Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2024-09-11 — TX
Operator
Centurion Pipeline L.p.
Cause
Natural Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$100
Incident datetime
2024-09-11 00:00 UTC
Report number
Location
TX
Narrative
On 8/11/24 at 23:30, a leak was discovered in the mainline pump strainer area of the el reno to cushing system #2 line at el reno station. The area was isolated and the line shutdown. The investigation determined the leak was coming from a threaded 1/2-inch pvit fitting. Approximately 5 barrels of crude oil was released to the ground. Released product was cleaned up and impacted soil remediated. Failed fitting was replaced and line restarted. The cause of the leak is still under investigation. A supplemental report will be submitted once the investigation is complete. Supplemental report filed on november 15, 2024: during the accident investigation, it was determined that sudden heavy rainfall cause increased settling of the soil in the area of the fitting. Prior to the leak, the ground had previously been excavated and backfilled. Weather conditions were in drought prior to the rainfall. With the age of the fitting and the sudden rainfall causing settling, the fitting leaked. The threaded fitting was replaced with a single stainless steel line to prevent future reoccurrence. The single stainless steel line will prevent multiple connection points that could serve as potential leak points.
Detailed record list
Report Received Date
2024-09-11 00:00:00
Iyear
2024
Report Number
20240216
Supplemental Number
40223
Report Type
Supplemental Final
Operator Id
31888
Name
Centurion Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
35.511293
Location Longitude
-97.884654
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Recovered Bbls
5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
El Reno Station
Segment Name
El Reno To Cushing System #2 16-Inch
Onshore State Abbreviation
Ok
Onshore Postal Code
73036
Onshore City Name
El Reno
Onshore County Name
Canadian
Designated Location
Milepost
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
28
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Tubing Material
Stainless Steel
Tubing Type
Rigid
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
100
Est Cost Emergency
20000
Est Cost Environmental
20000
Est Cost Other
0
Prpty
40100
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
258
Mop Psig
740
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2016-11-10 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Heavy Rains/floods
Natural Force Type
Heavy Rains/floods
Heavy Rains Subtype
Other
Nf Other Details
Increased Earth Settling From Extreme Dry Weather To Sudden Rainfall.
Nf Extreme Weather Ind
No
Preparer Name
T*** N*******
Preparer Title
Director - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2024-11-14 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 8/11/24 at 23:30, a leak was discovered in the mainline pump strainer area of the el reno to cushing system #2 line at el reno station. The area was isolated and the line shutdown. The investigation determined the leak was coming from a threaded 1/2-inch pvit fitting. Approximately 5 barrels of crude oil was released to the ground. Released product was cleaned up and impacted soil remediated. Failed fitting was replaced and line restarted. The cause of the leak is still under investigation. A supplemental report will be submitted once the investigation is complete. Supplemental report filed on november 15, 2024: during the accident investigation, it was determined that sudden heavy rainfall cause increased settling of the soil in the area of the fitting. Prior to the leak, the ground had previously been excavated and backfilled. Weather conditions were in drought prior to the rainfall. With the age of the fitting and the sudden rainfall causing settling, the fitting leaked. The threaded fitting was replaced with a single stainless steel line to prevent future reoccurrence. The single stainless steel line will prevent multiple connection points that could serve as potential leak points.
Report Received Date | 2024-09-11 00:00:00 |
---|---|
Iyear | 2024 |
Report Number | 20240216 |
Supplemental Number | 40223 |
Report Type | Supplemental Final |
Operator Id | 31888 PHMSA Enforcement |
Name | Centurion Pipeline L.p. |
Operator Street Address | 1300 Main Street |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 35.511293 Google Maps OpenStreetMap |
Location Longitude | -97.884654 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 5 |
Recovered Bbls | 5 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Pump/meter Station Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | No |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | El Reno Station |
Segment Name | El Reno To Cushing System #2 16-Inch |
Onshore State Abbreviation | Ok |
Onshore Postal Code | 73036 |
Onshore City Name | El Reno |
Onshore County Name | Canadian |
Designated Location | Milepost |
Designated Name | 0+00 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Underground |
Incident Area Subtype | Under Soil |
Depth Of Cover | 28 |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Tubing |
Tubing Material | Stainless Steel |
Tubing Type | Rigid |
Installation Year | Unknown |
Manufactured Year | Unknown |
Material Involved | Material Other Than Carbon Steel |
Material Details | Stainless Steel |
Release Type | Leak |
Leak Type | Crack |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | Yes |
Soil Remed Ind | Yes |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | Yes |
Other Pop Ind | Yes |
Other Pop Yes No | Yes |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 0 |
Est Cost Prop Damage | 100 |
Est Cost Emergency | 20000 |
Est Cost Environmental | 20000 |
Est Cost Other | 0 |
Prpty | 40100 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 258 |
Mop Psig | 740 |
Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
Maop Established Date | 2016-11-10 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | A review of the accident determined that there were no control room actions that contributed to the event. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Natural Force Damage |
Cause Details | Heavy Rains/floods |
Natural Force Type | Heavy Rains/floods |
Heavy Rains Subtype | Other |
Nf Other Details | Increased Earth Settling From Extreme Dry Weather To Sudden Rainfall. |
Nf Extreme Weather Ind | No |
Preparer Name | T*** N******* |
Preparer Title | Director - Dot Compliance |
Preparer Email | T************@e*************.com |
Preparer Telephone | 713-989-7126 |
Prepared Date | 2024-11-14 00:00:00 |
Authorizer Name | T*** N******* |
Authorizer Telephone | 713-989-7126 |
Authorizer Title | Director - Dot Compliance |
Authorizer Email | T************@e*************.com |
Narrative | On 8/11/24 at 23:30, a leak was discovered in the mainline pump strainer area of the el reno to cushing system #2 line at el reno station. The area was isolated and the line shutdown. The investigation determined the leak was coming from a threaded 1/2-inch pvit fitting. Approximately 5 barrels of crude oil was released to the ground. Released product was cleaned up and impacted soil remediated. Failed fitting was replaced and line restarted. The cause of the leak is still under investigation. A supplemental report will be submitted once the investigation is complete. Supplemental report filed on november 15, 2024: during the accident investigation, it was determined that sudden heavy rainfall cause increased settling of the soil in the area of the fitting. Prior to the leak, the ground had previously been excavated and backfilled. Weather conditions were in drought prior to the rainfall. With the age of the fitting and the sudden rainfall causing settling, the fitting leaked. The threaded fitting was replaced with a single stainless steel line to prevent future reoccurrence. The single stainless steel line will prevent multiple connection points that could serve as potential leak points. |
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