Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2024-06-13 — TX
Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$80,000
Incident datetime
2024-06-13 00:00 UTC
Report number
Location
TX
Narrative
On 5/22/2024 at 9:45 am cdt, during station rounds, enterprise operator identified a crude release on tank line 5661 at midland tank farm; approximately 40 barrels of crude oil has release. The leak has been isolated and remediated. Apparent cause has been identified to be internal corrosion, and b-sleeve was installed to repair the pipe.
Detailed record list
Report Received Date
2024-06-13 00:00:00
Iyear
2024
Report Number
20240143
Supplemental Number
40562
Report Type
Supplemental Final
Operator Id
30829
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
32.0209
Location Longitude
-102.0162
Commodity Released Type
Crude Oil
Unintentional Release Bbls
40
Recovered Bbls
40
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Still Shutdown Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
1399635
Additional Nrc Report Numbers
1399806
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
5/22/2024 11:30
Num Pub Evacuated
0
Pipe Fac Name
Midland Tank Farm
Segment Name
Tank Line #5661
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Not Within A Municipality
Onshore County Name
Midland
Designated Location
Milepost
Designated Name
Tank Farm
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
30
Pipe Wall Thickness
0.75
Pipe Smys
52000
Pipe Specification
O1cs235
Pipe Seam Type
Spiral Welded
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Coating Applied Ind
Yes
Installation Year
2020
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
3102
Est Cost Prop Damage
80000
Est Cost Emergency
30000
Est Cost Environmental
0
Est Cost Other
0
Prpty
113102
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
30
Mop Psig
285
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2020-01-01 00:00:00
Maop Reversal Flow Ind
Bi-Directional
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pipeline control was not involved in this release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
Y******* B**
Preparer Title
Pipeline Compliance Engineer
Preparer Email
Y***@e****.com
Preparer Telephone
713-381-5650
Prepared Date
2025-02-27 00:00:00
Local Contact Name
Y******* B**
Local Contact Email
Y***@e****.com
Local Contact Telephone
713-381-5650
Authorizer Name
Y******* B**
Authorizer Telephone
713-381-5650
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
Y***@e****.com
Narrative
On 5/22/2024 at 9:45 am cdt, during station rounds, enterprise operator identified a crude release on tank line 5661 at midland tank farm; approximately 40 barrels of crude oil has release. The leak has been isolated and remediated. Apparent cause has been identified to be internal corrosion, and b-sleeve was installed to repair the pipe.
Report Received Date | 2024-06-13 00:00:00 |
---|---|
Iyear | 2024 |
Report Number | 20240143 |
Supplemental Number | 40562 |
Report Type | Supplemental Final |
Operator Id | 30829 PHMSA Enforcement |
Name | Enterprise Crude Pipeline Llc |
Operator Street Address | 1100 Louisiana Street |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Latitude | 32.0209 Google Maps OpenStreetMap |
Location Longitude | -102.0162 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 40 |
Recovered Bbls | 40 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Still Shutdown Ind | Yes |
Communication State Fed Ind | No |
Nrc Rpt Num | 1399635 NRC Report How to search |
Additional Nrc Report Numbers | 1399806 |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | Yes |
Osro Arrived On Site Dt | 5/22/2024 11:30 |
Num Pub Evacuated | 0 |
Pipe Fac Name | Midland Tank Farm |
Segment Name | Tank Line #5661 |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 79706 |
Onshore City Name | Not Within A Municipality |
Onshore County Name | Midland |
Designated Location | Milepost |
Designated Name | Tank Farm |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Pipe |
Pipe Type | Pipe Body |
Puddle Weld Ind | No |
Pipe Diameter | 30 |
Pipe Wall Thickness | 0.75 |
Pipe Smys | 52000 |
Pipe Specification | O1cs235 |
Pipe Seam Type | Spiral Welded |
Pipe Manufacturer | Unknown |
Pipe Coating Type | Fusion Bonded Epoxy(Fbe) |
Coating Applied Ind | Yes |
Installation Year | 2020 |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Pinhole |
Wildlife Impact Ind | No |
Soil Contamination | No |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 3102 |
Est Cost Prop Damage | 80000 |
Est Cost Emergency | 30000 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 113102 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 30 |
Mop Psig | 285 |
Mop Cfr Section | Component Design Pressure �195.406(A)(2) View CFR 49 §192 |
Maop Established Date | 2020-01-01 00:00:00 |
Maop Reversal Flow Ind | Bi-Directional |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | < 20% Smys Regulated Transmission |
Scada In Place Ind | No |
Cpm In Place Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Pipeline control was not involved in this release. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Corrosion Failure |
Cause Details | Internal Corrosion |
Internal External | Internal Corrosion |
Int Visual Exam Results | Not Cut Open |
Int Microbiological Ind | Yes |
Int Field Exam Basis Ind | Yes |
Int Low Point Pipe Loc Ind | Yes |
Corrosion Inhibitors | No |
Corrosion Lining | No |
Cleaning Dewatering | Not Applicable - Not Mainline Pipe |
Corrosion Coupons | Not Applicable - Not Mainline Pipe |
Collected Data Ind | No |
Has Hydrtst Conduc Before Ind | No |
Direct Asmnt Conducted | No |
Non Destructive Exam Ind | No |
Preparer Name | Y******* B** |
Preparer Title | Pipeline Compliance Engineer |
Preparer Email | Y***@e****.com |
Preparer Telephone | 713-381-5650 |
Prepared Date | 2025-02-27 00:00:00 |
Local Contact Name | Y******* B** |
Local Contact Email | Y***@e****.com |
Local Contact Telephone | 713-381-5650 |
Authorizer Name | Y******* B** |
Authorizer Telephone | 713-381-5650 |
Authorizer Title | Pipeline Compliance Engineer |
Authorizer Email | Y***@e****.com |
Narrative | On 5/22/2024 at 9:45 am cdt, during station rounds, enterprise operator identified a crude release on tank line 5661 at midland tank farm; approximately 40 barrels of crude oil has release. The leak has been isolated and remediated. Apparent cause has been identified to be internal corrosion, and b-sleeve was installed to repair the pipe. |
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