GD incident on 2025-05-09 — MO

Operator
The Empire District Gas Company
Cause
Miscellaneous Root Causes
Commodity
Natural Gas
Program
GD
Damage and Injuries
1 fatality 2 injuries
Property damage (nominal)
$616,386
Incident datetime
2025-05-09 00:00 UTC
Report number
Location
MO, LAFAYETTE
Narrative
Please refer to the 05-05-2025 ntsb preliminary report for its in docket# pld25lr004, available at the link provided. (https://www.Ntsb.Gov/investigations/pages/pld25lr004.Aspx) contains the following description of the incident: 'on april 9, 2025, about 7:42 p.M. Local time, a natural gas-fueled explosion and fires in lexington, missouri, destroyed one single-family residence (1717 franklin avenue) and damaged two others, resulting in one fatality and two injuries. The explosion occurred more than 3 hours after alfra construction, llc, a drilling subcontractor installing a fiber optic line for sellenriek construction, drilled into an unmarked section of a capped underground gas distribution main located near the residences. The gas main was operated by liberty utilities, a subsidiary of algonquin power and utilities corporation, which provides gas service to the area. 'five days before the accident, on april 4, alfra construction called missouri 811 to have any buried utilities in the area marked.[2] liberty utilities sent a locator to mark its assets by painting and flagging and reported that this work was finished on april 7.(3) the location of the [capped] gas main section involved in the accident was not identified or marked during this process. 'shortly after 4:00 p.M. On the day of the accident, the alfra construction work crew member operating the drill felt the drill strike an object. The work crew saw and smelled odorized natural gas being released. The work crew's supervisor called 911 and 811 and reported a damaged gas line. Units from the lexington fire department arrived about 4:20 p.M.; personnel from liberty utilities began arriving about 4:39 p.M. Liberty utilities personnel attempted to isolate the leak by squeezing off the main but did not succeed in stopping the flow of gas.[4] at the direction of liberty utilities, a business about 15 feet from the leak was evacuated before the explosion. Other nearby buildings were not evacuated, including the destroyed and damaged residences, which ranged from 80 to 160 feet from the leak. The damaged main was isolated about 8:10 p.M., after the explosion. The gas main involved in this accident was a 4-inch polyethylene (plastic) pipe operating at 30 pounds per square inch gauge pressure; its maximum allowable operating pressure was 35 pounds per square inch gauge.'
Detailed record list
Report Received Date
2025-05-09 00:00:00
Iyear
2025.0
Report Number
20250027.0
Supplemental Number
41239.0
Report Type
Supplemental
Operator Id
Name
The Empire District Gas Company
Operator Street Address
602 Joplin Street
Operator City Name
Joplin
Operator State Abbreviation
MO
Operator Postal Code
64801.0
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
1717 Franklin Ave
Location City Name
Lexington
Location County Name
Lafayette
Location State Abbreviation
MO
Location Postal Code
64067.0
Location Latitude
Location Longitude
Flow Cont Main Valve Ind
Yes
Flow Cont Other Ind
Yes
Flow Cont Other Detail
Turned Off Two Gate Stations To Isolate System
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
53.68
Intentional Release
0.0
Fatality Ind
Yes
Num Emp Fatalities
0
Num Contr Fatalities
0
Num Er Fatalities
0
Num Worker Fatalities
0
Num Gp Fatalities
1
Fatal
1
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
2
Injure
2
Ignite Ind
Yes
How Extinguished
Other
How Extinguished Other Detail
Town Gas Flow Was Shut Down At City Gate Stations
Gas Consumed By Fire In Mcf
1
Explode Ind
Yes
Num Pub Evacuated
2.0
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
24.0
Other Underground Facilities
No
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Bored/drilled
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1989.0
Pipe Diameter
4.0
Pipe Specification
Pe2406
Pipe Manufacturer
Unknown
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11.5
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
0.5
Puncture Circum
0.5
Class Location Type
Class 3 Location
Est Cost Oper Paid
525722.0
Est Cost Prop Damage
616386.0
Est Cost Emergency
44085.0
Est Cost Other
0.0
Gas Cost In Mcf
7.0364
Est Cost Unintentional Release
378.0
Est Cost Intentional Release
0.0
Prpty
1186571.0
Commercial Affected
223.0
Industrial Affected
0.0
Residences Affected
1685.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
1685.0
Num Business Building Affctd
223.0
Accident Psig
30.0
Normal Psig
30.0
Mop Psig
35.0
Mop Cfr Section
192.619(A)(4)
Maop Established Date
1988-12-01 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
0.1
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Third party damage
Employee Drug Test Ind
Yes
Num Employees Tested
6
Num Employees Failed
0
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
Unknown
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
City Street
Joint Trench Ind
No
Cross Bore Ind
Yes
Depth Of Grade
18� � 36�
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Telecommunications
One Call Notified Ind
Yes
White Lined Ind
No
Locator Type
Facility Owner
Visible Marks
Unknown/other
Service Interruption
Unknown/other
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Root Cause Not Listed (Comment Required)
Root Cause Type Other
Under Ntsb Investigation,docket#pld25lr004
Preparer Name
R***** S*****
Preparer Title
Regional Director Operations
Preparer Email
R************@l***************.com
Preparer Telephone
573-225-7834
Authorizer Name
M****** D B*****
Authorizer Title
President
Authorizer Telephone
573-755-0108
Authorizer Email
M**********@l***************.com
Narrative
Please refer to the 05-05-2025 ntsb preliminary report for its in docket# pld25lr004, available at the link provided. (https://www.Ntsb.Gov/investigations/pages/pld25lr004.Aspx) contains the following description of the incident: 'on april 9, 2025, about 7:42 p.M. Local time, a natural gas-fueled explosion and fires in lexington, missouri, destroyed one single-family residence (1717 franklin avenue) and damaged two others, resulting in one fatality and two injuries. The explosion occurred more than 3 hours after alfra construction, llc, a drilling subcontractor installing a fiber optic line for sellenriek construction, drilled into an unmarked section of a capped underground gas distribution main located near the residences. The gas main was operated by liberty utilities, a subsidiary of algonquin power and utilities corporation, which provides gas service to the area. 'five days before the accident, on april 4, alfra construction called missouri 811 to have any buried utilities in the area marked.[2] liberty utilities sent a locator to mark its assets by painting and flagging and reported that this work was finished on april 7.(3) the location of the [capped] gas main section involved in the accident was not identified or marked during this process. 'shortly after 4:00 p.M. On the day of the accident, the alfra construction work crew member operating the drill felt the drill strike an object. The work crew saw and smelled odorized natural gas being released. The work crew's supervisor called 911 and 811 and reported a damaged gas line. Units from the lexington fire department arrived about 4:20 p.M.; personnel from liberty utilities began arriving about 4:39 p.M. Liberty utilities personnel attempted to isolate the leak by squeezing off the main but did not succeed in stopping the flow of gas.[4] at the direction of liberty utilities, a business about 15 feet from the leak was evacuated before the explosion. Other nearby buildings were not evacuated, including the destroyed and damaged residences, which ranged from 80 to 160 feet from the leak. The damaged main was isolated about 8:10 p.M., after the explosion. The gas main involved in this accident was a 4-inch polyethylene (plastic) pipe operating at 30 pounds per square inch gauge pressure; its maximum allowable operating pressure was 35 pounds per square inch gauge.'
Report Received Date 2025-05-09 00:00:00
Iyear 2025.0
Report Number 20250027.0
Supplemental Number 41239.0
Report Type Supplemental
Operator Id 12606 PHMSA Enforcement
Name The Empire District Gas Company
Operator Street Address 602 Joplin Street
Operator City Name Joplin
Operator State Abbreviation MO
Operator Postal Code 64801.0
Time Zone Central
Daylight Savings Ind Yes
Location Street Address 1717 Franklin Ave
Location City Name Lexington
Location County Name Lafayette
Location State Abbreviation MO
Location Postal Code 64067.0
Location Latitude 39.184002 Google Maps OpenStreetMap
Location Longitude -93.874447 Google Maps OpenStreetMap
Flow Cont Main Valve Ind Yes
Flow Cont Other Ind Yes
Flow Cont Other Detail Turned Off Two Gate Stations To Isolate System
Nrc Rpt Num 1428183.0 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 53.68
Intentional Release 0.0
Fatality Ind Yes
Num Emp Fatalities 0
Num Contr Fatalities 0
Num Er Fatalities 0
Num Worker Fatalities 0
Num Gp Fatalities 1
Fatal 1
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 2
Injure 2
Ignite Ind Yes
How Extinguished Other
How Extinguished Other Detail Town Gas Flow Was Shut Down At City Gate Stations
Gas Consumed By Fire In Mcf 1
Explode Ind Yes
Num Pub Evacuated 2.0
Communication State Fed Ind Yes
Party Initiated Communication Operator
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 24.0
Other Underground Facilities No
Crossing Yes
Road Crossing Ind Yes
Road Type Bored/drilled
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1989.0
Pipe Diameter 4.0
Pipe Specification Pe2406
Pipe Manufacturer Unknown
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11.5
Material Pe Pipe Code 2406
Release Type Mechanical Puncture
Puncture Axial 0.5
Puncture Circum 0.5
Class Location Type Class 3 Location
Est Cost Oper Paid 525722.0
Est Cost Prop Damage 616386.0
Est Cost Emergency 44085.0
Est Cost Other 0.0
Gas Cost In Mcf 7.0364
Est Cost Unintentional Release 378.0
Est Cost Intentional Release 0.0
Prpty 1186571.0
Commercial Affected 223.0
Industrial Affected 0.0
Residences Affected 1685.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 1685.0
Num Business Building Affctd 223.0
Accident Psig 30.0
Normal Psig 30.0
Mop Psig 35.0
Mop Cfr Section 192.619(A)(4) View CFR 49 §192
Maop Established Date 1988-12-01 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Level 0.1
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Third party damage
Employee Drug Test Ind Yes
Num Employees Tested 6
Num Employees Failed 0
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind Unknown
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype City Street
Joint Trench Ind No
Cross Bore Ind Yes
Depth Of Grade 18� � 36�
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Telecommunications
One Call Notified Ind Yes
White Lined Ind No
Locator Type Facility Owner
Visible Marks Unknown/other
Service Interruption Unknown/other
Root Cause Category Miscellaneous Root Causes
Root Cause Type Root Cause Not Listed (Comment Required)
Root Cause Type Other Under Ntsb Investigation,docket#pld25lr004
Preparer Name R***** S*****
Preparer Title Regional Director Operations
Preparer Email R************@l***************.com
Preparer Telephone 573-225-7834
Authorizer Name M****** D B*****
Authorizer Title President
Authorizer Telephone 573-755-0108
Authorizer Email M**********@l***************.com
Narrative Please refer to the 05-05-2025 ntsb preliminary report for its in docket# pld25lr004, available at the link provided. (https://www.Ntsb.Gov/investigations/pages/pld25lr004.Aspx) contains the following description of the incident: 'on april 9, 2025, about 7:42 p.M. Local time, a natural gas-fueled explosion and fires in lexington, missouri, destroyed one single-family residence (1717 franklin avenue) and damaged two others, resulting in one fatality and two injuries. The explosion occurred more than 3 hours after alfra construction, llc, a drilling subcontractor installing a fiber optic line for sellenriek construction, drilled into an unmarked section of a capped underground gas distribution main located near the residences. The gas main was operated by liberty utilities, a subsidiary of algonquin power and utilities corporation, which provides gas service to the area. 'five days before the accident, on april 4, alfra construction called missouri 811 to have any buried utilities in the area marked.[2] liberty utilities sent a locator to mark its assets by painting and flagging and reported that this work was finished on april 7.(3) the location of the [capped] gas main section involved in the accident was not identified or marked during this process. 'shortly after 4:00 p.M. On the day of the accident, the alfra construction work crew member operating the drill felt the drill strike an object. The work crew saw and smelled odorized natural gas being released. The work crew's supervisor called 911 and 811 and reported a damaged gas line. Units from the lexington fire department arrived about 4:20 p.M.; personnel from liberty utilities began arriving about 4:39 p.M. Liberty utilities personnel attempted to isolate the leak by squeezing off the main but did not succeed in stopping the flow of gas.[4] at the direction of liberty utilities, a business about 15 feet from the leak was evacuated before the explosion. Other nearby buildings were not evacuated, including the destroyed and damaged residences, which ranged from 80 to 160 feet from the leak. The damaged main was isolated about 8:10 p.M., after the explosion. The gas main involved in this accident was a 4-inch polyethylene (plastic) pipe operating at 30 pounds per square inch gauge pressure; its maximum allowable operating pressure was 35 pounds per square inch gauge.'

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