GD incident on 2025-04-10 — MS

Operator
Atmos Energy Corporation - Mississippi
Cause
Other Incident Cause
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 2 injuries
Property damage (nominal)
$100,000
Incident datetime
2025-04-10 00:00 UTC
Report number
Location
MS, LEE
Narrative
Atmos energy's second-party contractor was attempting to complete a stopple fitting when the completion plug was ejected, resulting in injuries to three contractor employees and a release of natural gas. A mainline valve was closed, eliminating the release of natural gas.
Detailed record list
Report Received Date
2025-04-10 00:00:00
Iyear
2025.0
Report Number
20250019.0
Supplemental Number
40745.0
Report Type
Original
Operator Id
Name
Atmos Energy Corporation - Mississippi
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240.0
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
137 County Road 660
Location City Name
Plantersville
Location County Name
Lee
Location State Abbreviation
MS
Location Postal Code
38862.0
Location Latitude
Location Longitude
Flow Cont Main Valve Ind
Yes
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
5874.0
Intentional Release
388.2
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
2
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
2
Ignite Ind
No
Num Pub Evacuated
0.0
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
84.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Other
System Part Details
Completion Plug Of A Stopple Fitting
Installation Year
2025.0
Manufactured Year
2024.0
Material Involved
Other
Material Details
Completion Plug Of A Stopple Fitting
Release Type
Other
Release Type Details
The Completion Plug Of A Stopple Fitting Was Ejected.
Class Location Type
Class 2 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
100000.0
Est Cost Emergency
50000.0
Est Cost Other
0.0
Gas Cost In Mcf
3.4944
Est Cost Unintentional Release
20526.0
Est Cost Intentional Release
1357.0
Prpty
171883.0
Commercial Affected
2285.0
Industrial Affected
215.0
Residences Affected
14998.0
Num Persons Hosp Not Ovnght
1.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
0.0
Accident Psig
330.0
Normal Psig
330.0
Mop Psig
385.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1991-10-10 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
8.8
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
There were contractor and inspection personnel onsite who called the appropriate first responders along with atmos energy operation personnel. Gas control did not perform any action that contributed to the incident.
Employee Drug Test Ind
Yes
Num Employees Tested
1
Num Employees Failed
0
Contractor Drug Test Ind
Yes
Num Contractors Tested
9
Num Contractors Failed
1
Cause
Other Incident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Still Under Investigation, Cause Of Incident To Be Determined* (*supplemental Report Required)
Preparer Name
F**** H* R***
Preparer Title
Manager Engineering Services
Preparer Email
F*********@a**********.com
Preparer Telephone
(601) 592-5313
Preparer Fax
(601) 360-1492
Local Contact Name
T**** H******
Local Contact Email
T************@a**********.com
Local Contact Telephone
(662) 690-5202
Authorizer Name
C*** K***
Authorizer Title
Vice-President Technical Services
Authorizer Telephone
(601) 624-1903
Authorizer Email
C********@a**********.com
Narrative
Atmos energy's second-party contractor was attempting to complete a stopple fitting when the completion plug was ejected, resulting in injuries to three contractor employees and a release of natural gas. A mainline valve was closed, eliminating the release of natural gas.
Report Received Date 2025-04-10 00:00:00
Iyear 2025.0
Report Number 20250019.0
Supplemental Number 40745.0
Report Type Original
Operator Id 12582 PHMSA Enforcement
Name Atmos Energy Corporation - Mississippi
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240.0
Time Zone Central
Daylight Savings Ind Yes
Location Street Address 137 County Road 660
Location City Name Plantersville
Location County Name Lee
Location State Abbreviation MS
Location Postal Code 38862.0
Location Latitude 34.16486 Google Maps OpenStreetMap
Location Longitude -88.61762 Google Maps OpenStreetMap
Flow Cont Main Valve Ind Yes
Nrc Rpt Num 1425629.0 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 5874.0
Intentional Release 388.2
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 2
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 2
Ignite Ind No
Num Pub Evacuated 0.0
Communication State Fed Ind Yes
Party Initiated Communication Operator
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 84.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Other
System Part Details Completion Plug Of A Stopple Fitting
Installation Year 2025.0
Manufactured Year 2024.0
Material Involved Other
Material Details Completion Plug Of A Stopple Fitting
Release Type Other
Release Type Details The Completion Plug Of A Stopple Fitting Was Ejected.
Class Location Type Class 2 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 100000.0
Est Cost Emergency 50000.0
Est Cost Other 0.0
Gas Cost In Mcf 3.4944
Est Cost Unintentional Release 20526.0
Est Cost Intentional Release 1357.0
Prpty 171883.0
Commercial Affected 2285.0
Industrial Affected 215.0
Residences Affected 14998.0
Num Persons Hosp Not Ovnght 1.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 0.0
Accident Psig 330.0
Normal Psig 330.0
Mop Psig 385.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1991-10-10 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Level 8.8
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details There were contractor and inspection personnel onsite who called the appropriate first responders along with atmos energy operation personnel. Gas control did not perform any action that contributed to the incident.
Employee Drug Test Ind Yes
Num Employees Tested 1
Num Employees Failed 0
Contractor Drug Test Ind Yes
Num Contractors Tested 9
Num Contractors Failed 1
Cause Other Incident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Still Under Investigation, Cause Of Incident To Be Determined* (*supplemental Report Required)
Preparer Name F**** H* R***
Preparer Title Manager Engineering Services
Preparer Email F*********@a**********.com
Preparer Telephone (601) 592-5313
Preparer Fax (601) 360-1492
Local Contact Name T**** H******
Local Contact Email T************@a**********.com
Local Contact Telephone (662) 690-5202
Authorizer Name C*** K***
Authorizer Title Vice-President Technical Services
Authorizer Telephone (601) 624-1903
Authorizer Email C********@a**********.com
Narrative Atmos energy's second-party contractor was attempting to complete a stopple fitting when the completion plug was ejected, resulting in injuries to three contractor employees and a release of natural gas. A mainline valve was closed, eliminating the release of natural gas.

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