Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2024-06-12 — TX
Operator
Buckeye Development & Logistics, Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$36,843
Incident datetime
2024-06-12 00:00 UTC
Report number
Location
TX
Narrative
On monday, may 13th, 2024 at approximately 03:11 a local operator discovered a release of gasoline from a flange on the l7918 inside the cenovus refinery. The line was not running but the leak was isolated in coordination local operations, mt. Belvieu control center, and cenovus refinery operations. There were no injuries, fires, or offsite product to report with this release. The root cause was determined to be failure to follow procedures and installation of an incorrect gasket.
Detailed record list
Report Received Date
2024-06-12 00:00:00
Iyear
2024
Report Number
20240142
Supplemental Number
41111
Report Type
Supplemental Final
Operator Id
31371
Name
Buckeye Development & Logistics, Llc
Operator Street Address
4200 Westheimer Road # 975
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77027
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
41.674404
Location Longitude
-83.46446
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
1
Recovered Bbls
0.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Shutdown At Time Of Accident Discovery And Not Scheduled To Run
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
1398758
Additional Nrc Report Numbers
1399060
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
5/13/2024 4:01
Num Pub Evacuated
0
Pipe Fac Name
Cenovus Dock Line - Otter Creek Gas Lateral
Segment Name
L7918
Onshore State Abbreviation
Oh
Onshore Postal Code
43616
Onshore City Name
Oregon
Onshore County Name
Lucas
Designated Location
Survey Station No.
Designated Name
10+69
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
2024
Manufactured Year
2024
Material Involved
Material Other Than Carbon Steel
Material Details
Buna-Nitrile
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
36843
Est Cost Emergency
92690
Est Cost Environmental
0
Est Cost Other
0
Prpty
129633
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
12
Mop Psig
736
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2023-06-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
14
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The contributing factors and root causes associated with installation of gaskets and flange make up with field operations, in combination with the minimal product released.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
No
Io Wrong Equipment Ind
Yes
Io Inadequate Procedure Ind
Yes
Io Follow Procedure Ind
Yes
Preparer Name
A*** S******
Preparer Title
Dot Compliance Specialist
Preparer Email
A*******@b******.com
Preparer Telephone
4192505361
Prepared Date
2025-07-02 00:00:00
Authorizer Name
R***** O****
Authorizer Telephone
6109044524
Authorizer Title
Director Dot Compliance
Authorizer Email
R*****@b******.com
Narrative
On monday, may 13th, 2024 at approximately 03:11 a local operator discovered a release of gasoline from a flange on the l7918 inside the cenovus refinery. The line was not running but the leak was isolated in coordination local operations, mt. Belvieu control center, and cenovus refinery operations. There were no injuries, fires, or offsite product to report with this release. The root cause was determined to be failure to follow procedures and installation of an incorrect gasket.
Report Received Date | 2024-06-12 00:00:00 |
---|---|
Iyear | 2024 |
Report Number | 20240142 |
Supplemental Number | 41111 |
Report Type | Supplemental Final |
Operator Id | 31371 PHMSA Enforcement |
Name | Buckeye Development & Logistics, Llc |
Operator Street Address | 4200 Westheimer Road # 975 |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77027 |
Time Zone | Eastern |
Daylight Savings Ind | Yes |
Location Latitude | 41.674404 Google Maps OpenStreetMap |
Location Longitude | -83.46446 Google Maps OpenStreetMap |
Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
Commodity Subtype | Gasoline (Non-Ethanol) |
Unintentional Release Bbls | 1 |
Recovered Bbls | 0.9 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Pipeline, Including Valve Sites |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | No |
Shutdown Explain | Line Was Shutdown At Time Of Accident Discovery And Not Scheduled To Run |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | 1398758 NRC Report How to search |
Additional Nrc Report Numbers | 1399060 |
Ignite Ind | No |
Upstream Action Taken | Valve Closure |
Upstream Valve Type Ind | Remotely Controlled |
Downstream Action Taken | Valve Closure |
Downstream Valve Type Ind | Remotely Controlled |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | Yes |
Osro Arrived On Site Dt | 5/13/2024 4:01 |
Num Pub Evacuated | 0 |
Pipe Fac Name | Cenovus Dock Line - Otter Creek Gas Lateral |
Segment Name | L7918 |
Onshore State Abbreviation | Oh |
Onshore Postal Code | 43616 |
Onshore City Name | Oregon |
Onshore County Name | Lucas |
Designated Location | Survey Station No. |
Designated Name | 10+69 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Intrastate |
Item Involved | Flange Assembly |
Installation Year | 2024 |
Manufactured Year | 2024 |
Material Involved | Material Other Than Carbon Steel |
Material Details | Buna-Nitrile |
Release Type | Leak |
Leak Type | Connection Failure |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | Yes |
Soil Remed Ind | Yes |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | Yes |
High Pop Ind | Yes |
High Pop Yes No | Yes |
Other Pop Ind | Yes |
Other Pop Yes No | Yes |
Usa Ecological Ind | Yes |
Usa Ecological Yes No | Yes |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 100 |
Est Cost Prop Damage | 36843 |
Est Cost Emergency | 92690 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 129633 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 12 |
Mop Psig | 736 |
Mop Cfr Section | Component Design Pressure �195.406(A)(2) View CFR 49 §192 |
Maop Established Date | 2023-06-01 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Length Segment Isolated | 14 |
Internal Inspection Ind | Yes |
Operation Complications Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | The contributing factors and root causes associated with installation of gaskets and flange make up with field operations, in combination with the minimal product released. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Incorrect Operation |
Cause Details | Equipment Not Installed Properly |
Operation Type | Equipment Not Installed Properly |
Related Failure Follow Ind | Yes |
Category Type | Routine Maintenance |
Operator Qualification Ind | No |
Io Wrong Equipment Ind | Yes |
Io Inadequate Procedure Ind | Yes |
Io Follow Procedure Ind | Yes |
Preparer Name | A*** S****** |
Preparer Title | Dot Compliance Specialist |
Preparer Email | A*******@b******.com |
Preparer Telephone | 4192505361 |
Prepared Date | 2025-07-02 00:00:00 |
Authorizer Name | R***** O**** |
Authorizer Telephone | 6109044524 |
Authorizer Title | Director Dot Compliance |
Authorizer Email | R*****@b******.com |
Narrative | On monday, may 13th, 2024 at approximately 03:11 a local operator discovered a release of gasoline from a flange on the l7918 inside the cenovus refinery. The line was not running but the leak was isolated in coordination local operations, mt. Belvieu control center, and cenovus refinery operations. There were no injuries, fires, or offsite product to report with this release. The root cause was determined to be failure to follow procedures and installation of an incorrect gasket. |
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