HL incident on 2024-06-12 — TX

Operator
Buckeye Development & Logistics, Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$36,843
Incident datetime
2024-06-12 00:00 UTC
Report number
Location
TX
Narrative
On monday, may 13th, 2024 at approximately 03:11 a local operator discovered a release of gasoline from a flange on the l7918 inside the cenovus refinery. The line was not running but the leak was isolated in coordination local operations, mt. Belvieu control center, and cenovus refinery operations. There were no injuries, fires, or offsite product to report with this release. The root cause was determined to be failure to follow procedures and installation of an incorrect gasket.
Detailed record list
Report Received Date
2024-06-12 00:00:00
Iyear
2024
Report Number
20240142
Supplemental Number
41111
Report Type
Supplemental Final
Operator Id
Name
Buckeye Development & Logistics, Llc
Operator Street Address
4200 Westheimer Road # 975
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77027
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
1
Recovered Bbls
0.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Shutdown At Time Of Accident Discovery And Not Scheduled To Run
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1399060
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
5/13/2024 4:01
Num Pub Evacuated
0
Pipe Fac Name
Cenovus Dock Line - Otter Creek Gas Lateral
Segment Name
L7918
Onshore State Abbreviation
Oh
Onshore Postal Code
43616
Onshore City Name
Oregon
Onshore County Name
Lucas
Designated Location
Survey Station No.
Designated Name
10+69
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
2024
Manufactured Year
2024
Material Involved
Material Other Than Carbon Steel
Material Details
Buna-Nitrile
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
36843
Est Cost Emergency
92690
Est Cost Environmental
0
Est Cost Other
0
Prpty
129633
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
12
Mop Psig
736
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2023-06-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
14
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The contributing factors and root causes associated with installation of gaskets and flange make up with field operations, in combination with the minimal product released.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
No
Io Wrong Equipment Ind
Yes
Io Inadequate Procedure Ind
Yes
Io Follow Procedure Ind
Yes
Preparer Name
A*** S******
Preparer Title
Dot Compliance Specialist
Preparer Email
A*******@b******.com
Preparer Telephone
4192505361
Prepared Date
2025-07-02 00:00:00
Authorizer Name
R***** O****
Authorizer Telephone
6109044524
Authorizer Title
Director Dot Compliance
Authorizer Email
R*****@b******.com
Narrative
On monday, may 13th, 2024 at approximately 03:11 a local operator discovered a release of gasoline from a flange on the l7918 inside the cenovus refinery. The line was not running but the leak was isolated in coordination local operations, mt. Belvieu control center, and cenovus refinery operations. There were no injuries, fires, or offsite product to report with this release. The root cause was determined to be failure to follow procedures and installation of an incorrect gasket.
Report Received Date 2024-06-12 00:00:00
Iyear 2024
Report Number 20240142
Supplemental Number 41111
Report Type Supplemental Final
Operator Id 31371 PHMSA Enforcement
Name Buckeye Development & Logistics, Llc
Operator Street Address 4200 Westheimer Road # 975
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77027
Time Zone Eastern
Daylight Savings Ind Yes
Location Latitude 41.674404 Google Maps OpenStreetMap
Location Longitude -83.46446 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 1
Recovered Bbls 0.9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Line Was Shutdown At Time Of Accident Discovery And Not Scheduled To Run
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1398758 NRC Report How to search
Additional Nrc Report Numbers 1399060
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Valve Type Ind Remotely Controlled
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind Yes
Osro Arrived On Site Dt 5/13/2024 4:01
Num Pub Evacuated 0
Pipe Fac Name Cenovus Dock Line - Otter Creek Gas Lateral
Segment Name L7918
Onshore State Abbreviation Oh
Onshore Postal Code 43616
Onshore City Name Oregon
Onshore County Name Lucas
Designated Location Survey Station No.
Designated Name 10+69
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Flange Assembly
Installation Year 2024
Manufactured Year 2024
Material Involved Material Other Than Carbon Steel
Material Details Buna-Nitrile
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 36843
Est Cost Emergency 92690
Est Cost Environmental 0
Est Cost Other 0
Prpty 129633
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 12
Mop Psig 736
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2023-06-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 14
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The contributing factors and root causes associated with installation of gaskets and flange make up with field operations, in combination with the minimal product released.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind No
Io Wrong Equipment Ind Yes
Io Inadequate Procedure Ind Yes
Io Follow Procedure Ind Yes
Preparer Name A*** S******
Preparer Title Dot Compliance Specialist
Preparer Email A*******@b******.com
Preparer Telephone 4192505361
Prepared Date 2025-07-02 00:00:00
Authorizer Name R***** O****
Authorizer Telephone 6109044524
Authorizer Title Director Dot Compliance
Authorizer Email R*****@b******.com
Narrative On monday, may 13th, 2024 at approximately 03:11 a local operator discovered a release of gasoline from a flange on the l7918 inside the cenovus refinery. The line was not running but the leak was isolated in coordination local operations, mt. Belvieu control center, and cenovus refinery operations. There were no injuries, fires, or offsite product to report with this release. The root cause was determined to be failure to follow procedures and installation of an incorrect gasket.

All rights reserved. Copyright © by ClearPHMSA