GD incident on 2025-04-11 — PA

Operator
Peoples Natural Gas Company Llc
Cause
Other Incident Cause
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$164,106
Incident datetime
2025-04-11 00:00 UTC
Report number
Location
PA, WESTMORELAND
Narrative
A leak occurred on a distribution pipeline along white cloud road in new kensington, pa on 3/9/2025. Initial responses were to isolate and expose the leaking pipeline for repairs. Due to a safety concern regarding the depth of the pipe it was decided upon to renew the mainline to eliminate this leaking pipeline. New plastic mainline was installed on and tied in on 3/11/2025.
Detailed record list
Report Received Date
2025-04-11 00:00:00
Iyear
2025.0
Report Number
20250020.0
Supplemental Number
40746.0
Report Type
Original Final
Operator Id
Name
Peoples Natural Gas Company Llc
Operator Street Address
375 North Shore Drive Suite 600
Operator City Name
Pittsburgh
Operator State Abbreviation
PA
Operator Postal Code
15212.0
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Street Address
859 White Cloud Rd
Location City Name
New Kensington
Location County Name
Westmoreland
Location State Abbreviation
PA
Location Postal Code
15068.0
Location Latitude
Location Longitude
Flow Cont Key Crit Ind
Yes
Nrc Rpt Num
Additional Nrc Report Numbers
1425619.0
Commodity Released Type
Natural Gas
Unintentional Release
3403.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
144.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1972.0
Pipe Diameter
12.0
Pipe Specification
Api-5lx-42
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Longitudinal Erw - Unknown Frequency
Wt Steel
0.219
Release Type
Leak
Leak Type
Other
Leak Type Other
Leak Not Exposed.
Class Location Type
Class 1 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
164106.0
Est Cost Emergency
9974.0
Est Cost Other
0.0
Gas Cost In Mcf
10.6952
Est Cost Unintentional Release
36396.0
Est Cost Intentional Release
0.0
Prpty
210476.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
41.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
41.0
Num Business Building Affctd
0.0
Accident Psig
82.0
Normal Psig
82.0
Mop Psig
115.0
Mop Cfr Section
192.619(A)(1)
Maop Established Date
1972-08-23 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Odorized By Others
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The control room did not contribute to this leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Incident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Investigation Complete, Cause Of Incident Unknown
Incident Unknown Comments
The Leaking Section Of Pipe Was Not Exposed. Pipeline Was Replaced.
Preparer Name
T***** P*******
Preparer Title
Compliance Manager
Preparer Email
T****************@p**********.com
Preparer Telephone
412-554-3433
Local Contact Name
T***** P*******
Local Contact Email
T****************@p**********.com
Local Contact Telephone
412-554-3433
Authorizer Name
E***** A* P******
Authorizer Title
Vice President Reliability
Authorizer Telephone
(412) 258-4453
Authorizer Email
E***************@p**********.com
Narrative
A leak occurred on a distribution pipeline along white cloud road in new kensington, pa on 3/9/2025. Initial responses were to isolate and expose the leaking pipeline for repairs. Due to a safety concern regarding the depth of the pipe it was decided upon to renew the mainline to eliminate this leaking pipeline. New plastic mainline was installed on and tied in on 3/11/2025.
Report Received Date 2025-04-11 00:00:00
Iyear 2025.0
Report Number 20250020.0
Supplemental Number 40746.0
Report Type Original Final
Operator Id 15350 PHMSA Enforcement
Name Peoples Natural Gas Company Llc
Operator Street Address 375 North Shore Drive Suite 600
Operator City Name Pittsburgh
Operator State Abbreviation PA
Operator Postal Code 15212.0
Time Zone Eastern
Daylight Savings Ind Yes
Location Street Address 859 White Cloud Rd
Location City Name New Kensington
Location County Name Westmoreland
Location State Abbreviation PA
Location Postal Code 15068.0
Location Latitude 40.550322 Google Maps OpenStreetMap
Location Longitude -79.644814 Google Maps OpenStreetMap
Flow Cont Key Crit Ind Yes
Nrc Rpt Num 1425478.0 NRC Report How to search
Additional Nrc Report Numbers 1425619.0
Commodity Released Type Natural Gas
Unintentional Release 3403.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 144.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1972.0
Pipe Diameter 12.0
Pipe Specification Api-5lx-42
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Longitudinal Erw - Unknown Frequency
Wt Steel 0.219
Release Type Leak
Leak Type Other
Leak Type Other Leak Not Exposed.
Class Location Type Class 1 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 164106.0
Est Cost Emergency 9974.0
Est Cost Other 0.0
Gas Cost In Mcf 10.6952
Est Cost Unintentional Release 36396.0
Est Cost Intentional Release 0.0
Prpty 210476.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 41.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 41.0
Num Business Building Affctd 0.0
Accident Psig 82.0
Normal Psig 82.0
Mop Psig 115.0
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 1972-08-23 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Odorized By Others
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The control room did not contribute to this leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Incident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Investigation Complete, Cause Of Incident Unknown
Incident Unknown Comments The Leaking Section Of Pipe Was Not Exposed. Pipeline Was Replaced.
Preparer Name T***** P*******
Preparer Title Compliance Manager
Preparer Email T****************@p**********.com
Preparer Telephone 412-554-3433
Local Contact Name T***** P*******
Local Contact Email T****************@p**********.com
Local Contact Telephone 412-554-3433
Authorizer Name E***** A* P******
Authorizer Title Vice President Reliability
Authorizer Telephone (412) 258-4453
Authorizer Email E***************@p**********.com
Narrative A leak occurred on a distribution pipeline along white cloud road in new kensington, pa on 3/9/2025. Initial responses were to isolate and expose the leaking pipeline for repairs. Due to a safety concern regarding the depth of the pipe it was decided upon to renew the mainline to eliminate this leaking pipeline. New plastic mainline was installed on and tied in on 3/11/2025.

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