GTG incident on 2025-07-16 — MI

Operator
Dtm Louisiana Gathering, Llc
Cause
Other Incident Cause
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$190,000
Incident datetime
2025-07-16 00:00 UTC
Report number
Location
MI
Narrative
On june 16, 2025, at approximately 0815 hours, a rupture occurred in a bored section of the pipeline. This resulted in an unintentional release of natural gas exceeding 3 mmcf. Dtm's field technicians responded to the unintentional release, isolating the affected section of the pipeline and preventing further release. The cause of the failure is still under investigation. The failed section of pipe has been removed and sent off for a complete analysis. A supplemental report will be submitted when dtm has more information.
Detailed record list
Report Received Date
2025-07-16 00:00:00
Iyear
2025
Report Number
20250081
Supplemental Number
41151
Report Type
Original
Operator Id
Name
Dtm Louisiana Gathering, Llc
Operator Street Address
500 Woodward Ave. Suite 2900
Operator City Name
Detroit
Operator State Abbreviation
MI
Operator Postal Code
48226
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Additional Nrc Report Numbers
1434426
Commodity Released Type
Natural Gas
Unintentional Release
17810
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Still Shutdown Ind
Yes
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Downstream Action Taken
Valve Closure
Num Pub Evacuated
0
On Off Shore
Onshore
Onshore State Abbreviation
La
Onshore Postal Code
71032
Onshore City Name
Not Within A Municipality
Onshore County Name
Desoto
Designated Location
Not Applicable
Pipe Fac Name
Long Main
Segment Name
M5l-308-00d
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
180
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Puddle Weld Ind
No
Pipe Wall Thickness
0.322
Pipe Smys
52000
Pipe Specification
Api 5l X52m
Pipe Seam Type
Longitudinal Erw - High Frequency
Pipe Manufacturer
Seah Steel Corp
Pipe Coating Type
Epoxy
Coating Applied Ind
No
Installation Year
2018
Manufactured Year
2017
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
15
Rupture Width
8
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
221
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
235983
Est Cost Intentional Release
0
Est Cost Prop Damage
190000
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
13.25
Prpty
425983
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
939
Gas Flow In Pipe In Mcf
12400
Mop Psig
1235
Mop Cfr Section
192.619(A)(2)
Maop Established Date
2018-04-11 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
3546
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Type C Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The control room is monitor-only for that system and successfully handled the alarm by notifying local field staff.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Incident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Still Under Investigation, Cause Of Incident To Be Determined* (*supplemental Report Required)
Preparer Name
N*** N******
Preparer Title
Senior Compliance Specialist
Preparer Email
N***********@d**********.com
Preparer Telephone
1-318-918-8381
Preparer Fax
1-318-447-2097
Local Contact Name
R** G***
Local Contact Email
R*******@d**********.com
Local Contact Telephone
1-304-712-1758
Authorizer Name
P****** C******
Authorizer Title
Director Codes And Regulatory
Authorizer Telephone
1-734-730-4870
Authorizer Email
P**************@d**********.com
Narrative
On june 16, 2025, at approximately 0815 hours, a rupture occurred in a bored section of the pipeline. This resulted in an unintentional release of natural gas exceeding 3 mmcf. Dtm's field technicians responded to the unintentional release, isolating the affected section of the pipeline and preventing further release. The cause of the failure is still under investigation. The failed section of pipe has been removed and sent off for a complete analysis. A supplemental report will be submitted when dtm has more information.
Report Received Date 2025-07-16 00:00:00
Iyear 2025
Report Number 20250081
Supplemental Number 41151
Report Type Original
Operator Id 39913 PHMSA Enforcement
Name Dtm Louisiana Gathering, Llc
Operator Street Address 500 Woodward Ave. Suite 2900
Operator City Name Detroit
Operator State Abbreviation MI
Operator Postal Code 48226
Time Zone Central
Daylight Savings Ind No
Location Latitude 32.0681 Google Maps OpenStreetMap
Location Longitude -93.9091 Google Maps OpenStreetMap
Nrc Rpt Num 1434216 NRC Report How to search
Additional Nrc Report Numbers 1434426
Commodity Released Type Natural Gas
Unintentional Release 17810
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Still Shutdown Ind Yes
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Valve Closure
Downstream Action Taken Valve Closure
Num Pub Evacuated 0
On Off Shore Onshore
Onshore State Abbreviation La
Onshore Postal Code 71032
Onshore City Name Not Within A Municipality
Onshore County Name Desoto
Designated Location Not Applicable
Pipe Fac Name Long Main
Segment Name M5l-308-00d
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 180
Other Underground Facilities No
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Puddle Weld Ind No
Pipe Wall Thickness 0.322
Pipe Smys 52000
Pipe Specification Api 5l X52m
Pipe Seam Type Longitudinal Erw - High Frequency
Pipe Manufacturer Seah Steel Corp
Pipe Coating Type Epoxy
Coating Applied Ind No
Installation Year 2018
Manufactured Year 2017
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Circumferential
Rupture Length 15
Rupture Width 8
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 221
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 235983
Est Cost Intentional Release 0
Est Cost Prop Damage 190000
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 13.25
Prpty 425983
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 939
Gas Flow In Pipe In Mcf 12400
Mop Psig 1235
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 2018-04-11 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 3546
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Type C Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The control room is monitor-only for that system and successfully handled the alarm by notifying local field staff.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Incident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Still Under Investigation, Cause Of Incident To Be Determined* (*supplemental Report Required)
Preparer Name N*** N******
Preparer Title Senior Compliance Specialist
Preparer Email N***********@d**********.com
Preparer Telephone 1-318-918-8381
Preparer Fax 1-318-447-2097
Local Contact Name R** G***
Local Contact Email R*******@d**********.com
Local Contact Telephone 1-304-712-1758
Authorizer Name P****** C******
Authorizer Title Director Codes And Regulatory
Authorizer Telephone 1-734-730-4870
Authorizer Email P**************@d**********.com
Narrative On june 16, 2025, at approximately 0815 hours, a rupture occurred in a bored section of the pipeline. This resulted in an unintentional release of natural gas exceeding 3 mmcf. Dtm's field technicians responded to the unintentional release, isolating the affected section of the pipeline and preventing further release. The cause of the failure is still under investigation. The failed section of pipe has been removed and sent off for a complete analysis. A supplemental report will be submitted when dtm has more information.

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