GTG incident on 2025-04-25 — TX

Operator
Energy Transfer Company
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$873,500
Incident datetime
2025-04-25 00:00 UTC
Report number
Location
TX
Narrative
On march 27th, 2025, 11:59 a.M., an unexpected release of natural gas was observed at the hollywood and vine facility. The release came from the launcher door closure and blowdown stack of the loading barrel. An etc employee was onsite and was able to quickly engage the asd system allowing the system to block and bleed within five minutes. During our internal investigation it was determined that the employee loading the sphere pigs into the launcher had failed to secure the pig launcher door closure assembly which resulted in a gas release during the barrel purging process.
Detailed record list
Report Received Date
2025-04-25 00:00:00
Iyear
2025
Report Number
20250044
Supplemental Number
41049
Report Type
Supplemental Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Additional Nrc Report Numbers
1427135
Commodity Released Type
Natural Gas
Unintentional Release
22988
Intentional Release
799
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Ignite Ind
No
Upstream Action Taken
Valve Closure
Downstream Action Taken
Valve Closure
Num Pub Evacuated
15
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
78836
Onshore City Name
Catarina
Onshore County Name
Dimmit
Designated Location
Not Applicable
Pipe Fac Name
20101161 Rich Eagleford Mainline
Segment Name
20101161 Rich Eagleford Mainline
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Scraper/pig Trap
Installation Year
2012
Manufactured Year
2011
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
From Opening Of Ball Valve
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
660
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
12000
Est Cost Unintentional Release
89193
Est Cost Intentional Release
3100
Est Cost Prop Damage
873500
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
3.88
Prpty
977793
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
1
Wildlife Impact Ind
No
Accident Psig
1003
Gas Flow In Pipe In Mcf
600000
Mop Psig
1300
Mop Cfr Section
192.619(A)(2)
Maop Established Date
2011-09-21 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Length Segment Isolated
550
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Type C Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller did not contribute to the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Failure To Follow Procedures
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
J***** S*****
Preparer Title
Sr. Specialist Dot Compliance
Preparer Email
J************@e*************.com
Preparer Telephone
8323241027
Authorizer Name
J***** D*******
Authorizer Title
Manager Dot Compliance
Authorizer Telephone
7138820590
Authorizer Email
J**************@e*************.com
Narrative
On march 27th, 2025, 11:59 a.M., an unexpected release of natural gas was observed at the hollywood and vine facility. The release came from the launcher door closure and blowdown stack of the loading barrel. An etc employee was onsite and was able to quickly engage the asd system allowing the system to block and bleed within five minutes. During our internal investigation it was determined that the employee loading the sphere pigs into the launcher had failed to secure the pig launcher door closure assembly which resulted in a gas release during the barrel purging process.
Report Received Date 2025-04-25 00:00:00
Iyear 2025
Report Number 20250044
Supplemental Number 41049
Report Type Supplemental Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 28.332579 Google Maps OpenStreetMap
Location Longitude -99.611097 Google Maps OpenStreetMap
Nrc Rpt Num 1427041 NRC Report How to search
Additional Nrc Report Numbers 1427135
Commodity Released Type Natural Gas
Unintentional Release 22988
Intentional Release 799
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Operator
Ignite Ind No
Upstream Action Taken Valve Closure
Downstream Action Taken Valve Closure
Num Pub Evacuated 15
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 78836
Onshore City Name Catarina
Onshore County Name Dimmit
Designated Location Not Applicable
Pipe Fac Name 20101161 Rich Eagleford Mainline
Segment Name 20101161 Rich Eagleford Mainline
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Scraper/pig Trap
Installation Year 2012
Manufactured Year 2011
Material Involved Carbon Steel
Release Type Other
Release Type Details From Opening Of Ball Valve
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 660
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 12000
Est Cost Unintentional Release 89193
Est Cost Intentional Release 3100
Est Cost Prop Damage 873500
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 3.88
Prpty 977793
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 1
Wildlife Impact Ind No
Accident Psig 1003
Gas Flow In Pipe In Mcf 600000
Mop Psig 1300
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 2011-09-21 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Length Segment Isolated 550
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Type C Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller did not contribute to the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Failure To Follow Procedures
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name J***** S*****
Preparer Title Sr. Specialist Dot Compliance
Preparer Email J************@e*************.com
Preparer Telephone 8323241027
Authorizer Name J***** D*******
Authorizer Title Manager Dot Compliance
Authorizer Telephone 7138820590
Authorizer Email J**************@e*************.com
Narrative On march 27th, 2025, 11:59 a.M., an unexpected release of natural gas was observed at the hollywood and vine facility. The release came from the launcher door closure and blowdown stack of the loading barrel. An etc employee was onsite and was able to quickly engage the asd system allowing the system to block and bleed within five minutes. During our internal investigation it was determined that the employee loading the sphere pigs into the launcher had failed to secure the pig launcher door closure assembly which resulted in a gas release during the barrel purging process.

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