name | Sea Robin Pipeline Co |
Operator Street Address | 1300 Main Street |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 28.245986 Google Maps OpenStreetMap |
Location Longitude | -91.705189 Google Maps OpenStreetMap |
Nrc Rpt Num | 1438692 NRC Report How to search |
Additional Nrc Report Numbers | 1438805 |
Commodity Released Type | Natural Gas |
Unintentional Release | 229 |
Intentional Release | 527853 |
Accompanying Liquid | 0 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Status When Identified | Normal Operation, Includes Pauses During Maintenance |
Shutdown Due Accident Ind | Yes |
Still Shutdown Ind | Yes |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Ignite Ind | No |
Upstream Action Taken | Valve Closure |
Downstream Action Taken | Valve Closure |
Num Pub Evacuated | 0 |
On Off Shore | Offshore |
Pipe Fac Name | Sea Robin |
Segment Name | Line 716-10-1 |
Off Water Depth | 260 |
Off Accident Origin | On The Outer Continental Shelf (Ocs) |
Ocs Type | Ocs-Gulf Of America |
Off Ocs Area | Eugene Island |
Off Ocs Block | 330 |
Off Area Accident Type | Below Water, Pipe Buried Or Jetted Below Seabed |
Pipe Facility Type | Interstate |
System Part Involved | Offshore Pipeline, Including Riser And Riser Bend |
Item Involved | Pipe |
Pipe Type | Pipe Body |
Pipe Diameter | 8.625 |
Puddle Weld Ind | No |
Pipe Wall Thickness | 0.41 |
Pipe Smys | 24000 |
Pipe Specification | Api 5l X-52 |
Pipe Seam Type | Other |
Pipe Seam Details | Unknown |
Pipe Manufacturer | Unknown |
Pipe Coating Type | Other |
Pipe Coating Details | Mastec & Concrete |
Coating Applied Ind | Yes |
Installation Year | 1973 |
Manufactured Year | 1973 |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Pinhole |
Class Location Type | Class 1 Location |
Could Be Hca | No |
Pir Radius | 215 |
Heat Damage Ind | No |
Non Heat Damage Ind | No |
Did Occur In Mca Ind | No |
Est Cost Oper Paid | 0 |
Est Cost Unintentional Release | 563 |
Est Cost Intentional Release | 1298518 |
Est Cost Prop Damage | 350000 |
Est Cost Emergency | 0 |
Est Cost Other | 0 |
Gas Cost In Mcf | 2.46 |
Prpty | 1649081 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Wildlife Impact Ind | No |
Accident Psig | 906 |
Gas Flow In Pipe In Mcf | 3000 |
Mop Psig | 1306 |
Mop Cfr Section | 192.619(A)(1) View CFR 49 §192 |
Maop Established Date | 1977-01-01 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Maop |
Pressure Restriction Ind | No |
Gas Required Odorized Ind | No |
Upstream Valve Type Ind | Manual |
Downstream Valve Type Ind | Manual |
Length Segment Isolated | 31680 |
Internal Inspection Ind | No |
Tight Mitered Ind | Yes |
Operation Complications Ind | Yes |
Low Flow Ind | Yes |
Pipeline Function | Transmission System |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Accident Identifier | Other |
Accident Details | Notified By Producer |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Leak was too small for scada to detect |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Corrosion Failure |
Cause Details | Internal Corrosion |
Internal External | Internal Corrosion |
Int Visual Exam Results | Not Cut Open |
Int Corrosive Commodity Ind | Yes |
Int Field Exam Basis Ind | Yes |
Int Low Point Pipe Loc Ind | Yes |
Corrosion Inhibitors | No |
Corrosion Lining | No |
Cleaning Dewatering | No |
Corrosion Coupons | Yes |
Collected Data Ind | No |
Has Hydrtst Conduc Before Ind | No |
Direct Asmnt Conducted | No |
Non Destructive Exam Ind | No |
Preparer Name | P*** W*** |
Preparer Title | Manager Dot Compliance |
Preparer Email | P*********@e*************.com |
Preparer Telephone | 3187291832 |
Local Contact Name | P**** W*** |
Local Contact Email | P*********@e*************.com |
Local Contact Telephone | 4093823918 |
Authorizer Name | P**** W*** |
Authorizer Title | Manager Dot Compliance |
Authorizer Telephone | 3187291832 |
Authorizer Email | P*********@e*************.com |
Narrative | While conducting an overflight, at approximately 15:30 on 08/02/25 bubbles were spotted near our sea robin 716-10-1 lateral in eugene island 330 (ei 330). Nrc (#1438692) was called reporting the bubbles in ei 330. The leak was confirmed to be sea robin and the 48hr update (#1438805) was made. The dsv was deployed on 08/02/25. The leak was located and a clamp was install on 08/05/25 at 07:10. |
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