HL incident on 2024-09-05 — TX

Operator
Sunoco Pipeline L.p.
Cause
Other Accident Cause
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,750,000
Incident datetime
2024-09-05 00:00 UTC
Report number
Location
TX
Narrative
On 8/9/24 at 07:45, bubbling around chime of tank 327 was observed during rounds at marcus hook tank farm. Approximately 1,342 bbls of gasoline was released into containment. Remaining product from tank 327 was transferred to an adjacent tank. Free product was recovered from tank dike area. Tank manways removed. The cause of the accident is still under investigation. A supplemental report will be submitted once the investigation is completed.
Detailed record list
Report Received Date
2024-09-05 00:00:00
Iyear
2024
Report Number
20240213
Supplemental Number
39973
Report Type
Original
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
1342
Recovered Bbls
1342
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Still Shutdown Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1407549
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
8/9/2024 8:35
Num Pub Evacuated
0
Pipe Fac Name
Marcus Hook Tank Farm
Segment Name
Tank 327
Onshore State Abbreviation
Pa
Onshore Postal Code
19014
Onshore City Name
Aston
Onshore County Name
Delaware
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Chime
Tank Type
Atmospheric
Safe Fill Level
48
Safe Fill Level Exceeded Ind
No
Api Std Out Of Service Year
2016
Api Std In Service Year
2021
Installation Year
1951
Manufactured Year
1951
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Under Investigation
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
0.2
Rel Water Name
Mw35
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
18900
Est Cost Prop Damage
2750000
Est Cost Emergency
250000
Est Cost Environmental
75000
Est Cost Other
0
Prpty
3093900
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
14.7
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required)
Preparer Name
T*** N*******
Preparer Title
Director - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2024-09-05 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 8/9/24 at 07:45, bubbling around chime of tank 327 was observed during rounds at marcus hook tank farm. Approximately 1,342 bbls of gasoline was released into containment. Remaining product from tank 327 was transferred to an adjacent tank. Free product was recovered from tank dike area. Tank manways removed. The cause of the accident is still under investigation. A supplemental report will be submitted once the investigation is completed.
Report Received Date 2024-09-05 00:00:00
Iyear 2024
Report Number 20240213
Supplemental Number 39973
Report Type Original
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Eastern
Daylight Savings Ind Yes
Location Latitude 39.851131 Google Maps OpenStreetMap
Location Longitude -75.41527 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 1342
Recovered Bbls 1342
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Still Shutdown Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1407384 NRC Report How to search
Additional Nrc Report Numbers 1407549
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind Yes
Osro Arrived On Site Dt 8/9/2024 8:35
Num Pub Evacuated 0
Pipe Fac Name Marcus Hook Tank Farm
Segment Name Tank 327
Onshore State Abbreviation Pa
Onshore Postal Code 19014
Onshore City Name Aston
Onshore County Name Delaware
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Chime
Tank Type Atmospheric
Safe Fill Level 48
Safe Fill Level Exceeded Ind No
Api Std Out Of Service Year 2016
Api Std In Service Year 2021
Installation Year 1951
Manufactured Year 1951
Material Involved Carbon Steel
Release Type Other
Release Type Details Under Investigation
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 0.2
Rel Water Name Mw35
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 18900
Est Cost Prop Damage 2750000
Est Cost Emergency 250000
Est Cost Environmental 75000
Est Cost Other 0
Prpty 3093900
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 14.7
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Still Under Investigation, Cause Of Accident To Be Determined* (*supplemental Report Required)
Preparer Name T*** N*******
Preparer Title Director - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Prepared Date 2024-09-05 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Director - Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 8/9/24 at 07:45, bubbling around chime of tank 327 was observed during rounds at marcus hook tank farm. Approximately 1,342 bbls of gasoline was released into containment. Remaining product from tank 327 was transferred to an adjacent tank. Free product was recovered from tank dike area. Tank manways removed. The cause of the accident is still under investigation. A supplemental report will be submitted once the investigation is completed.

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