Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2024-10-17 — TX
Operator
Enterprise Products Operating Llc
Cause
Other Accident Cause
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$100,000
Incident datetime
2024-10-17 00:00 UTC
Report number
Location
TX
Narrative
On 9/25/2024 at 10:34 edst operations at lebanon terminal discovered product on the ground near above ground storage tank 3361. An estimated 70 barrels of transmix were released. The tank has been isolated. All product released remained inside containment and no environmental impact occurred. Investigation is ongoing. Nrc: #1411860 at 12:10 edst on 9/25/2024 48hr nrc: #1412039 at 9:33 edst on 9/27/2024
Detailed record list
Report Received Date
2024-10-17 00:00:00
Iyear
2024
Report Number
20240250
Supplemental Number
40122
Report Type
Original
Operator Id
31618
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
39.484664
Location Longitude
-84.222963
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
70
Recovered Bbls
70
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Still Shutdown Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
1411860
Additional Nrc Report Numbers
1412039
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
9/25/2024 13:00
Num Pub Evacuated
0
Pipe Fac Name
Lebanon Terminal
Segment Name
Tnk 3361
Onshore State Abbreviation
Oh
Onshore Postal Code
45036
Onshore City Name
Lebanon
Onshore County Name
Warren
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Other
Tank Vessel Details
Not Yet Known.
Tank Type
Atmospheric
Safe Fill Level
22.5
Safe Fill Level Exceeded Ind
No
Api Std Out Of Service Year
2015
Api Std In Service Year
2020
Installation Year
1958
Manufactured Year
1958
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Not Yet Known.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
100000
Est Cost Emergency
25000
Est Cost Environmental
80000
Est Cost Other
0
Prpty
205000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required)
Preparer Name
R*** T********
Preparer Email
R*********@e****.com
Preparer Telephone
7133814659
Prepared Date
2024-10-17 00:00:00
Authorizer Name
R*** T********
Authorizer Telephone
7133814659
Authorizer Email
R*********@e****.com
Narrative
On 9/25/2024 at 10:34 edst operations at lebanon terminal discovered product on the ground near above ground storage tank 3361. An estimated 70 barrels of transmix were released. The tank has been isolated. All product released remained inside containment and no environmental impact occurred. Investigation is ongoing. Nrc: #1411860 at 12:10 edst on 9/25/2024 48hr nrc: #1412039 at 9:33 edst on 9/27/2024
Report Received Date | 2024-10-17 00:00:00 |
---|---|
Iyear | 2024 |
Report Number | 20240250 |
Supplemental Number | 40122 |
Report Type | Original |
Operator Id | 31618 PHMSA Enforcement |
Name | Enterprise Products Operating Llc |
Operator Street Address | 1100 Louisiana Street |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Eastern |
Daylight Savings Ind | Yes |
Location Latitude | 39.484664 Google Maps OpenStreetMap |
Location Longitude | -84.222963 Google Maps OpenStreetMap |
Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
Commodity Subtype | Mixture Of Refined Products (Transmix Or Other Mixture) |
Unintentional Release Bbls | 70 |
Recovered Bbls | 70 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Still Shutdown Ind | Yes |
Communication State Fed Ind | No |
Nrc Rpt Num | 1411860 NRC Report How to search |
Additional Nrc Report Numbers | 1412039 |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | Yes |
Osro Arrived On Site Dt | 9/25/2024 13:00 |
Num Pub Evacuated | 0 |
Pipe Fac Name | Lebanon Terminal |
Segment Name | Tnk 3361 |
Onshore State Abbreviation | Oh |
Onshore Postal Code | 45036 |
Onshore City Name | Lebanon |
Onshore County Name | Warren |
Designated Location | Milepost |
Designated Name | 0 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Tank, Including Attached Appurtenances |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Tank/vessel |
Tank Vessel Subtype | Other |
Tank Vessel Details | Not Yet Known. |
Tank Type | Atmospheric |
Safe Fill Level | 22.5 |
Safe Fill Level Exceeded Ind | No |
Api Std Out Of Service Year | 2015 |
Api Std In Service Year | 2020 |
Installation Year | 1958 |
Manufactured Year | 1958 |
Material Involved | Carbon Steel |
Release Type | Other |
Release Type Details | Not Yet Known. |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | Yes |
Soil Remed Ind | Yes |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 0 |
Est Cost Prop Damage | 100000 |
Est Cost Emergency | 25000 |
Est Cost Environmental | 80000 |
Est Cost Other | 0 |
Prpty | 205000 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 1 |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | No |
Cpm In Place Ind | No |
Investigation Status | No, the facility was not monitored by a controller(s) at the time of the accident |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Other Accident Cause |
Cause Details | Unknown |
Other Type | Unknown |
Unknown Subtype | Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required) |
Preparer Name | R*** T******** |
Preparer Email | R*********@e****.com |
Preparer Telephone | 7133814659 |
Prepared Date | 2024-10-17 00:00:00 |
Authorizer Name | R*** T******** |
Authorizer Telephone | 7133814659 |
Authorizer Email | R*********@e****.com |
Narrative | On 9/25/2024 at 10:34 edst operations at lebanon terminal discovered product on the ground near above ground storage tank 3361. An estimated 70 barrels of transmix were released. The tank has been isolated. All product released remained inside containment and no environmental impact occurred. Investigation is ongoing. Nrc: #1411860 at 12:10 edst on 9/25/2024 48hr nrc: #1412039 at 9:33 edst on 9/27/2024 |
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