HL incident on 2024-10-10 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$6,000
Incident datetime
2024-10-10 00:00 UTC
Report number
Location
TX
Narrative
On 9/11/2024 at 16:43 cdt enterprise pipeline control received a seal fail alarm for the interface detector pump on the tw products/seminole red pipeline at gaines station. Approximately 2 barrels of natural gasoline leaked from the interface detector pump. Pipeline control immediately shut off the pump, and on-site personnel isolated and repaired the pump and returned the interface detector to service.
Detailed record list
Report Received Date
2024-10-10 00:00:00
Iyear
2024
Report Number
20240239
Supplemental Number
40291
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
C5-Natural Gasoline
Unintentional Release Bbls
2
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Interface Detection Pump Was Isolated From The Pipeline.
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Upstream Oprtnl Cntrl Detail
Isolation Of Interface Detection Pump On Which Seal Failure Occurred.see 23a.
Downstream Oprtnl Cntrl Detail
See 23a.
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Tw Products/seminole Red Pipeline Gaines Station
Segment Name
Lid 50
Onshore State Abbreviation
Tx
Onshore Postal Code
79360
Onshore City Name
Seminole
Onshore County Name
Gaines
Designated Location
Milepost
Designated Name
1
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Pump Type
Positive Displacement
Pump Service Type
Other
Pump Service Type Details
Sampling Pump For Optical Interface Detector
Installation Year
2023
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
80
Est Cost Prop Damage
6000
Est Cost Emergency
400
Est Cost Environmental
0
Est Cost Other
0
Prpty
6480
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
450
Mop Psig
1440
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
1992-10-16 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Neither controller nor control room contributed to the accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
No Other Known Factors At This Time
Preparer Name
T****** A* G********
Preparer Title
Senior Staff Pipeline Compliance Engineer
Preparer Email
T**********@e****.com
Preparer Telephone
713-381-6433
Prepared Date
2024-12-05 00:00:00
Local Contact Name
T****** A* G********
Local Contact Email
T**********@e****.com
Local Contact Telephone
713-381-6433
Authorizer Name
T****** A* G********
Authorizer Telephone
713-381-6433
Authorizer Title
Senior Staff Pipeline Compliance Engineer
Authorizer Email
T**********@e****.com
Narrative
On 9/11/2024 at 16:43 cdt enterprise pipeline control received a seal fail alarm for the interface detector pump on the tw products/seminole red pipeline at gaines station. Approximately 2 barrels of natural gasoline leaked from the interface detector pump. Pipeline control immediately shut off the pump, and on-site personnel isolated and repaired the pump and returned the interface detector to service.
Report Received Date 2024-10-10 00:00:00
Iyear 2024
Report Number 20240239
Supplemental Number 40291
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 32.7754488 Google Maps OpenStreetMap
Location Longitude -102.959693 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Other
Commodity Details C5-Natural Gasoline
Unintentional Release Bbls 2
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Interface Detection Pump Was Isolated From The Pipeline.
Communication State Fed Ind No
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Upstream Oprtnl Cntrl Detail Isolation Of Interface Detection Pump On Which Seal Failure Occurred.see 23a.
Downstream Oprtnl Cntrl Detail See 23a.
Notify Qualified Indiv Ind No
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Tw Products/seminole Red Pipeline Gaines Station
Segment Name Lid 50
Onshore State Abbreviation Tx
Onshore Postal Code 79360
Onshore City Name Seminole
Onshore County Name Gaines
Designated Location Milepost
Designated Name 1
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Pump Type Positive Displacement
Pump Service Type Other
Pump Service Type Details Sampling Pump For Optical Interface Detector
Installation Year 2023
Manufactured Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 80
Est Cost Prop Damage 6000
Est Cost Emergency 400
Est Cost Environmental 0
Est Cost Other 0
Prpty 6480
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 450
Mop Psig 1440
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 1992-10-16 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Neither controller nor control room contributed to the accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details No Other Known Factors At This Time
Preparer Name T****** A* G********
Preparer Title Senior Staff Pipeline Compliance Engineer
Preparer Email T**********@e****.com
Preparer Telephone 713-381-6433
Prepared Date 2024-12-05 00:00:00
Local Contact Name T****** A* G********
Local Contact Email T**********@e****.com
Local Contact Telephone 713-381-6433
Authorizer Name T****** A* G********
Authorizer Telephone 713-381-6433
Authorizer Title Senior Staff Pipeline Compliance Engineer
Authorizer Email T**********@e****.com
Narrative On 9/11/2024 at 16:43 cdt enterprise pipeline control received a seal fail alarm for the interface detector pump on the tw products/seminole red pipeline at gaines station. Approximately 2 barrels of natural gasoline leaked from the interface detector pump. Pipeline control immediately shut off the pump, and on-site personnel isolated and repaired the pump and returned the interface detector to service.

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