Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2024-09-25 — TX
Operator
Enbridge Holdings (Gray Oak) Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$14,182
Incident datetime
2024-09-25 00:00 UTC
Report number
Location
TX
Narrative
On august 26, 2024, at approximately 1:43 pm cdt, a local technician performing daily rounds of the crane terminal discovered a release of crude oil coming from the tank mixer on tank 402. The edmonton control center was contacted and the tank was isolated. The tertiary containment was used to prevent further release into the secondary containment. The area supervisor arrived on site and determined that the release exceeded 5 gallons at 2:45 pm cdt. The source of the release was identified as a failed outer mixer seal causing the release of oil. The torque on the internal mixer seal was adjusted to prevent any further release. The railroad commission of texas was notified of the release at 3:26 pm cdt (report # ici-3153). Operations personnel were dispatched to begin cleanup of product and remediation. Approximately 20 gallons of crude oil was released. All contaminated soil has been removed and properly disposed of at an approved site. An investigation determined the mixer seal failed due to the shaft on the mixer having damage due to a bearing failure. The mixer is currently locked out and will be repaired at a future date. The nrc was notified on september 25, 2024, at 1:42 pm cdt (report # 1411888) as costs are expected to exceed the $50,000 nrc reporting threshold. A 48-hour update to the nrc was made on september 27, 2024, at 12:31 pm cdt (report # 1412079).
Detailed record list
Report Received Date
2024-09-25 00:00:00
Iyear
2024
Report Number
20240228
Supplemental Number
40054
Report Type
Supplemental Final
Operator Id
40668
Name
Enbridge Holdings (Gray Oak) Llc
Operator Street Address
915 N Eldridge Pkwy, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
31.438415
Location Longitude
-102.379743
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.48
Recovered Bbls
0.48
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Mixer Was Isolated And Locked Out
Communication State Fed Ind
No
Nrc Rpt Num
1411888
Additional Nrc Report Numbers
1412079
Ignite Ind
No
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Crane Terminal
Segment Name
Tank 402
Onshore State Abbreviation
Tx
Onshore Postal Code
79731
Onshore City Name
Crane
Onshore County Name
Crane
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Mixer
Tank Type
Atmospheric
Safe Fill Level
53
Safe Fill Level Exceeded Ind
No
Api Std Out Of Srvc None Ind
Yes
Api Std In Service Year
2024
Installation Year
2019
Manufactured Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
38
Est Cost Prop Damage
14182
Est Cost Emergency
7000
Est Cost Environmental
41800
Est Cost Other
0
Prpty
63020
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
10
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Lack of control center involvement. Release was identified by field personnel.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Tank Mixer Seal
Additional Erosion Wear Ind
Yes
Preparer Name
S**** S****
Preparer Title
Advisor Regulatory Compliance
Preparer Email
S**********@e*******.com
Preparer Telephone
7153953620
Prepared Date
2024-09-30 00:00:00
Authorizer Name
L*** S**********
Authorizer Telephone
7153941584
Authorizer Title
Supervisor Regulatory Compliance
Authorizer Email
L***************@e*******.com
Narrative
On august 26, 2024, at approximately 1:43 pm cdt, a local technician performing daily rounds of the crane terminal discovered a release of crude oil coming from the tank mixer on tank 402. The edmonton control center was contacted and the tank was isolated. The tertiary containment was used to prevent further release into the secondary containment. The area supervisor arrived on site and determined that the release exceeded 5 gallons at 2:45 pm cdt. The source of the release was identified as a failed outer mixer seal causing the release of oil. The torque on the internal mixer seal was adjusted to prevent any further release. The railroad commission of texas was notified of the release at 3:26 pm cdt (report # ici-3153). Operations personnel were dispatched to begin cleanup of product and remediation. Approximately 20 gallons of crude oil was released. All contaminated soil has been removed and properly disposed of at an approved site. An investigation determined the mixer seal failed due to the shaft on the mixer having damage due to a bearing failure. The mixer is currently locked out and will be repaired at a future date. The nrc was notified on september 25, 2024, at 1:42 pm cdt (report # 1411888) as costs are expected to exceed the $50,000 nrc reporting threshold. A 48-hour update to the nrc was made on september 27, 2024, at 12:31 pm cdt (report # 1412079).
Report Received Date | 2024-09-25 00:00:00 |
---|---|
Iyear | 2024 |
Report Number | 20240228 |
Supplemental Number | 40054 |
Report Type | Supplemental Final |
Operator Id | 40668 PHMSA Enforcement |
Name | Enbridge Holdings (Gray Oak) Llc |
Operator Street Address | 915 N Eldridge Pkwy, Suite 1100 |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77079 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 31.438415 Google Maps OpenStreetMap |
Location Longitude | -102.379743 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 0.48 |
Recovered Bbls | 0.48 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | No |
Shutdown Explain | Tank Mixer Was Isolated And Locked Out |
Communication State Fed Ind | No |
Nrc Rpt Num | 1411888 NRC Report How to search |
Additional Nrc Report Numbers | 1412079 |
Ignite Ind | No |
Notify Qualified Indiv Ind | No |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Crane Terminal |
Segment Name | Tank 402 |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 79731 |
Onshore City Name | Crane |
Onshore County Name | Crane |
Designated Location | Milepost |
Designated Name | 0 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Tank, Including Attached Appurtenances |
Crossing | No |
Pipe Facility Type | Intrastate |
Item Involved | Tank/vessel |
Tank Vessel Subtype | Mixer |
Tank Type | Atmospheric |
Safe Fill Level | 53 |
Safe Fill Level Exceeded Ind | No |
Api Std Out Of Srvc None Ind | Yes |
Api Std In Service Year | 2024 |
Installation Year | 2019 |
Manufactured Year | 2019 |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Seal Or Packing |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 38 |
Est Cost Prop Damage | 14182 |
Est Cost Emergency | 7000 |
Est Cost Environmental | 41800 |
Est Cost Other | 0 |
Prpty | 63020 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 10 |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Lack of control center involvement. Release was identified by field personnel. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Equipment Failure |
Cause Details | Other Equipment Failure |
Eq Failure Type | Other Equipment Failure |
Failure Details | Tank Mixer Seal |
Additional Erosion Wear Ind | Yes |
Preparer Name | S**** S**** |
Preparer Title | Advisor Regulatory Compliance |
Preparer Email | S**********@e*******.com |
Preparer Telephone | 7153953620 |
Prepared Date | 2024-09-30 00:00:00 |
Authorizer Name | L*** S********** |
Authorizer Telephone | 7153941584 |
Authorizer Title | Supervisor Regulatory Compliance |
Authorizer Email | L***************@e*******.com |
Narrative | On august 26, 2024, at approximately 1:43 pm cdt, a local technician performing daily rounds of the crane terminal discovered a release of crude oil coming from the tank mixer on tank 402. The edmonton control center was contacted and the tank was isolated. The tertiary containment was used to prevent further release into the secondary containment. The area supervisor arrived on site and determined that the release exceeded 5 gallons at 2:45 pm cdt. The source of the release was identified as a failed outer mixer seal causing the release of oil. The torque on the internal mixer seal was adjusted to prevent any further release. The railroad commission of texas was notified of the release at 3:26 pm cdt (report # ici-3153). Operations personnel were dispatched to begin cleanup of product and remediation. Approximately 20 gallons of crude oil was released. All contaminated soil has been removed and properly disposed of at an approved site. An investigation determined the mixer seal failed due to the shaft on the mixer having damage due to a bearing failure. The mixer is currently locked out and will be repaired at a future date. The nrc was notified on september 25, 2024, at 1:42 pm cdt (report # 1411888) as costs are expected to exceed the $50,000 nrc reporting threshold. A 48-hour update to the nrc was made on september 27, 2024, at 12:31 pm cdt (report # 1412079). |
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