GTG incident on 2024-08-28 — TX

Operator
Northwest Pipeline Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200,000
Incident datetime
2024-08-28 00:00 UTC
Report number
Location
TX
Narrative
On friday august, 2 2024 at 10:59 am, dig 32020 was being excavated at mp 1153.5 on the ignacio to sumas mainline line 1400. This work is part of the 2024 goldendale to willard anomaly digs. During excavation, personnel heard the sound of gas blowing through a hole. The excavation was stopped and it was investigated using gas detectors. Lel was picked up on gas monitors, and the leak location was confirmed using liquid leak detect agent. A leak clamp was not readily available, so the crew demobilized for the day. The following morning, the excavation was completed by hand while monitoring for lel. Initial investigation indicates a manufacturing defect in the long seam of the dsaw pipe. A temporary plidco leak clamp was successfully installed on 8/3/24, at 10:30 am. Permanent repair by cutout is expected to be completed in the future.
Detailed record list
Report Received Date
2024-08-28 00:00:00
Iyear
2024
Report Number
20240104
Supplemental Number
39947
Report Type
Original
Operator Id
Name
Northwest Pipeline Llc
Operator Street Address
2800 Post Oak Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77056
Time Zone
Pacific
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
-121.1975303
Nrc Rpt Num
Additional Nrc Report Numbers
1406825
Commodity Released Type
Natural Gas
Unintentional Release
700
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Small Crack In Long Seam Appears Stable. Temporary Plidco Leak Clamp Installed
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
Line Was Already At Reduced Pressure For The Dig. Line Already Isolated For A Near By Project.
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
Line Was Already At Reduced Pressure For The Dig. Line Already Isolated For A Near By Project.
Num Pub Evacuated
0
On Off Shore
Onshore
Onshore State Abbreviation
Wa
Onshore Postal Code
98635
Onshore City Name
Lyle
Onshore County Name
Klickitat
Designated Location
Milepost
Designated Name
1153.5
Pipe Fac Name
Ignacio To Sumas Mainline
Segment Name
1400
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
60
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
26
Pipe Wall Thickness
0.281
Pipe Smys
52000
Pipe Specification
Api 5lx
Pipe Seam Type
Dsaw
Pipe Manufacturer
Consolidated
Pipe Coating Type
Asphalt
Coating Applied Ind
Unknown
Installation Year
1956
Manufactured Year
1955
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
630
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
1750
Est Cost Intentional Release
0
Est Cost Prop Damage
200000
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
2.5
Prpty
201750
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
610
Gas Flow In Pipe In Mcf
0
Mop Psig
809
Mop Cfr Section
Maop Established Date
1970-06-30 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Length Segment Isolated
85166
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Other
Accident Details
Dig Investigation Following Ili Tool Survey
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak found during an anomaly dig resulting from an ili inspection. Leak was too small to cause a drop in line pressure.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Pwjf Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Still Under Invest Ind
Yes
Post Constr Pressure Test Val
860
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Emat Ind
Yes
Axial Recent Year
2023
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
High Resolution
Axial Previous Year
2019
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
High Resolution
Geometry Recent Year
2023
Geometry Rcnt Propul Method
Free Swimming
Geometry Rcnt Resolution
High Resolution
Geometrt Rcnt Measur Cups
No Cups
Geometry Previous Year
2019
Geometry Prev Propul Method
Free Swimming
Geometry Prev Resolution
High Resolution
Geometrt Prev Measur Cups
No Cups
Emat Recent Year
2023
Emat Rcnt Propul Method
Free Swimming
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
C********** E*****
Preparer Title
Senior Engineer
Preparer Email
C***********@w*******.com
Preparer Telephone
570-406-0743
Authorizer Name
E*** W****
Authorizer Title
Manager Pipeline Safety
Authorizer Telephone
713-215-3459
Authorizer Email
E*********@w*******.com
Narrative
On friday august, 2 2024 at 10:59 am, dig 32020 was being excavated at mp 1153.5 on the ignacio to sumas mainline line 1400. This work is part of the 2024 goldendale to willard anomaly digs. During excavation, personnel heard the sound of gas blowing through a hole. The excavation was stopped and it was investigated using gas detectors. Lel was picked up on gas monitors, and the leak location was confirmed using liquid leak detect agent. A leak clamp was not readily available, so the crew demobilized for the day. The following morning, the excavation was completed by hand while monitoring for lel. Initial investigation indicates a manufacturing defect in the long seam of the dsaw pipe. A temporary plidco leak clamp was successfully installed on 8/3/24, at 10:30 am. Permanent repair by cutout is expected to be completed in the future.
Report Received Date 2024-08-28 00:00:00
Iyear 2024
Report Number 20240104
Supplemental Number 39947
Report Type Original
Operator Id 13845 PHMSA Enforcement
Name Northwest Pipeline Llc
Operator Street Address 2800 Post Oak Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77056
Time Zone Pacific
Daylight Savings Ind Yes
Location Latitude 45.7652948 Google Maps OpenStreetMap
Location Longitude -121.1975303 Google Maps OpenStreetMap
Nrc Rpt Num 1406700 NRC Report How to search
Additional Nrc Report Numbers 1406825
Commodity Released Type Natural Gas
Unintentional Release 700
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Small Crack In Long Seam Appears Stable. Temporary Plidco Leak Clamp Installed
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Operational Control
Upstream Oprtnl Cntrl Detail Line Was Already At Reduced Pressure For The Dig. Line Already Isolated For A Near By Project.
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail Line Was Already At Reduced Pressure For The Dig. Line Already Isolated For A Near By Project.
Num Pub Evacuated 0
On Off Shore Onshore
Onshore State Abbreviation Wa
Onshore Postal Code 98635
Onshore City Name Lyle
Onshore County Name Klickitat
Designated Location Milepost
Designated Name 1153.5
Pipe Fac Name Ignacio To Sumas Mainline
Segment Name 1400
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 60
Other Underground Facilities No
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 26
Pipe Wall Thickness 0.281
Pipe Smys 52000
Pipe Specification Api 5lx
Pipe Seam Type Dsaw
Pipe Manufacturer Consolidated
Pipe Coating Type Asphalt
Coating Applied Ind Unknown
Installation Year 1956
Manufactured Year 1955
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 630
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 1750
Est Cost Intentional Release 0
Est Cost Prop Damage 200000
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 2.5
Prpty 201750
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 610
Gas Flow In Pipe In Mcf 0
Mop Psig 809
Mop Cfr Section 192.619(C) View CFR 49 §192
Maop Established Date 1970-06-30 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Length Segment Isolated 85166
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Other
Accident Details Dig Investigation Following Ili Tool Survey
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak found during an anomaly dig resulting from an ili inspection. Leak was too small to cause a drop in line pressure.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Pwjf Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Still Under Invest Ind Yes
Post Constr Pressure Test Val 860
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Emat Ind Yes
Axial Recent Year 2023
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal High Resolution
Axial Previous Year 2019
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal High Resolution
Geometry Recent Year 2023
Geometry Rcnt Propul Method Free Swimming
Geometry Rcnt Resolution High Resolution
Geometrt Rcnt Measur Cups No Cups
Geometry Previous Year 2019
Geometry Prev Propul Method Free Swimming
Geometry Prev Resolution High Resolution
Geometrt Prev Measur Cups No Cups
Emat Recent Year 2023
Emat Rcnt Propul Method Free Swimming
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name C********** E*****
Preparer Title Senior Engineer
Preparer Email C***********@w*******.com
Preparer Telephone 570-406-0743
Authorizer Name E*** W****
Authorizer Title Manager Pipeline Safety
Authorizer Telephone 713-215-3459
Authorizer Email E*********@w*******.com
Narrative On friday august, 2 2024 at 10:59 am, dig 32020 was being excavated at mp 1153.5 on the ignacio to sumas mainline line 1400. This work is part of the 2024 goldendale to willard anomaly digs. During excavation, personnel heard the sound of gas blowing through a hole. The excavation was stopped and it was investigated using gas detectors. Lel was picked up on gas monitors, and the leak location was confirmed using liquid leak detect agent. A leak clamp was not readily available, so the crew demobilized for the day. The following morning, the excavation was completed by hand while monitoring for lel. Initial investigation indicates a manufacturing defect in the long seam of the dsaw pipe. A temporary plidco leak clamp was successfully installed on 8/3/24, at 10:30 am. Permanent repair by cutout is expected to be completed in the future.

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