GD incident on 2025-05-22 — MO

Operator
Spire Missouri Inc. West
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 1 injury
Property damage (nominal)
$175,915
Incident datetime
2025-05-22 00:00 UTC
Report number
Location
MO, JACKSON
Narrative
A third-party excavator was backfilling when they damaged a 1-inch nipple on a 10-inch steel natural gas pipeline. The natural gas ignited during the company's response to the damage. The condition was made safe by closing two nearby valves and repair was completed by removing the damaged 1-inch nipple and welding on a pumpkin. Two company employees were injured as a result of the incident and transported to the hospital. One employee was admitted for extended treatment and the second employee was treated and released. A mini-excavator and a nearby regulator station were also damaged by the fire during the incident. A 48-hour update to the nrc was made on april 24, 2025, at 15:34 - report number 1429366
Detailed record list
Report Received Date
2025-05-22 00:00:00
Iyear
2025.0
Report Number
20250031.0
Supplemental Number
41094.0
Report Type
Supplemental Final
Operator Id
Name
Spire Missouri Inc. West
Operator Street Address
700 Market Street
Operator City Name
Saint Louis
Operator State Abbreviation
MO
Operator Postal Code
63101.0
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
9509 Grandview Rd
Location City Name
Kansas City
Location County Name
Jackson
Location State Abbreviation
MO
Location Postal Code
64137.0
Location Latitude
Location Longitude
-94.54989956
Flow Cont Main Valve Ind
Yes
Nrc Rpt Num
Additional Nrc Report Numbers
1429366.0
Commodity Released Type
Natural Gas
Unintentional Release
186.22
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
1
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Ignite Ind
Yes
How Extinguished
Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf
159.62
Explode Ind
No
Num Pub Evacuated
16.0
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
30.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1929.0
Pipe Diameter
10.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Longitudinal Erw - Unknown Frequency
Release Type
Leak
Leak Type
Other
Leak Type Other
.5" Hole From 1-Inch Nipple
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
175915.0
Est Cost Emergency
500.0
Est Cost Other
0.0
Gas Cost In Mcf
6.333
Est Cost Unintentional Release
1179.0
Est Cost Intentional Release
0.0
Prpty
177594.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
16.0
Num Persons Hosp Not Ovnght
1.0
Num Injured Treated By Emt
1.0
Num Resident Building Affctd
16.0
Num Business Building Affctd
0.0
Accident Psig
130.24
Normal Psig
130.0
Mop Psig
150.0
Mop Cfr Section
192.619(A)(3)
Maop Established Date
1970-07-01 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
0.4
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller(s) actions did not result in any abnormal pipeline operation or pressures that caused or contributed to the incident.
Employee Drug Test Ind
Yes
Num Employees Tested
2
Num Employees Failed
0
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
City Street
Joint Trench Ind
No
Cross Bore Ind
No
Depth Of Grade
18� � 36�
Excavator Type
Utility
Excavator Equipment
Backhoe/trackhoe
Work Performed
Water
One Call Notified Ind
Yes
One Call Ticket Num
251045717.0
White Lined Ind
Yes
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
24.0
Root Cause Category
Excavation Issue
Root Cause Type
Improper Backfilling Practices
Preparer Name
E*** M******
Preparer Title
Manager Distribution Integrity
Preparer Email
E***********@s**********.com
Preparer Telephone
314-349-2932
Local Contact Name
E*** M******
Local Contact Email
E***********@s**********.com
Local Contact Telephone
314-349-2932
Authorizer Name
R**** W*****
Authorizer Title
Director - Pipeline And System Integrity
Authorizer Telephone
205-337-1337
Authorizer Email
R***********@s**********.com
Narrative
A third-party excavator was backfilling when they damaged a 1-inch nipple on a 10-inch steel natural gas pipeline. The natural gas ignited during the company's response to the damage. The condition was made safe by closing two nearby valves and repair was completed by removing the damaged 1-inch nipple and welding on a pumpkin. Two company employees were injured as a result of the incident and transported to the hospital. One employee was admitted for extended treatment and the second employee was treated and released. A mini-excavator and a nearby regulator station were also damaged by the fire during the incident. A 48-hour update to the nrc was made on april 24, 2025, at 15:34 - report number 1429366
Report Received Date 2025-05-22 00:00:00
Iyear 2025.0
Report Number 20250031.0
Supplemental Number 41094.0
Report Type Supplemental Final
Operator Id 30769 PHMSA Enforcement
Name Spire Missouri Inc. West
Operator Street Address 700 Market Street
Operator City Name Saint Louis
Operator State Abbreviation MO
Operator Postal Code 63101.0
Time Zone Central
Daylight Savings Ind Yes
Location Street Address 9509 Grandview Rd
Location City Name Kansas City
Location County Name Jackson
Location State Abbreviation MO
Location Postal Code 64137.0
Location Latitude 38.95367504 Google Maps OpenStreetMap
Location Longitude -94.54989956 Google Maps OpenStreetMap
Flow Cont Main Valve Ind Yes
Nrc Rpt Num 1429178.0 NRC Report How to search
Additional Nrc Report Numbers 1429366.0
Commodity Released Type Natural Gas
Unintentional Release 186.22
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 1
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 1
Ignite Ind Yes
How Extinguished Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf 159.62
Explode Ind No
Num Pub Evacuated 16.0
Communication State Fed Ind Yes
Party Initiated Communication Operator
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 30.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1929.0
Pipe Diameter 10.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Longitudinal Erw - Unknown Frequency
Release Type Leak
Leak Type Other
Leak Type Other .5" Hole From 1-Inch Nipple
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 175915.0
Est Cost Emergency 500.0
Est Cost Other 0.0
Gas Cost In Mcf 6.333
Est Cost Unintentional Release 1179.0
Est Cost Intentional Release 0.0
Prpty 177594.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 16.0
Num Persons Hosp Not Ovnght 1.0
Num Injured Treated By Emt 1.0
Num Resident Building Affctd 16.0
Num Business Building Affctd 0.0
Accident Psig 130.24
Normal Psig 130.0
Mop Psig 150.0
Mop Cfr Section 192.619(A)(3) View CFR 49 §192
Maop Established Date 1970-07-01 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Level 0.4
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller(s) actions did not result in any abnormal pipeline operation or pressures that caused or contributed to the incident.
Employee Drug Test Ind Yes
Num Employees Tested 2
Num Employees Failed 0
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind No
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype City Street
Joint Trench Ind No
Cross Bore Ind No
Depth Of Grade 18� � 36�
Excavator Type Utility
Excavator Equipment Backhoe/trackhoe
Work Performed Water
One Call Notified Ind Yes
One Call Ticket Num 251045717.0
White Lined Ind Yes
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 24.0
Root Cause Category Excavation Issue
Root Cause Type Improper Backfilling Practices
Preparer Name E*** M******
Preparer Title Manager Distribution Integrity
Preparer Email E***********@s**********.com
Preparer Telephone 314-349-2932
Local Contact Name E*** M******
Local Contact Email E***********@s**********.com
Local Contact Telephone 314-349-2932
Authorizer Name R**** W*****
Authorizer Title Director - Pipeline And System Integrity
Authorizer Telephone 205-337-1337
Authorizer Email R***********@s**********.com
Narrative A third-party excavator was backfilling when they damaged a 1-inch nipple on a 10-inch steel natural gas pipeline. The natural gas ignited during the company's response to the damage. The condition was made safe by closing two nearby valves and repair was completed by removing the damaged 1-inch nipple and welding on a pumpkin. Two company employees were injured as a result of the incident and transported to the hospital. One employee was admitted for extended treatment and the second employee was treated and released. A mini-excavator and a nearby regulator station were also damaged by the fire during the incident. A 48-hour update to the nrc was made on april 24, 2025, at 15:34 - report number 1429366

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