HL incident on 2024-11-13 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,000
Incident datetime
2024-11-13 00:00 UTC
Report number
Location
OK
Narrative
During routine inspection the pump seal on the fast loop system was found to be leaking. Approximately 2 bbls (84 gallons) of diesel was released. About 42 gallons was released into concrete containment at the pump dike area with the remainder 42 being released to the ground. Local operator shut off the pump using the hoa switch and proceeded to close the inlet and outlet of the pump to isolate. It was determined the failure was due misalignment on the carrier bearing which caused the magnetic pump coupling to rub on the pump can causing a crack to occur in the can and allowing the release. The pump was replaced with a c- face motor to remove the carrier bearing. Temp and vibration monitoring was added to the magnetic coupling and additional pipe supports were added to the suction and discharge piping. Contaminated soil was removed and put in roll off boxes
Detailed record list
Report Received Date
2024-11-13 00:00:00
Iyear
2024
Report Number
20240265
Supplemental Number
40753
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
2
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Pump Was Blocked In And Isolated
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
East Houston
Segment Name
Fac Id 357
Onshore State Abbreviation
Tx
Onshore Postal Code
77029
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Pump Type
Positive Displacement
Pump Service Type
Other
Pump Service Type Details
Fast Loop Closed Sampling System
Installation Year
2024
Manufactured Year
2024
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
261
Est Cost Prop Damage
2000
Est Cost Emergency
4076
Est Cost Environmental
0
Est Cost Other
0
Prpty
6337
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
91
Mop Psig
500
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2019-04-30 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Ief Addl Misalignment Ind
Yes
Eqf Pump Equipment Ind
Yes
Preparer Name
G*** C*********
Preparer Email
G**************@o****.com
Preparer Telephone
9183818066
Prepared Date
2025-04-14 00:00:00
Local Contact Name
R*** M****
Local Contact Email
R*********@o****.com
Local Contact Telephone
5807410185
Authorizer Name
R*** M****
Authorizer Telephone
5807410185
Authorizer Email
R*********@o****.com
Narrative
During routine inspection the pump seal on the fast loop system was found to be leaking. Approximately 2 bbls (84 gallons) of diesel was released. About 42 gallons was released into concrete containment at the pump dike area with the remainder 42 being released to the ground. Local operator shut off the pump using the hoa switch and proceeded to close the inlet and outlet of the pump to isolate. It was determined the failure was due misalignment on the carrier bearing which caused the magnetic pump coupling to rub on the pump can causing a crack to occur in the can and allowing the release. The pump was replaced with a c- face motor to remove the carrier bearing. Temp and vibration monitoring was added to the magnetic coupling and additional pipe supports were added to the suction and discharge piping. Contaminated soil was removed and put in roll off boxes
Report Received Date 2024-11-13 00:00:00
Iyear 2024
Report Number 20240265
Supplemental Number 40753
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Time Zone Central
Daylight Savings Ind No
Location Latitude 29.794507 Google Maps OpenStreetMap
Location Longitude -95.280996 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 2
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Pump Was Blocked In And Isolated
Communication State Fed Ind No
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name East Houston
Segment Name Fac Id 357
Onshore State Abbreviation Tx
Onshore Postal Code 77029
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Pump Type Positive Displacement
Pump Service Type Other
Pump Service Type Details Fast Loop Closed Sampling System
Installation Year 2024
Manufactured Year 2024
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 261
Est Cost Prop Damage 2000
Est Cost Emergency 4076
Est Cost Environmental 0
Est Cost Other 0
Prpty 6337
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 91
Mop Psig 500
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2019-04-30 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Ief Addl Misalignment Ind Yes
Eqf Pump Equipment Ind Yes
Preparer Name G*** C*********
Preparer Email G**************@o****.com
Preparer Telephone 9183818066
Prepared Date 2025-04-14 00:00:00
Local Contact Name R*** M****
Local Contact Email R*********@o****.com
Local Contact Telephone 5807410185
Authorizer Name R*** M****
Authorizer Telephone 5807410185
Authorizer Email R*********@o****.com
Narrative During routine inspection the pump seal on the fast loop system was found to be leaking. Approximately 2 bbls (84 gallons) of diesel was released. About 42 gallons was released into concrete containment at the pump dike area with the remainder 42 being released to the ground. Local operator shut off the pump using the hoa switch and proceeded to close the inlet and outlet of the pump to isolate. It was determined the failure was due misalignment on the carrier bearing which caused the magnetic pump coupling to rub on the pump can causing a crack to occur in the can and allowing the release. The pump was replaced with a c- face motor to remove the carrier bearing. Temp and vibration monitoring was added to the magnetic coupling and additional pipe supports were added to the suction and discharge piping. Contaminated soil was removed and put in roll off boxes

All rights reserved. Copyright © by ClearPHMSA