Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2024-12-13 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$1,500
Incident datetime
2024-12-13 00:00 UTC
Report number
Location
OK
Narrative
During a facility inspection an operator found a leak around a 4-way prover valve at colorado city terminal. The operator immediately called their supervisor to report the leak. It was determined the bottom flange nuts had backed off causing the release. Discussions with the valve company confirmed that the valve was properly installed per the manufacturer's specifications in 2023. Local ops locked out and tagged out the prover and performed a thorough inspection of the 4-way valve. Soft goods and internal mechanical components did not show any signs of wear, indicative of good working condition. The valve was reassembled and reinstalled. Per recommendations from the valve company, thread lock was applied to the bottom blind flange studs to ensure the nuts would not back off. Local ops conducted several manual proves and were onsite to monitor the system throughout the entire duration of the prove to inspect for leaks. There were no leaks observed, and the prover was approved for return to service.
Detailed record list
Report Received Date
2024-12-13 00:00:00
Iyear
2024
Report Number
20240290
Supplemental Number
40353
Report Type
Supplemental
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
32.530053
Location Longitude
-100.848981
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.23
Recovered Bbls
0.23
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
The Prover Was Isolated From Operation And Repairs Were Made
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Colorado City
Segment Name
Fac Id 850
Onshore State Abbreviation
Tx
Onshore Postal Code
79526
Onshore City Name
Hermleigh
Onshore County Name
Scurry
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Installation Year
2023
Manufactured Year
2023
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
1500
Est Cost Emergency
0
Est Cost Environmental
1200
Est Cost Other
0
Prpty
2700
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
200
Mop Psig
275
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2014-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller did not cause or contribute to the release. Field identified a small release from a loose flange connection
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Mechanical Coupling
Additional Vibration Ind
Yes
Preparer Name
G*** C*********
Preparer Email
G**************@o****.com
Preparer Telephone
9183818066
Prepared Date
2024-12-23 00:00:00
Local Contact Name
R*** M****
Local Contact Email
R*********@o****.com
Local Contact Telephone
5807410185
Authorizer Name
R*** M****
Authorizer Telephone
5807410185
Authorizer Email
R*********@o****.com
Narrative
During a facility inspection an operator found a leak around a 4-way prover valve at colorado city terminal. The operator immediately called their supervisor to report the leak. It was determined the bottom flange nuts had backed off causing the release. Discussions with the valve company confirmed that the valve was properly installed per the manufacturer's specifications in 2023. Local ops locked out and tagged out the prover and performed a thorough inspection of the 4-way valve. Soft goods and internal mechanical components did not show any signs of wear, indicative of good working condition. The valve was reassembled and reinstalled. Per recommendations from the valve company, thread lock was applied to the bottom blind flange studs to ensure the nuts would not back off. Local ops conducted several manual proves and were onsite to monitor the system throughout the entire duration of the prove to inspect for leaks. There were no leaks observed, and the prover was approved for return to service.
Report Received Date | 2024-12-13 00:00:00 |
---|---|
Iyear | 2024 |
Report Number | 20240290 |
Supplemental Number | 40353 |
Report Type | Supplemental |
Operator Id | 22610 PHMSA Enforcement |
Name | Magellan Pipeline Company, Lp |
Operator Street Address | 100 West 5th Street |
Operator City Name | Tulsa |
Operator State Abbreviation | OK |
Operator Postal Code | 74103 |
Time Zone | Central |
Daylight Savings Ind | No |
Location Latitude | 32.530053 Google Maps OpenStreetMap |
Location Longitude | -100.848981 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 0.23 |
Recovered Bbls | 0.23 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Pump/meter Station Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | No |
Shutdown Explain | The Prover Was Isolated From Operation And Repairs Were Made |
Communication State Fed Ind | No |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Colorado City |
Segment Name | Fac Id 850 |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 79526 |
Onshore City Name | Hermleigh |
Onshore County Name | Scurry |
Designated Location | Milepost |
Designated Name | 0 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Meter/prover |
Installation Year | 2023 |
Manufactured Year | 2023 |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Connection Failure |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 0 |
Est Cost Prop Damage | 1500 |
Est Cost Emergency | 0 |
Est Cost Environmental | 1200 |
Est Cost Other | 0 |
Prpty | 2700 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 200 |
Mop Psig | 275 |
Mop Cfr Section | Internal Design Pressure �195.406(A)(1) View CFR 49 §192 |
Maop Established Date | 2014-01-01 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | The controller did not cause or contribute to the release. Field identified a small release from a loose flange connection |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Equipment Failure |
Cause Details | Threaded Connection/coupling Failure |
Eq Failure Type | Threaded Connection/coupling Failure |
Other Stripped Ind | Mechanical Coupling |
Additional Vibration Ind | Yes |
Preparer Name | G*** C********* |
Preparer Email | G**************@o****.com |
Preparer Telephone | 9183818066 |
Prepared Date | 2024-12-23 00:00:00 |
Local Contact Name | R*** M**** |
Local Contact Email | R*********@o****.com |
Local Contact Telephone | 5807410185 |
Authorizer Name | R*** M**** |
Authorizer Telephone | 5807410185 |
Authorizer Email | R*********@o****.com |
Narrative | During a facility inspection an operator found a leak around a 4-way prover valve at colorado city terminal. The operator immediately called their supervisor to report the leak. It was determined the bottom flange nuts had backed off causing the release. Discussions with the valve company confirmed that the valve was properly installed per the manufacturer's specifications in 2023. Local ops locked out and tagged out the prover and performed a thorough inspection of the 4-way valve. Soft goods and internal mechanical components did not show any signs of wear, indicative of good working condition. The valve was reassembled and reinstalled. Per recommendations from the valve company, thread lock was applied to the bottom blind flange studs to ensure the nuts would not back off. Local ops conducted several manual proves and were onsite to monitor the system throughout the entire duration of the prove to inspect for leaks. There were no leaks observed, and the prover was approved for return to service. |
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