Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2025-07-12 — IL
Operator
Northern Illinois Gas Co
Cause
Other Incident Cause
Commodity
Natural Gas
Program
GD
Damage and Injuries
1 fatality
0 injuries
Property damage (nominal)
$200
Incident datetime
2025-07-12 00:00 UTC
Report number
Location
IL, COOK
Narrative
Per national transportation safety board ("ntsb") investigation id pld25fr006, the following information is preliminary and subject to change. On june 12, 2025, a natural gas-fueled explosion and fire destroyed a single-family residence at 14109 kenneth court in crestwood, illinois. The explosion killed one person and damaged neighboring residences. Nicor gas provided natural gas service to the home and the neighboring residences. The crestwood fire department responded to the explosion and fire at about 2:16 p.M. Nicor gas arrived on the scene at about 2:40 p.M. And disconnected and capped the service line at about 4:44 p.M. On june 13, 2025, nicor gas performed a pressure test of the service line. The service line did not hold pressure, indicating a leak. After national transportation safety board (ntsb) investigators arrived on scene, nicor gas performed flow tests on the service line to estimate the size of the leak. Barhole testing conducted by nicor gas confirmed the presence of gas in the ground near the foundation of the home. Nicor gas located and marked underground utilities at the accident site and obtained gas consumption data from the home�s gas meter. While on scene, ntsb investigators completed the following actions: � examined the accident site, � secured a section of the service line containing the leak for examination at the ntsb�s materials laboratory in washington, dc, � reviewed the accident home�s gas consumption data over the past year, which was higher than the neighboring residences, � requested documentation from nicor gas, � requested communication logs from nicor gas and the crestwood fire department, � and conducted interviews. (https://www.Ntsb.Gov/investigations/pages/pld25fr006.Aspx)
Detailed record list
Report Received Date
2025-07-12 00:00:00
Iyear
2025.0
Report Number
20250040.0
Supplemental Number
41141.0
Report Type
Original
Operator Id
13710
Name
Northern Illinois Gas Co
Operator Street Address
P.o. Box 190, Rt 59 & I-88
Operator City Name
Aurora
Operator State Abbreviation
IL
Operator Postal Code
60507.0
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
14109 Kenneth Court
Location City Name
Crestwood
Location County Name
Cook
Location State Abbreviation
IL
Location Postal Code
60445.0
Location Latitude
41.63601701
Location Longitude
-87.72934154
Flow Cont Meter Reg Ind
Yes
Nrc Rpt Num
1433929.0
Additional Nrc Report Numbers
1434029.0
Commodity Released Type
Natural Gas
Unintentional Release
0.0
Intentional Release
0.0
Fatality Ind
Yes
Num Emp Fatalities
0
Num Contr Fatalities
0
Num Er Fatalities
0
Num Worker Fatalities
0
Num Gp Fatalities
1
Fatal
1
Injury Ind
No
Injure
0
Ignite Ind
Yes
How Extinguished
Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf
0
Explode Ind
Yes
Num Pub Evacuated
0.0
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Service
Installation Year
1992.0
Manufactured Year
1992.0
Customer Type
Single Family Residential
Was Efv Installed Before Ind
No
Curb Valve Inst Before Inc Ind
No
Pipe Diameter
0.625
Pipe Specification
Astm D2513
Pipe Manufacturer
Unknown
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Wt Plastic
0.09
Material Pe Pipe Code
2406
Release Type
Leak
Leak Type
Other
Leak Type Other
Still Under Investigation
Class Location Type
Class 3 Location
Est Cost Oper Paid
308043.0
Est Cost Prop Damage
200.0
Est Cost Emergency
11692.0
Est Cost Other
0.0
Gas Cost In Mcf
0.0
Est Cost Unintentional Release
0.0
Est Cost Intentional Release
0.0
Prpty
319935.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
1.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
1.0
Num Business Building Affctd
0.0
Accident Psig
24.69
Normal Psig
25.0
Mop Psig
28.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1988-07-01 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Combination Of Odorization Types
Gas Odorized Level
0.2
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Incident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Still Under Investigation, Cause Of Incident To Be Determined* (*supplemental Report Required)
Preparer Name
P***** L* R***
Preparer Title
Manager - Compliance And Qa
Preparer Email
P****@s*********.com
Preparer Telephone
2244570663
Local Contact Name
P***** L* R***
Local Contact Email
P****@s*********.com
Local Contact Telephone
2244570663
Authorizer Name
P***** L* R***
Authorizer Title
Manager - Compliance And Qa
Authorizer Telephone
2244570663
Authorizer Email
P****@s*********.com
Narrative
Per national transportation safety board ("ntsb") investigation id pld25fr006, the following information is preliminary and subject to change. On june 12, 2025, a natural gas-fueled explosion and fire destroyed a single-family residence at 14109 kenneth court in crestwood, illinois. The explosion killed one person and damaged neighboring residences. Nicor gas provided natural gas service to the home and the neighboring residences. The crestwood fire department responded to the explosion and fire at about 2:16 p.M. Nicor gas arrived on the scene at about 2:40 p.M. And disconnected and capped the service line at about 4:44 p.M. On june 13, 2025, nicor gas performed a pressure test of the service line. The service line did not hold pressure, indicating a leak. After national transportation safety board (ntsb) investigators arrived on scene, nicor gas performed flow tests on the service line to estimate the size of the leak. Barhole testing conducted by nicor gas confirmed the presence of gas in the ground near the foundation of the home. Nicor gas located and marked underground utilities at the accident site and obtained gas consumption data from the home�s gas meter. While on scene, ntsb investigators completed the following actions: � examined the accident site, � secured a section of the service line containing the leak for examination at the ntsb�s materials laboratory in washington, dc, � reviewed the accident home�s gas consumption data over the past year, which was higher than the neighboring residences, � requested documentation from nicor gas, � requested communication logs from nicor gas and the crestwood fire department, � and conducted interviews. (https://www.Ntsb.Gov/investigations/pages/pld25fr006.Aspx)
Report Received Date | 2025-07-12 00:00:00 |
---|---|
Iyear | 2025.0 |
Report Number | 20250040.0 |
Supplemental Number | 41141.0 |
Report Type | Original |
Operator Id | 13710 PHMSA Enforcement |
Name | Northern Illinois Gas Co |
Operator Street Address | P.o. Box 190, Rt 59 & I-88 |
Operator City Name | Aurora |
Operator State Abbreviation | IL |
Operator Postal Code | 60507.0 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Street Address | 14109 Kenneth Court |
Location City Name | Crestwood |
Location County Name | Cook |
Location State Abbreviation | IL |
Location Postal Code | 60445.0 |
Location Latitude | 41.63601701 Google Maps OpenStreetMap |
Location Longitude | -87.72934154 Google Maps OpenStreetMap |
Flow Cont Meter Reg Ind | Yes |
Nrc Rpt Num | 1433929.0 NRC Report How to search |
Additional Nrc Report Numbers | 1434029.0 |
Commodity Released Type | Natural Gas |
Unintentional Release | 0.0 |
Intentional Release | 0.0 |
Fatality Ind | Yes |
Num Emp Fatalities | 0 |
Num Contr Fatalities | 0 |
Num Er Fatalities | 0 |
Num Worker Fatalities | 0 |
Num Gp Fatalities | 1 |
Fatal | 1 |
Injury Ind | No |
Injure | 0 |
Ignite Ind | Yes |
How Extinguished | Local/state/federal Emergency Responder |
Gas Consumed By Fire In Mcf | 0 |
Explode Ind | Yes |
Num Pub Evacuated | 0.0 |
Federal | No |
Location Type | Private Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Inside A Building |
Crossing | No |
Pipe Facility Type | Investor Owned |
System Part Involved | Service |
Installation Year | 1992.0 |
Manufactured Year | 1992.0 |
Customer Type | Single Family Residential |
Was Efv Installed Before Ind | No |
Curb Valve Inst Before Inc Ind | No |
Pipe Diameter | 0.625 |
Pipe Specification | Astm D2513 |
Pipe Manufacturer | Unknown |
Material Involved | Plastic |
Plastic Type | Polyethylene (Pe) |
Wt Plastic | 0.09 |
Material Pe Pipe Code | 2406 |
Release Type | Leak |
Leak Type | Other |
Leak Type Other | Still Under Investigation |
Class Location Type | Class 3 Location |
Est Cost Oper Paid | 308043.0 |
Est Cost Prop Damage | 200.0 |
Est Cost Emergency | 11692.0 |
Est Cost Other | 0.0 |
Gas Cost In Mcf | 0.0 |
Est Cost Unintentional Release | 0.0 |
Est Cost Intentional Release | 0.0 |
Prpty | 319935.0 |
Commercial Affected | 0.0 |
Industrial Affected | 0.0 |
Residences Affected | 1.0 |
Num Persons Hosp Not Ovnght | 0.0 |
Num Injured Treated By Emt | 0.0 |
Num Resident Building Affctd | 1.0 |
Num Business Building Affctd | 0.0 |
Accident Psig | 24.69 |
Normal Psig | 25.0 |
Mop Psig | 28.0 |
Mop Cfr Section | 192.619(A)(2) View CFR 49 §192 |
Maop Established Date | 1988-07-01 00:00:00 |
Accident Pressure | Pressure Did Not Exceed Maop |
Gas Odorized System Type | Combination Of Odorization Types |
Gas Odorized Level | 0.2 |
Scada In Place Ind | No |
Accident Identifier | Notification From Emergency Responder |
Investigation Status | No, the facility was not monitored by a controller(s) at the time of the incident |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Other Incident Cause |
Cause Details | Unknown |
Other Type | Unknown |
Unknown Subtype | Still Under Investigation, Cause Of Incident To Be Determined* (*supplemental Report Required) |
Preparer Name | P***** L* R*** |
Preparer Title | Manager - Compliance And Qa |
Preparer Email | P****@s*********.com |
Preparer Telephone | 2244570663 |
Local Contact Name | P***** L* R*** |
Local Contact Email | P****@s*********.com |
Local Contact Telephone | 2244570663 |
Authorizer Name | P***** L* R*** |
Authorizer Title | Manager - Compliance And Qa |
Authorizer Telephone | 2244570663 |
Authorizer Email | P****@s*********.com |
Narrative | Per national transportation safety board ("ntsb") investigation id pld25fr006, the following information is preliminary and subject to change. On june 12, 2025, a natural gas-fueled explosion and fire destroyed a single-family residence at 14109 kenneth court in crestwood, illinois. The explosion killed one person and damaged neighboring residences. Nicor gas provided natural gas service to the home and the neighboring residences. The crestwood fire department responded to the explosion and fire at about 2:16 p.M. Nicor gas arrived on the scene at about 2:40 p.M. And disconnected and capped the service line at about 4:44 p.M. On june 13, 2025, nicor gas performed a pressure test of the service line. The service line did not hold pressure, indicating a leak. After national transportation safety board (ntsb) investigators arrived on scene, nicor gas performed flow tests on the service line to estimate the size of the leak. Barhole testing conducted by nicor gas confirmed the presence of gas in the ground near the foundation of the home. Nicor gas located and marked underground utilities at the accident site and obtained gas consumption data from the home�s gas meter. While on scene, ntsb investigators completed the following actions: � examined the accident site, � secured a section of the service line containing the leak for examination at the ntsb�s materials laboratory in washington, dc, � reviewed the accident home�s gas consumption data over the past year, which was higher than the neighboring residences, � requested documentation from nicor gas, � requested communication logs from nicor gas and the crestwood fire department, � and conducted interviews. (https://www.Ntsb.Gov/investigations/pages/pld25fr006.Aspx) |
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