GTG incident on 2024-10-17 — OK

Operator
Monroe Gas Storage Company, Llc
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$400,000
Incident datetime
2024-10-17 00:00 UTC
Report number
Location
OK
Narrative
On friday afternoon 9/20/24 at 13:21 ct, a technician at the monroe gas storage compressor station observed small bubbles rising within a puddle of water while doing regular inspection rounds within the fenced facility. After confirming the presence of natural gas at the location and suspecting a pinhole leak, the 18" eastside gas transmission line was isolated by manually closing the downstream valves. Because the line was not flowing at the time, the upstream valves were already closed. The effected line segment was isolated by 14:13 ct. After initial coordination regarding possible cost of repair, it was determined to classify the event as an incident and notify the national response center (nrc). The nrc was notified by the williams security operations center at 15:27 ct. The pipeline was safely blown down with lock out / tag out completed by 19:20 ct that evening. Due to the pipeline's 10' depth in the area, it took multiple days for contractors to clean the line through cleaning pigs, purge with nitrogen and pothole through hydrovacing to pinpoint the leak location. Once identified (through detecting the presence of nitrogen), the leak location was fully and safely excavated (considering the significant depth) on 10/14/24. As of 10/15/24, internal corrosion was found at the pinhole leak location. The effected pipe immediately near the leak location was cut-out on 10/17/24 and sent to a lab for analysis. Williams operations, pipeline integrity and construction teams established a conservative plan to replace necessary pipe and return the line to service. Approximately 350 feet of 18-inch pipe in the low area of the pipeline (within the facility) was replaced and hydrotested. The line was returned to service on 11/9/2024. The cause is suspected to be sulfate reducing bacteria microbiologically influenced corrosion (srb-mic) based on lab results. Representatives from operations, management and pipeline integrity have established an internal corrosion mitigation plan to prevent reoccurrence. Coupons have been installed at each well head location and other locations, based on internal corrosion data gathered, operations, management, compliance and corrosion department will deem if more locations are needed. A pigging program that includes all 13 laterals is forthcoming, with additional focus on the 18" lateral.
Detailed record list
Report Received Date
2024-10-17 00:00:00
Iyear
2024
Report Number
20240118
Supplemental Number
40404
Report Type
Supplemental Final
Operator Id
Name
Monroe Gas Storage Company, Llc
Operator Street Address
One Williams Center
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Additional Nrc Report Numbers
1411606
Commodity Released Type
Natural Gas
Unintentional Release
164
Intentional Release
530
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Still Shutdown Ind
Yes
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Downstream Action Taken
Valve Closure
Num Pub Evacuated
0
On Off Shore
Onshore
Onshore State Abbreviation
Ms
Onshore Postal Code
38821
Onshore City Name
Amory
Onshore County Name
Monroe
Designated Location
Milepost
Designated Name
0.01
Pipe Fac Name
Monroe Gas Storage Facility
Segment Name
18" Eastside Transmission Line
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
120
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
18
Puddle Weld Ind
No
Pipe Wall Thickness
0.375
Pipe Smys
60000
Pipe Specification
Api 5l Psl2
Pipe Seam Type
Longitudinal Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Epoxy
Coating Applied Ind
Yes
Installation Year
2009
Manufactured Year
2008
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
471
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
492
Est Cost Intentional Release
1590
Est Cost Prop Damage
400000
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
3
Prpty
402082
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
876
Gas Flow In Pipe In Mcf
0
Mop Psig
1440
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2009-04-06 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Manual
Length Segment Isolated
4804
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room management was not considered a factor in the incident cause or response.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Suspected Microbial.
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2024
Hydrtst Most Rcnt Pressure
2193
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S*** R***
Preparer Title
Pipeline Safety Engineer
Preparer Email
S********@w*******.com
Preparer Telephone
713-449-2720
Local Contact Name
L**** V******
Local Contact Email
L***************@w*******.com
Local Contact Telephone
318-535-8035
Authorizer Name
E*** W****
Authorizer Title
Mgr Pipeline Safety
Authorizer Telephone
281-536-9504
Authorizer Email
E*********@w*******.com
Narrative
On friday afternoon 9/20/24 at 13:21 ct, a technician at the monroe gas storage compressor station observed small bubbles rising within a puddle of water while doing regular inspection rounds within the fenced facility. After confirming the presence of natural gas at the location and suspecting a pinhole leak, the 18" eastside gas transmission line was isolated by manually closing the downstream valves. Because the line was not flowing at the time, the upstream valves were already closed. The effected line segment was isolated by 14:13 ct. After initial coordination regarding possible cost of repair, it was determined to classify the event as an incident and notify the national response center (nrc). The nrc was notified by the williams security operations center at 15:27 ct. The pipeline was safely blown down with lock out / tag out completed by 19:20 ct that evening. Due to the pipeline's 10' depth in the area, it took multiple days for contractors to clean the line through cleaning pigs, purge with nitrogen and pothole through hydrovacing to pinpoint the leak location. Once identified (through detecting the presence of nitrogen), the leak location was fully and safely excavated (considering the significant depth) on 10/14/24. As of 10/15/24, internal corrosion was found at the pinhole leak location. The effected pipe immediately near the leak location was cut-out on 10/17/24 and sent to a lab for analysis. Williams operations, pipeline integrity and construction teams established a conservative plan to replace necessary pipe and return the line to service. Approximately 350 feet of 18-inch pipe in the low area of the pipeline (within the facility) was replaced and hydrotested. The line was returned to service on 11/9/2024. The cause is suspected to be sulfate reducing bacteria microbiologically influenced corrosion (srb-mic) based on lab results. Representatives from operations, management and pipeline integrity have established an internal corrosion mitigation plan to prevent reoccurrence. Coupons have been installed at each well head location and other locations, based on internal corrosion data gathered, operations, management, compliance and corrosion department will deem if more locations are needed. A pigging program that includes all 13 laterals is forthcoming, with additional focus on the 18" lateral.
Report Received Date 2024-10-17 00:00:00
Iyear 2024
Report Number 20240118
Supplemental Number 40404
Report Type Supplemental Final
Operator Id 32374 PHMSA Enforcement
Name Monroe Gas Storage Company, Llc
Operator Street Address One Williams Center
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 34.01305 Google Maps OpenStreetMap
Location Longitude -88.45674 Google Maps OpenStreetMap
Nrc Rpt Num 1411453 NRC Report How to search
Additional Nrc Report Numbers 1411606
Commodity Released Type Natural Gas
Unintentional Release 164
Intentional Release 530
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Still Shutdown Ind Yes
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Valve Closure
Downstream Action Taken Valve Closure
Num Pub Evacuated 0
On Off Shore Onshore
Onshore State Abbreviation Ms
Onshore Postal Code 38821
Onshore City Name Amory
Onshore County Name Monroe
Designated Location Milepost
Designated Name 0.01
Pipe Fac Name Monroe Gas Storage Facility
Segment Name 18" Eastside Transmission Line
Federal No
Location Type Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 120
Other Underground Facilities No
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 18
Puddle Weld Ind No
Pipe Wall Thickness 0.375
Pipe Smys 60000
Pipe Specification Api 5l Psl2
Pipe Seam Type Longitudinal Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Epoxy
Coating Applied Ind Yes
Installation Year 2009
Manufactured Year 2008
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 471
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 492
Est Cost Intentional Release 1590
Est Cost Prop Damage 400000
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 3
Prpty 402082
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 876
Gas Flow In Pipe In Mcf 0
Mop Psig 1440
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 2009-04-06 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Manual
Length Segment Isolated 4804
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room management was not considered a factor in the incident cause or response.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Other Corrosion Ind Yes
Int Corrosion Type Details Suspected Microbial.
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2024
Hydrtst Most Rcnt Pressure 2193
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S*** R***
Preparer Title Pipeline Safety Engineer
Preparer Email S********@w*******.com
Preparer Telephone 713-449-2720
Local Contact Name L**** V******
Local Contact Email L***************@w*******.com
Local Contact Telephone 318-535-8035
Authorizer Name E*** W****
Authorizer Title Mgr Pipeline Safety
Authorizer Telephone 281-536-9504
Authorizer Email E*********@w*******.com
Narrative On friday afternoon 9/20/24 at 13:21 ct, a technician at the monroe gas storage compressor station observed small bubbles rising within a puddle of water while doing regular inspection rounds within the fenced facility. After confirming the presence of natural gas at the location and suspecting a pinhole leak, the 18" eastside gas transmission line was isolated by manually closing the downstream valves. Because the line was not flowing at the time, the upstream valves were already closed. The effected line segment was isolated by 14:13 ct. After initial coordination regarding possible cost of repair, it was determined to classify the event as an incident and notify the national response center (nrc). The nrc was notified by the williams security operations center at 15:27 ct. The pipeline was safely blown down with lock out / tag out completed by 19:20 ct that evening. Due to the pipeline's 10' depth in the area, it took multiple days for contractors to clean the line through cleaning pigs, purge with nitrogen and pothole through hydrovacing to pinpoint the leak location. Once identified (through detecting the presence of nitrogen), the leak location was fully and safely excavated (considering the significant depth) on 10/14/24. As of 10/15/24, internal corrosion was found at the pinhole leak location. The effected pipe immediately near the leak location was cut-out on 10/17/24 and sent to a lab for analysis. Williams operations, pipeline integrity and construction teams established a conservative plan to replace necessary pipe and return the line to service. Approximately 350 feet of 18-inch pipe in the low area of the pipeline (within the facility) was replaced and hydrotested. The line was returned to service on 11/9/2024. The cause is suspected to be sulfate reducing bacteria microbiologically influenced corrosion (srb-mic) based on lab results. Representatives from operations, management and pipeline integrity have established an internal corrosion mitigation plan to prevent reoccurrence. Coupons have been installed at each well head location and other locations, based on internal corrosion data gathered, operations, management, compliance and corrosion department will deem if more locations are needed. A pigging program that includes all 13 laterals is forthcoming, with additional focus on the 18" lateral.

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