Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2024-06-14 — TX
Operator
Plains Pipeline, L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$14,000
Incident datetime
2024-06-14 00:00 UTC
Report number
Location
TX
Narrative
Approximately 6.5 barrels of crude oil were released from an auxiliary pig trap kicker valve at hewitt station. The date and time of the release (part a q4) are indicative of the earliest possible date/time the release could have started based on the last time the incident location had been visited and confirmed to be no release of crude oil. The cause of the release is attributed to equipment failure of the valve as a result of an incorrect o-ring installed by the manufacturer. To prevent future incidents, the valve will be replaced.
Detailed record list
Report Received Date
2024-06-14 00:00:00
Iyear
2024
Report Number
20240146
Supplemental Number
39682
Report Type
Original Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
34.1885674
Location Longitude
-97.37598619
Commodity Released Type
Crude Oil
Unintentional Release Bbls
6.5
Recovered Bbls
6.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
5/16/2024 12:45
Num Pub Evacuated
0
Pipe Fac Name
Hewitt Station
Segment Name
Valve 5013
Onshore State Abbreviation
Ok
Onshore Postal Code
73463
Onshore City Name
Wilson
Onshore County Name
Carter
Designated Location
Milepost
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2024
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Rubber Seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
80
Est Cost Prop Damage
14000
Est Cost Emergency
20000
Est Cost Environmental
0
Est Cost Other
0
Prpty
34080
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1120
Mop Psig
1440
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2021-07-08 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Additional Defect Ind
Yes
Preparer Name
N****** A G*******
Preparer Title
Hse Regulatory Compliance Supervisor
Preparer Email
N***************@p*****.com
Preparer Telephone
7136464376
Prepared Date
2024-06-14 00:00:00
Local Contact Name
N****** A G*******
Local Contact Email
N***************@p*****.com
Local Contact Telephone
7136464376
Authorizer Name
S***** A A*****
Authorizer Telephone
7139935676
Authorizer Title
Senior Manager-Hse-Integrity-And-Phmsa
Authorizer Email
S************@p*****.com
Narrative
Approximately 6.5 barrels of crude oil were released from an auxiliary pig trap kicker valve at hewitt station. The date and time of the release (part a q4) are indicative of the earliest possible date/time the release could have started based on the last time the incident location had been visited and confirmed to be no release of crude oil. The cause of the release is attributed to equipment failure of the valve as a result of an incorrect o-ring installed by the manufacturer. To prevent future incidents, the valve will be replaced.
Report Received Date | 2024-06-14 00:00:00 |
---|---|
Iyear | 2024 |
Report Number | 20240146 |
Supplemental Number | 39682 |
Report Type | Original Final |
Operator Id | 300 PHMSA Enforcement |
Name | Plains Pipeline, L.p. |
Operator Street Address | 333 Clay Street, Suite 1900 |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 34.1885674 Google Maps OpenStreetMap |
Location Longitude | -97.37598619 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 6.5 |
Recovered Bbls | 6.5 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | Yes |
Osro Arrived On Site Dt | 5/16/2024 12:45 |
Num Pub Evacuated | 0 |
Pipe Fac Name | Hewitt Station |
Segment Name | Valve 5013 |
Onshore State Abbreviation | Ok |
Onshore Postal Code | 73463 |
Onshore City Name | Wilson |
Onshore County Name | Carter |
Designated Location | Milepost |
Designated Name | 0+00 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Valve |
Valve Type | Auxiliary Or Other Valve |
Installation Year | 2024 |
Manufactured Year | Unknown |
Material Involved | Material Other Than Carbon Steel |
Material Details | Rubber Seal |
Release Type | Leak |
Leak Type | Seal Or Packing |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 80 |
Est Cost Prop Damage | 14000 |
Est Cost Emergency | 20000 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 34080 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 1120 |
Mop Psig | 1440 |
Mop Cfr Section | Component Design Pressure �195.406(A)(2) View CFR 49 §192 |
Maop Established Date | 2021-07-08 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | Yes, specify investigation result(s): (select all that apply) |
Invest Schedule Ind | Yes |
Invest No Control Room Ind | Yes |
Invest No Controller Ind | Yes |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Equipment Failure |
Cause Details | Non-Threaded Connection Failure |
Eq Failure Type | Non-Threaded Connection Failure |
Other Non Threaded Ind | O-Ring |
Additional Defect Ind | Yes |
Preparer Name | N****** A G******* |
Preparer Title | Hse Regulatory Compliance Supervisor |
Preparer Email | N***************@p*****.com |
Preparer Telephone | 7136464376 |
Prepared Date | 2024-06-14 00:00:00 |
Local Contact Name | N****** A G******* |
Local Contact Email | N***************@p*****.com |
Local Contact Telephone | 7136464376 |
Authorizer Name | S***** A A***** |
Authorizer Telephone | 7139935676 |
Authorizer Title | Senior Manager-Hse-Integrity-And-Phmsa |
Authorizer Email | S************@p*****.com |
Narrative | Approximately 6.5 barrels of crude oil were released from an auxiliary pig trap kicker valve at hewitt station. The date and time of the release (part a q4) are indicative of the earliest possible date/time the release could have started based on the last time the incident location had been visited and confirmed to be no release of crude oil. The cause of the release is attributed to equipment failure of the valve as a result of an incorrect o-ring installed by the manufacturer. To prevent future incidents, the valve will be replaced. |
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