HL incident on 2024-12-11 — TX

Operator
Boardwalk Louisiana Midstream, Llc
Cause
Other Outside Force Damage
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$48,680
Incident datetime
2024-12-11 00:00 UTC
Report number
Location
TX
Narrative
On 11/27/2024 at approximately 02:30, boardwalk louisiana midstream's (blm) control center received scada alarms at ashland road rsd site for high lel and low pressure on the downstream transmitter; operations personnel were dispatched to investigate. When operations personnel arrived, first responders were onsite responding to a vehicle accident in which the vehicle struck the valve site and caused the ethylene leak. Operations personnel discovered ethylene venting into the air with the wind blowing ethylene across ashland road. Operations personnel requested the control center close the upstream main line valve. Once inside the fenced area, operations personnel determined that tubing was damaged by the vehicle and they were able to isolate a 1/2-inch ball valve going to the tubing. Once the ball valve was closed, the ethylene leak stopped within approximately 2 minutes. At approximately 04:45, the site was deemed safe to reopen the mainline valve and control center personnel did so. Operations personnel repaired the damaged tubing and adjusted the pressure transmitter and the facility was returned to service.
Detailed record list
Report Received Date
2024-12-11 00:00:00
Iyear
2024
Report Number
20240287
Supplemental Number
40308
Report Type
Original Final
Operator Id
Name
Boardwalk Louisiana Midstream, Llc
Operator Street Address
9 Greenway Plaza
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77046
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethylene
Unintentional Release Bbls
99
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Closed Upstream Mainline Valve But Did Not Shut Down Pipeline.
Communication State Fed Ind
Yes
Party Initiated Communication
Local/state/federal Emergency Responder
Nrc Rpt Num
Additional Nrc Report Numbers
1417573
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
No Downstream Action Was Required.
Num Pub Evacuated
0
Pipe Fac Name
Ashland Road Valve Site
Segment Name
Blm-705
Onshore State Abbreviation
La
Onshore Postal Code
70725
Onshore City Name
Geismar
Onshore County Name
Ascension
Designated Location
Survey Station No.
Designated Name
308+55
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tubing
Tubing Material
Stainless Steel
Tubing Type
Rigid
Installation Year
1979
Manufactured Year
1979
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel Tubing
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
2787
Est Cost Prop Damage
48680
Est Cost Emergency
992
Est Cost Environmental
0
Est Cost Other
0
Prpty
52459
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1178
Mop Psig
1440
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1978-04-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype
Third Party
Driver Issued Citation Ind
Yes
Citation Dui Ind
Yes
Citation Other Ind
Yes
Citation Other Detail
Careless Operation
Driver In Control Ind
Yes
Estimated Speed Unknown Ind
Yes
Vehicle Type
Passenger Car
Vehicle Travel From
Roadway
Vehicle Travel Distance Ft
80
Protections Installed Ind
Yes
Protection Barricades Ind
Yes
Preparer Name
S****** M********
Preparer Title
Compliance Program Leader
Preparer Email
S****************@b**********.com
Preparer Telephone
2709035764
Prepared Date
2024-12-11 00:00:00
Authorizer Name
T*** B****
Authorizer Telephone
2703146546
Authorizer Title
Manager Compliance Services
Authorizer Email
T*********@b**********.com
Narrative
On 11/27/2024 at approximately 02:30, boardwalk louisiana midstream's (blm) control center received scada alarms at ashland road rsd site for high lel and low pressure on the downstream transmitter; operations personnel were dispatched to investigate. When operations personnel arrived, first responders were onsite responding to a vehicle accident in which the vehicle struck the valve site and caused the ethylene leak. Operations personnel discovered ethylene venting into the air with the wind blowing ethylene across ashland road. Operations personnel requested the control center close the upstream main line valve. Once inside the fenced area, operations personnel determined that tubing was damaged by the vehicle and they were able to isolate a 1/2-inch ball valve going to the tubing. Once the ball valve was closed, the ethylene leak stopped within approximately 2 minutes. At approximately 04:45, the site was deemed safe to reopen the mainline valve and control center personnel did so. Operations personnel repaired the damaged tubing and adjusted the pressure transmitter and the facility was returned to service.
Report Received Date 2024-12-11 00:00:00
Iyear 2024
Report Number 20240287
Supplemental Number 40308
Report Type Original Final
Operator Id 39138 PHMSA Enforcement
Name Boardwalk Louisiana Midstream, Llc
Operator Street Address 9 Greenway Plaza
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77046
Time Zone Central
Daylight Savings Ind No
Location Latitude 30.18478 Google Maps OpenStreetMap
Location Longitude -90.98617 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethylene
Unintentional Release Bbls 99
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Closed Upstream Mainline Valve But Did Not Shut Down Pipeline.
Communication State Fed Ind Yes
Party Initiated Communication Local/state/federal Emergency Responder
Nrc Rpt Num 1417472 NRC Report How to search
Additional Nrc Report Numbers 1417573
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail No Downstream Action Was Required.
Num Pub Evacuated 0
Pipe Fac Name Ashland Road Valve Site
Segment Name Blm-705
Onshore State Abbreviation La
Onshore Postal Code 70725
Onshore City Name Geismar
Onshore County Name Ascension
Designated Location Survey Station No.
Designated Name 308+55
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Tubing
Tubing Material Stainless Steel
Tubing Type Rigid
Installation Year 1979
Manufactured Year 1979
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel Tubing
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 2787
Est Cost Prop Damage 48680
Est Cost Emergency 992
Est Cost Environmental 0
Est Cost Other 0
Prpty 52459
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1178
Mop Psig 1440
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 1978-04-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype Third Party
Driver Issued Citation Ind Yes
Citation Dui Ind Yes
Citation Other Ind Yes
Citation Other Detail Careless Operation
Driver In Control Ind Yes
Estimated Speed Unknown Ind Yes
Vehicle Type Passenger Car
Vehicle Travel From Roadway
Vehicle Travel Distance Ft 80
Protections Installed Ind Yes
Protection Barricades Ind Yes
Preparer Name S****** M********
Preparer Title Compliance Program Leader
Preparer Email S****************@b**********.com
Preparer Telephone 2709035764
Prepared Date 2024-12-11 00:00:00
Authorizer Name T*** B****
Authorizer Telephone 2703146546
Authorizer Title Manager Compliance Services
Authorizer Email T*********@b**********.com
Narrative On 11/27/2024 at approximately 02:30, boardwalk louisiana midstream's (blm) control center received scada alarms at ashland road rsd site for high lel and low pressure on the downstream transmitter; operations personnel were dispatched to investigate. When operations personnel arrived, first responders were onsite responding to a vehicle accident in which the vehicle struck the valve site and caused the ethylene leak. Operations personnel discovered ethylene venting into the air with the wind blowing ethylene across ashland road. Operations personnel requested the control center close the upstream main line valve. Once inside the fenced area, operations personnel determined that tubing was damaged by the vehicle and they were able to isolate a 1/2-inch ball valve going to the tubing. Once the ball valve was closed, the ethylene leak stopped within approximately 2 minutes. At approximately 04:45, the site was deemed safe to reopen the mainline valve and control center personnel did so. Operations personnel repaired the damaged tubing and adjusted the pressure transmitter and the facility was returned to service.

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