HL incident on 2024-05-06 — TX

Operator
Oryx Delaware Oil Transport Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$4,000
Incident datetime
2024-05-06 00:00 UTC
Report number
Location
TX
Narrative
Approximately 6 barrels of crude oil were released from sump 2090 at oryx carlsbad station. The date and time of the release (part a q4) are indicative of the earliest possible date/time the release could have started based on control center information. The cause of the release is attributed to equipment failure of a check valve likely as a result of debris caught in the check valve, allowing the sump to overfill. Additionally, the sump hi-hi alarm failed to alarm due to program settings that were not re-set following testing. To prevent future incidents, the check valve was replaced and the programming on the sump hi-hi alarm was reset, tested, and verified. Supplemental narrative (1): updates applied to question 8 in part d.
Detailed record list
Report Received Date
2024-05-06 00:00:00
Iyear
2024
Report Number
20240111
Supplemental Number
39535
Report Type
Supplemental Final
Operator Id
Name
Oryx Delaware Oil Transport Llc
Operator Street Address
333 Clay St. Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Mountain
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
6
Recovered Bbls
6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oryx Carlsbad
Segment Name
Sump 2090
Onshore State Abbreviation
Nm
Onshore Postal Code
88256
Onshore City Name
Loving
Onshore County Name
Eddy
Designated Location
Milepost
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
516
Est Cost Prop Damage
4000
Est Cost Emergency
9600
Est Cost Environmental
0
Est Cost Other
0
Prpty
14116
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
66
Mop Psig
285
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2021-01-21 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Check Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Debris Caught In The Check Valve
Io Follow Procedure Ind
Yes
Preparer Name
N****** A G*******
Preparer Title
Hse Regulatory Compliance Supervisor
Preparer Email
N***************@p*****.com
Preparer Telephone
7136464376
Prepared Date
2024-05-09 00:00:00
Local Contact Name
N****** A G*******
Local Contact Email
N***************@p*****.com
Local Contact Telephone
7136464376
Authorizer Name
S***** A A*****
Authorizer Telephone
7139935676
Authorizer Title
Senior Manager-Hse-Integrity-And-Phmsa
Authorizer Email
S************@p*****.com
Narrative
Approximately 6 barrels of crude oil were released from sump 2090 at oryx carlsbad station. The date and time of the release (part a q4) are indicative of the earliest possible date/time the release could have started based on control center information. The cause of the release is attributed to equipment failure of a check valve likely as a result of debris caught in the check valve, allowing the sump to overfill. Additionally, the sump hi-hi alarm failed to alarm due to program settings that were not re-set following testing. To prevent future incidents, the check valve was replaced and the programming on the sump hi-hi alarm was reset, tested, and verified. Supplemental narrative (1): updates applied to question 8 in part d.
Report Received Date 2024-05-06 00:00:00
Iyear 2024
Report Number 20240111
Supplemental Number 39535
Report Type Supplemental Final
Operator Id 39654 PHMSA Enforcement
Name Oryx Delaware Oil Transport Llc
Operator Street Address 333 Clay St. Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Mountain
Daylight Savings Ind Yes
Location Latitude 32.296488 Google Maps OpenStreetMap
Location Longitude -104.123804 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 6
Recovered Bbls 6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Oryx Carlsbad
Segment Name Sump 2090
Onshore State Abbreviation Nm
Onshore Postal Code 88256
Onshore City Name Loving
Onshore County Name Eddy
Designated Location Milepost
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 516
Est Cost Prop Damage 4000
Est Cost Emergency 9600
Est Cost Environmental 0
Est Cost Other 0
Prpty 14116
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 66
Mop Psig 285
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2021-01-21 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Check Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Debris Caught In The Check Valve
Io Follow Procedure Ind Yes
Preparer Name N****** A G*******
Preparer Title Hse Regulatory Compliance Supervisor
Preparer Email N***************@p*****.com
Preparer Telephone 7136464376
Prepared Date 2024-05-09 00:00:00
Local Contact Name N****** A G*******
Local Contact Email N***************@p*****.com
Local Contact Telephone 7136464376
Authorizer Name S***** A A*****
Authorizer Telephone 7139935676
Authorizer Title Senior Manager-Hse-Integrity-And-Phmsa
Authorizer Email S************@p*****.com
Narrative Approximately 6 barrels of crude oil were released from sump 2090 at oryx carlsbad station. The date and time of the release (part a q4) are indicative of the earliest possible date/time the release could have started based on control center information. The cause of the release is attributed to equipment failure of a check valve likely as a result of debris caught in the check valve, allowing the sump to overfill. Additionally, the sump hi-hi alarm failed to alarm due to program settings that were not re-set following testing. To prevent future incidents, the check valve was replaced and the programming on the sump hi-hi alarm was reset, tested, and verified. Supplemental narrative (1): updates applied to question 8 in part d.

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