HL incident on 2024-09-04 — TX

Operator
Enterprise Products Operating Llc
Cause
Incorrect Operation
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$150,000
Incident datetime
2024-09-04 00:00 UTC
Report number
Location
TX
Narrative
On august 7, 2024 at 13:57 cst, during routine pipeline repairs on the west red line near mile post 36.5, a burn-thru occurred resulting in a leak. After investigation, it was discovered the welder did not properly follow company standards and the inspector failed to provide oversight to ensure protocol was followed. Oq's were suspended immediately for the welder and inspector performing the work. The damaged pipe was cut out and replaced. Pipe replacement costs exceeded $50,000 which required an nrc notification.
Detailed record list
Report Received Date
2024-09-04 00:00:00
Iyear
2024
Report Number
20240211
Supplemental Number
41076
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propane
Unintentional Release Bbls
6.1
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Additional Nrc Report Numbers
1407383
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
West Leg Loop 8"
Segment Name
Lid 428
Onshore State Abbreviation
Ks
Onshore Postal Code
67401
Onshore City Name
Greeley
Onshore County Name
Saline
Designated Location
Milepost
Designated Name
36.5
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
Unknown
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
8
Pipe Wall Thickness
0.156
Pipe Smys
52000
Pipe Specification
Api-5l
Pipe Seam Type
Seamless
Pipe Manufacturer
U.s. Steel
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Coating Applied Ind
Unknown
Installation Year
1969
Manufactured Year
1969
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Burn Through
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
210
Est Cost Prop Damage
150000
Est Cost Emergency
50
Est Cost Environmental
0
Est Cost Other
0
Prpty
150260
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
469
Mop Psig
1345
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
1969-09-18 00:00:00
Maop Reversal Flow Ind
Bi-Directional
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
47520
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak caused by contractor on rehab
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
A***** A******** I*
Preparer Title
Pipeline Compliance Engineer
Preparer Email
A***********@e****.com
Preparer Telephone
713-381-3659
Prepared Date
2025-06-25 00:00:00
Authorizer Name
A***** A******** I*
Authorizer Telephone
713-381-3659
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
A***********@e****.com
Narrative
On august 7, 2024 at 13:57 cst, during routine pipeline repairs on the west red line near mile post 36.5, a burn-thru occurred resulting in a leak. After investigation, it was discovered the welder did not properly follow company standards and the inspector failed to provide oversight to ensure protocol was followed. Oq's were suspended immediately for the welder and inspector performing the work. The damaged pipe was cut out and replaced. Pipe replacement costs exceeded $50,000 which required an nrc notification.
Report Received Date 2024-09-04 00:00:00
Iyear 2024
Report Number 20240211
Supplemental Number 41076
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 38.8185016 Google Maps OpenStreetMap
Location Longitude -97.4912931 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propane
Unintentional Release Bbls 6.1
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num 1407214 NRC Report How to search
Additional Nrc Report Numbers 1407383
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Manual
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name West Leg Loop 8"
Segment Name Lid 428
Onshore State Abbreviation Ks
Onshore Postal Code 67401
Onshore City Name Greeley
Onshore County Name Saline
Designated Location Milepost
Designated Name 36.5
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover Unknown
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 8
Pipe Wall Thickness 0.156
Pipe Smys 52000
Pipe Specification Api-5l
Pipe Seam Type Seamless
Pipe Manufacturer U.s. Steel
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Coating Applied Ind Unknown
Installation Year 1969
Manufactured Year 1969
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Burn Through
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 210
Est Cost Prop Damage 150000
Est Cost Emergency 50
Est Cost Environmental 0
Est Cost Other 0
Prpty 150260
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 469
Mop Psig 1345
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 1969-09-18 00:00:00
Maop Reversal Flow Ind Bi-Directional
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 47520
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak caused by contractor on rehab
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 1
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name A***** A******** I*
Preparer Title Pipeline Compliance Engineer
Preparer Email A***********@e****.com
Preparer Telephone 713-381-3659
Prepared Date 2025-06-25 00:00:00
Authorizer Name A***** A******** I*
Authorizer Telephone 713-381-3659
Authorizer Title Pipeline Compliance Engineer
Authorizer Email A***********@e****.com
Narrative On august 7, 2024 at 13:57 cst, during routine pipeline repairs on the west red line near mile post 36.5, a burn-thru occurred resulting in a leak. After investigation, it was discovered the welder did not properly follow company standards and the inspector failed to provide oversight to ensure protocol was followed. Oq's were suspended immediately for the welder and inspector performing the work. The damaged pipe was cut out and replaced. Pipe replacement costs exceeded $50,000 which required an nrc notification.

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