HL incident on 2024-09-03 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$120,000
Incident datetime
2024-09-03 00:00 UTC
Report number
Location
TX
Narrative
On august 5th, 2024, at approximately 10:55 cdst, enterprise employees removed tank 1022 vertical booster pump for maintenance. Employees then observed product re-entering the evacuated can from a one-inch threaded plug on bottom of the pump. Upon investigation it appeared that the original sealant applied to the plug during install had degraded. For repair the failed plug was replaced with a solid steel core plug with approved thread sealant. Approximately 4 gallons were released and have been cleaned up. Nrc: #1406987 at 16:00 on 8/5/2024 48hr nrc: #1407177 at 10:32 on 8/7/2024
Detailed record list
Report Received Date
2024-09-03 00:00:00
Iyear
2024
Report Number
20240209
Supplemental Number
40082
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.1
Recovered Bbls
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Asset Was Already Shut Down For Maintenance.
Communication State Fed Ind
No
Nrc Rpt Num
Additional Nrc Report Numbers
1407177
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
8/5/2024 10:55
Num Pub Evacuated
0
Pipe Fac Name
El Dorado Terminal
Segment Name
Arxx0266
Onshore State Abbreviation
Ar
Onshore Postal Code
71730
Onshore City Name
El Dorado
Onshore County Name
Union
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
131
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Pump Type
Centrifugal
Pump Service Type
Other
Pump Service Type Details
Internal Booster
Installation Year
1951
Manufactured Year
1951
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
120000
Est Cost Emergency
45000
Est Cost Environmental
5000
Est Cost Other
0
Prpty
170020
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
0
Mop Psig
125
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
1951-01-01 00:00:00
Maop Reversal Flow Ind
Bi-Directional
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller did not contribute to the accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Other
Other Stripped Details
Threaded Plug
Eq Additional Other Ind
Yes
Eq Additional Other Details
Sealant Had Degraded.
Preparer Name
R*** T********
Preparer Title
Pipeline Compliance Senior Engineer
Preparer Email
R*********@e****.com
Preparer Telephone
713-381-4659
Prepared Date
2024-10-09 00:00:00
Authorizer Name
R*** T********
Authorizer Telephone
713-381-4659
Authorizer Title
Pipeline Compliance Senior Engineer
Authorizer Email
R*********@e****.com
Narrative
On august 5th, 2024, at approximately 10:55 cdst, enterprise employees removed tank 1022 vertical booster pump for maintenance. Employees then observed product re-entering the evacuated can from a one-inch threaded plug on bottom of the pump. Upon investigation it appeared that the original sealant applied to the plug during install had degraded. For repair the failed plug was replaced with a solid steel core plug with approved thread sealant. Approximately 4 gallons were released and have been cleaned up. Nrc: #1406987 at 16:00 on 8/5/2024 48hr nrc: #1407177 at 10:32 on 8/7/2024
Report Received Date 2024-09-03 00:00:00
Iyear 2024
Report Number 20240209
Supplemental Number 40082
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 33.26101 Google Maps OpenStreetMap
Location Longitude -92.62769 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.1
Recovered Bbls 0.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Asset Was Already Shut Down For Maintenance.
Communication State Fed Ind No
Nrc Rpt Num 1406987 NRC Report How to search
Additional Nrc Report Numbers 1407177
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind Yes
Osro Arrived On Site Dt 8/5/2024 10:55
Num Pub Evacuated 0
Pipe Fac Name El Dorado Terminal
Segment Name Arxx0266
Onshore State Abbreviation Ar
Onshore Postal Code 71730
Onshore City Name El Dorado
Onshore County Name Union
Designated Location Milepost
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 131
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Pump Type Centrifugal
Pump Service Type Other
Pump Service Type Details Internal Booster
Installation Year 1951
Manufactured Year 1951
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 120000
Est Cost Emergency 45000
Est Cost Environmental 5000
Est Cost Other 0
Prpty 170020
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 0
Mop Psig 125
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 1951-01-01 00:00:00
Maop Reversal Flow Ind Bi-Directional
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller did not contribute to the accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Other
Other Stripped Details Threaded Plug
Eq Additional Other Ind Yes
Eq Additional Other Details Sealant Had Degraded.
Preparer Name R*** T********
Preparer Title Pipeline Compliance Senior Engineer
Preparer Email R*********@e****.com
Preparer Telephone 713-381-4659
Prepared Date 2024-10-09 00:00:00
Authorizer Name R*** T********
Authorizer Telephone 713-381-4659
Authorizer Title Pipeline Compliance Senior Engineer
Authorizer Email R*********@e****.com
Narrative On august 5th, 2024, at approximately 10:55 cdst, enterprise employees removed tank 1022 vertical booster pump for maintenance. Employees then observed product re-entering the evacuated can from a one-inch threaded plug on bottom of the pump. Upon investigation it appeared that the original sealant applied to the plug during install had degraded. For repair the failed plug was replaced with a solid steel core plug with approved thread sealant. Approximately 4 gallons were released and have been cleaned up. Nrc: #1406987 at 16:00 on 8/5/2024 48hr nrc: #1407177 at 10:32 on 8/7/2024

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