HL incident on 2024-07-26 — TX

Operator
Plains Pipeline, L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,915
Incident datetime
2024-07-26 00:00 UTC
Report number
Location
TX
Narrative
Approximately 15.3 barrels of crude oil were released from the tank 9 10inch inlet station piping at china grove station. The date and time of the release (part a q4) are indicative of the earliest date/time the release could have started based on the last time the incident location had been visited and confirmed to be no release of crude oil. The cause of the release is attributed to internal corrosion as a result of low-flow/no-flow conditions. To stop the immediate release, the release point was clamped, and the station piping will be cut out and replaced. Supplemental (1): updated the restart date/time.
Detailed record list
Report Received Date
2024-07-26 00:00:00
Iyear
2024
Report Number
20240174
Supplemental Number
40019
Report Type
Supplemental Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
-100.8419713
Commodity Released Type
Crude Oil
Unintentional Release Bbls
15.3
Recovered Bbls
15.3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
China Grove
Segment Name
Tank 9 10inch Inlet Station Piping
Onshore State Abbreviation
Tx
Onshore Postal Code
79526
Onshore City Name
Dunn
Onshore County Name
Scurry
Designated Location
Milepost
Designated Name
0+00mi
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
10
Pipe Wall Thickness
0.188
Pipe Smys
42000
Pipe Specification
Api5l
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Coating Applied Ind
No
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
978
Est Cost Prop Damage
5915
Est Cost Emergency
22904
Est Cost Environmental
0
Est Cost Other
0
Prpty
29797
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
30
Mop Psig
285
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1993-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Low-Flow/no-Flow Conditions
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
Yes
Exm Wave Ultrasonic Rcnt Year
2021
Exm Wave Ultrasonic Rcnt Ind
Yes
Preparer Name
N****** A G*******
Preparer Title
Hse Regulatory Compliance Supervisor
Preparer Email
N***************@p*****.com
Preparer Telephone
7136464376
Prepared Date
2024-09-23 00:00:00
Local Contact Name
N****** A G*******
Local Contact Email
N***************@p*****.com
Local Contact Telephone
8323341293
Authorizer Name
G******* P****
Authorizer Telephone
403-261-7420
Authorizer Title
Senior Manager - Regulatory
Authorizer Email
G*************@p*****.com
Narrative
Approximately 15.3 barrels of crude oil were released from the tank 9 10inch inlet station piping at china grove station. The date and time of the release (part a q4) are indicative of the earliest date/time the release could have started based on the last time the incident location had been visited and confirmed to be no release of crude oil. The cause of the release is attributed to internal corrosion as a result of low-flow/no-flow conditions. To stop the immediate release, the release point was clamped, and the station piping will be cut out and replaced. Supplemental (1): updated the restart date/time.
Report Received Date 2024-07-26 00:00:00
Iyear 2024
Report Number 20240174
Supplemental Number 40019
Report Type Supplemental Final
Operator Id 300 PHMSA Enforcement
Name Plains Pipeline, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 32.5320273 Google Maps OpenStreetMap
Location Longitude -100.8419713 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 15.3
Recovered Bbls 15.3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name China Grove
Segment Name Tank 9 10inch Inlet Station Piping
Onshore State Abbreviation Tx
Onshore Postal Code 79526
Onshore City Name Dunn
Onshore County Name Scurry
Designated Location Milepost
Designated Name 0+00mi
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 10
Pipe Wall Thickness 0.188
Pipe Smys 42000
Pipe Specification Api5l
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Coating Applied Ind No
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 978
Est Cost Prop Damage 5915
Est Cost Emergency 22904
Est Cost Environmental 0
Est Cost Other 0
Prpty 29797
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 30
Mop Psig 285
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 1993-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Other Corrosion Ind Yes
Int Corrosion Type Details Low-Flow/no-Flow Conditions
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind Yes
Exm Wave Ultrasonic Rcnt Year 2021
Exm Wave Ultrasonic Rcnt Ind Yes
Preparer Name N****** A G*******
Preparer Title Hse Regulatory Compliance Supervisor
Preparer Email N***************@p*****.com
Preparer Telephone 7136464376
Prepared Date 2024-09-23 00:00:00
Local Contact Name N****** A G*******
Local Contact Email N***************@p*****.com
Local Contact Telephone 8323341293
Authorizer Name G******* P****
Authorizer Telephone 403-261-7420
Authorizer Title Senior Manager - Regulatory
Authorizer Email G*************@p*****.com
Narrative Approximately 15.3 barrels of crude oil were released from the tank 9 10inch inlet station piping at china grove station. The date and time of the release (part a q4) are indicative of the earliest date/time the release could have started based on the last time the incident location had been visited and confirmed to be no release of crude oil. The cause of the release is attributed to internal corrosion as a result of low-flow/no-flow conditions. To stop the immediate release, the release point was clamped, and the station piping will be cut out and replaced. Supplemental (1): updated the restart date/time.

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