Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2024-10-09 — LA
Operator
Empire Midstream Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$190,026
Incident datetime
2024-10-09 00:00 UTC
Report number
Location
LA
Narrative
On 8/27/24 @ 1450 hours, empire was notified there was a sheen on the water near psn-11724. Immediately, the producer pumping into this pipeline was instructed to shut-in & remain shut-in until further notice. The line was isolated & depressurized. Our smt was notified & nrc report no. 1409176 was filed followed by 1409245, 140936. An aerial flight was flown at 1700 hours w updated coordinates. Dsv joanne morrison arrived @ location on 8/29/24 @1315 hrs. Source: a ssti f/ a disconnected flowline decommissioned in 2018 by mcmoran oil & gas who failed to install & torque blind flange according to procedure along w/ leaving the isolation valve for the ssti assembly in the open position. Repair plan was developed w/tony wright's involvement. Blind flange was removed, cleaned & new r-50 o-ring & teflon coated studs & nuts were installed & the isolation valve was placed in the closed position. A pressure test was performed during daylight hours on 9/1/24 along with an aerial flight of area. Pipeline was returned to service on 9/1/24 at 1930 hrs.
Detailed record list
Report Received Date
2024-10-09 00:00:00
Iyear
2024
Report Number
20240237
Supplemental Number
40108
Report Type
Supplemental Final
Operator Id
39069
Name
Empire Midstream Llc
Operator Street Address
601 Poydras Street Suite 1725
Operator City Name
New Orleans
Operator State Abbreviation
LA
Operator Postal Code
70130
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
28.102973
Location Longitude
-92.481779
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Sheen On Water
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
On Off Shore
Offshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
1409176
Additional Nrc Report Numbers
1409245, 140936
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Automatic
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
East Cameron Gathering Llc
Segment Name
11724
Off Water Depth
220
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Ocs Type
Ocs-Gulf Of Mexico
Off Ocs Area
Ec
Off Ocs Block
330
Off Area Accident Type
Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
2018
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Loose Blind Flange
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Ocean Seawater Ind
Yes
Amount Released
0.1
Rel Water Name
Gulf Of Mexico
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
150
Est Cost Prop Damage
190026
Est Cost Emergency
390817
Est Cost Environmental
0
Est Cost Other
451
Est Cost Other Details
Bsee Repair Plan Fee
Prpty
581444
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
250
Mop Psig
2140
Mop Cfr Section
Other
Mop Cfr Section Details
Pressure Lowered F/ 2920 Psi To 2140 Psi To Be In Line W/ Connecting Psn-4235
Maop Established Date
2015-02-26 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
38227
Internal Inspection Ind
No
Unsuitable Mainline Ind
Yes
Other Restrictions Ind
Yes
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Pipeline Not Configured To Handle Ili
Pipeline Function
=< 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Based on the liquid detection setting, the pressure decline was too low to detect.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Other
Other Non Threaded Details
Blind Flange Not Installed Properly In 2018.
Additional Installation Ind
Yes
Eqf Non Threaded Ind
Yes
Io Not Installed Properly Ind
Yes
Io Follow Procedure Ind
Yes
Preparer Name
M******* C* W***
Preparer Title
Compliance And Regulatory Manager
Preparer Email
M*******@e**************.com
Preparer Telephone
5048282564 X2
Preparer Fax
5048720194
Prepared Date
2024-10-15 00:00:00
Local Contact Name
M******* C* W***
Local Contact Email
M*******@e**************.com
Local Contact Telephone
5048282564 X2
Authorizer Name
L****** M W********* I**
Authorizer Telephone
5048282564 X5
Authorizer Title
Vice President - Operations
Authorizer Email
L**@e**************.com
Narrative
O**********@ 1450 hours, empire was notified there was a sheen on the water near psn-11724. Immediately, the producer pumping into this pipeline was instructed to shut-in & remain shut-in until further notice. The line was isolated & depressurized. Our smt was notified & nrc report no. 1409176 was filed followed by 1409245, 140936. An aerial flight was flown at 1700 hours w updated coordinates. Dsv joanne morrison arrived @ location on 8/29/24 @1315 hrs. Source: a ssti f/ a disconnected flowline decommissioned in 2018 by mcmoran oil & gas who failed to install & torque blind flange according to procedure along w/ leaving the isolation valve for the ssti assembly in the open position. Repair plan was developed w/tony wright's involvement. Blind flange was removed, cleaned & new r-50 o-ring & teflon coated studs & nuts were installed & the isolation valve was placed in the closed position. A pressure test was performed during daylight hours on 9/1/24 along with an aerial flight of area. ******************************************************.
Report Received Date | 2024-10-09 00:00:00 |
---|---|
Iyear | 2024 |
Report Number | 20240237 |
Supplemental Number | 40108 |
Report Type | Supplemental Final |
Operator Id | 39069 PHMSA Enforcement |
Name | Empire Midstream Llc |
Operator Street Address | 601 Poydras Street Suite 1725 |
Operator City Name | New Orleans |
Operator State Abbreviation | LA |
Operator Postal Code | 70130 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 28.102973 Google Maps OpenStreetMap |
Location Longitude | -92.481779 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 0.1 |
Recovered Bbls | 0 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Other |
Accident Details | Sheen On Water |
System Part Involved | Offshore Pipeline, Including Riser And Riser Bend |
On Off Shore | Offshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | 1409176 NRC Report How to search |
Additional Nrc Report Numbers | 1409245, 140936 |
Ignite Ind | No |
Upstream Action Taken | Valve Closure |
Upstream Valve Type Ind | Automatic |
Downstream Action Taken | Valve Closure |
Downstream Valve Type Ind | Automatic |
Num Pub Evacuated | 0 |
Pipe Fac Name | East Cameron Gathering Llc |
Segment Name | 11724 |
Off Water Depth | 220 |
Off Accident Origin | On The Outer Continental Shelf (Ocs) |
Ocs Type | Ocs-Gulf Of Mexico |
Off Ocs Area | Ec |
Off Ocs Block | 330 |
Off Area Accident Type | Below Water, Pipe Buried Or Jetted Below Seabed |
Pipe Facility Type | Interstate |
Item Involved | Flange Assembly |
Installation Year | 2018 |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Other |
Leak Type Other | Loose Blind Flange |
Wildlife Impact Ind | No |
Soil Contamination | No |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | Yes |
Ocean Seawater Ind | Yes |
Amount Released | 0.1 |
Rel Water Name | Gulf Of Mexico |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 150 |
Est Cost Prop Damage | 190026 |
Est Cost Emergency | 390817 |
Est Cost Environmental | 0 |
Est Cost Other | 451 |
Est Cost Other Details | Bsee Repair Plan Fee |
Prpty | 581444 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 250 |
Mop Psig | 2140 |
Mop Cfr Section | Other View CFR 49 §192 |
Mop Cfr Section Details | Pressure Lowered F/ 2920 Psi To 2140 Psi To Be In Line W/ Connecting Psn-4235 |
Maop Established Date | 2015-02-26 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Length Segment Isolated | 38227 |
Internal Inspection Ind | No |
Unsuitable Mainline Ind | Yes |
Other Restrictions Ind | Yes |
Operation Complications Ind | Yes |
Other Complications Ind | Yes |
Inspect Comp Details | Pipeline Not Configured To Handle Ili |
Pipeline Function | =< 20% Smys Regulated Gathering |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Based on the liquid detection setting, the pressure decline was too low to detect. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Equipment Failure |
Cause Details | Non-Threaded Connection Failure |
Eq Failure Type | Non-Threaded Connection Failure |
Other Non Threaded Ind | Other |
Other Non Threaded Details | Blind Flange Not Installed Properly In 2018. |
Additional Installation Ind | Yes |
Eqf Non Threaded Ind | Yes |
Io Not Installed Properly Ind | Yes |
Io Follow Procedure Ind | Yes |
Preparer Name | M******* C* W*** |
Preparer Title | Compliance And Regulatory Manager |
Preparer Email | M*******@e**************.com |
Preparer Telephone | 5048282564 X2 |
Preparer Fax | 5048720194 |
Prepared Date | 2024-10-15 00:00:00 |
Local Contact Name | M******* C* W*** |
Local Contact Email | M*******@e**************.com |
Local Contact Telephone | 5048282564 X2 |
Authorizer Name | L****** M W********* I** |
Authorizer Telephone | 5048282564 X5 |
Authorizer Title | Vice President - Operations |
Authorizer Email | L**@e**************.com |
Narrative | O**********@ 1450 hours, empire was notified there was a sheen on the water near psn-11724. Immediately, the producer pumping into this pipeline was instructed to shut-in & remain shut-in until further notice. The line was isolated & depressurized. Our smt was notified & nrc report no. 1409176 was filed followed by 1409245, 140936. An aerial flight was flown at 1700 hours w updated coordinates. Dsv joanne morrison arrived @ location on 8/29/24 @1315 hrs. Source: a ssti f/ a disconnected flowline decommissioned in 2018 by mcmoran oil & gas who failed to install & torque blind flange according to procedure along w/ leaving the isolation valve for the ssti assembly in the open position. Repair plan was developed w/tony wright's involvement. Blind flange was removed, cleaned & new r-50 o-ring & teflon coated studs & nuts were installed & the isolation valve was placed in the closed position. A pressure test was performed during daylight hours on 9/1/24 along with an aerial flight of area. ******************************************************. |
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