HL incident on 2024-09-24 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$120,000
Incident datetime
2024-09-24 00:00 UTC
Report number
Location
TX
Narrative
On august 27, 2024 at 11:42 am cst, row patrol discovered an area of dead vegetation south of tulia station on the south leg loop. Approximately .01 barrels of natural gasoline leaked from a buried stopple. Operations replaced the buried stopple with new pipe. Nrc reportable on costs of pipe replacement only.
Detailed record list
Report Received Date
2024-09-24 00:00:00
Iyear
2024
Report Number
20240223
Supplemental Number
40494
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.1
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Line Pressure Was Reduced And Isolated
Communication State Fed Ind
No
Nrc Rpt Num
Additional Nrc Report Numbers
1409476
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
South Leg Loop
Segment Name
Lid 220
Onshore State Abbreviation
Tx
Onshore Postal Code
79088
Onshore City Name
Tulia
Onshore County Name
Swisher
Designated Location
Milepost
Designated Name
Mp 146
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
Unknown
Manufactured Year
1970
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
120000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
120020
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
411
Mop Psig
1198
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
1969-09-30 00:00:00
Maop Reversal Flow Ind
Bi-Directional
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
72336
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller was not involved in the release
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Eq Additional Other Ind
Yes
Eq Additional Other Details
O-Ring Failure
Preparer Name
A***** A******** I*
Preparer Title
Pipeline Compliance Engineer
Preparer Email
A***********@e****.com
Preparer Telephone
713-381-3659
Prepared Date
2025-02-11 00:00:00
Authorizer Name
A***** A******** I*
Authorizer Telephone
713-381-3659
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
A***********@e****.com
Narrative
On august 27, 2024 at 11:42 am cst, row patrol discovered an area of dead vegetation south of tulia station on the south leg loop. Approximately .01 barrels of natural gasoline leaked from a buried stopple. Operations replaced the buried stopple with new pipe. Nrc reportable on costs of pipe replacement only.
Report Received Date 2024-09-24 00:00:00
Iyear 2024
Report Number 20240223
Supplemental Number 40494
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind No
Location Latitude 34.574346 Google Maps OpenStreetMap
Location Longitude -101.789158 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.1
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Line Pressure Was Reduced And Isolated
Communication State Fed Ind No
Nrc Rpt Num 1409305 NRC Report How to search
Additional Nrc Report Numbers 1409476
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name South Leg Loop
Segment Name Lid 220
Onshore State Abbreviation Tx
Onshore Postal Code 79088
Onshore City Name Tulia
Onshore County Name Swisher
Designated Location Milepost
Designated Name Mp 146
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year Unknown
Manufactured Year 1970
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 120000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 120020
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 411
Mop Psig 1198
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 1969-09-30 00:00:00
Maop Reversal Flow Ind Bi-Directional
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 72336
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller was not involved in the release
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Eq Additional Other Ind Yes
Eq Additional Other Details O-Ring Failure
Preparer Name A***** A******** I*
Preparer Title Pipeline Compliance Engineer
Preparer Email A***********@e****.com
Preparer Telephone 713-381-3659
Prepared Date 2025-02-11 00:00:00
Authorizer Name A***** A******** I*
Authorizer Telephone 713-381-3659
Authorizer Title Pipeline Compliance Engineer
Authorizer Email A***********@e****.com
Narrative On august 27, 2024 at 11:42 am cst, row patrol discovered an area of dead vegetation south of tulia station on the south leg loop. Approximately .01 barrels of natural gasoline leaked from a buried stopple. Operations replaced the buried stopple with new pipe. Nrc reportable on costs of pipe replacement only.

All rights reserved. Copyright © by ClearPHMSA