GTG incident on 2024-07-16 — TX

Operator
Bbt Sigco Intrastate, Llc
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$389,000
Incident datetime
2024-07-16 00:00 UTC
Report number
Location
TX
Narrative
On 6/17/2024 bubbling was seen from a third-party helicopter pilot. The pilot reported the situation to bbt which they investigated and confirmed on 6/18/2024 to be the 16" bbt pipeline. Bbt initially treated it as a src due to the nature of the event (slow leak) and the vicinity (in the marsh, 1.5 miles from the nearest building), but was elevated to an incident within an hour when it was determined it was going to exceed the regulatory requirement in becoming an incident on 6/28/2024 (due to the mobilization cost and equipment needed in the marsh) . The leak was isolated immediately, and discussions were made to minimize fugitive emissions. As a result, customers burned down the gas to the regulator set point (200psi). The remaining gas was blown down to initiate repairs. Repairs started on 6/24/2024 (weld-on sleeve) and the pipeline was returned to service on 7/1/2024. Localized pitting was determined to be the cause in-between the concrete coatings near the seams where coal tar is the coating.
Detailed record list
Report Received Date
2024-07-16 00:00:00
Iyear
2024
Report Number
20240092
Supplemental Number
40198
Report Type
Supplemental Final
Operator Id
Name
Bbt Sigco Intrastate, Llc
Operator Street Address
Black Bear Transmission, Llc 1501 Mckinney, Suite 800
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77010
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Additional Nrc Report Numbers
1403477
Commodity Released Type
Natural Gas
Unintentional Release
1900
Intentional Release
2570
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Downstream Action Taken
Valve Closure
Num Pub Evacuated
0
On Off Shore
Onshore
Onshore State Abbreviation
La
Onshore Postal Code
70043
Onshore City Name
Not Within A Municipality
Onshore County Name
St. Bernard Parish
Designated Location
Not Applicable
Pipe Fac Name
Bbt Sigco Intrastate, Llc - 31424
Segment Name
16" Pipeline
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Other
Incident Area Details
Marsh
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
16
Puddle Weld Ind
No
Pipe Wall Thickness
0.25
Pipe Smys
42000
Pipe Specification
Api 5l X42
Pipe Seam Type
Longitudinal Erw - Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Other
Pipe Coating Details
Coal Tar
Coating Applied Ind
Unknown
Installation Year
1958
Manufactured Year
1958
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
340
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
746
Est Cost Intentional Release
1009
Est Cost Prop Damage
389000
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
0.3928
Prpty
390755
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
730
Gas Flow In Pipe In Mcf
15
Mop Psig
945
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1958-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
76612
Internal Inspection Ind
No
Unsuitable Mainline Ind
Yes
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Pig Traps Needed For An Ili Run
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was elevated to be an incident only due to the cost of the repair. Initially treated as a src.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Other Corrosion Ind
Yes
Corrosion Type Details
Corrosion Was In-Between The Concrete Coatings Near The Seam Where Coal Tar Is The Coating (Localized Pitting).
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2023
Prior Damage
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
J**** K*********
Preparer Title
Director - Compliance Engineering And Operations
Preparer Email
J**********@c******.com
Preparer Telephone
8325817806
Local Contact Name
T*** S******
Local Contact Email
T*******@b***********.com
Local Contact Telephone
3183553439
Authorizer Name
W****** K*********
Authorizer Title
Director - Compliance Engineering And Operations
Authorizer Telephone
8325817806
Authorizer Email
J**********@c******.com
Narrative
On 6/17/2024 bubbling was seen from a third-party helicopter pilot. The pilot reported the situation to bbt which they investigated and confirmed on 6/18/2024 to be the 16" bbt pipeline. Bbt initially treated it as a src due to the nature of the event (slow leak) and the vicinity (in the marsh, 1.5 miles from the nearest building), but was elevated to an incident within an hour when it was determined it was going to exceed the regulatory requirement in becoming an incident on 6/28/2024 (due to the mobilization cost and equipment needed in the marsh) . The leak was isolated immediately, and discussions were made to minimize fugitive emissions. As a result, customers burned down the gas to the regulator set point (200psi). The remaining gas was blown down to initiate repairs. Repairs started on 6/24/2024 (weld-on sleeve) and the pipeline was returned to service on 7/1/2024. Localized pitting was determined to be the cause in-between the concrete coatings near the seams where coal tar is the coating.
Report Received Date 2024-07-16 00:00:00
Iyear 2024
Report Number 20240092
Supplemental Number 40198
Report Type Supplemental Final
Operator Id 31424 PHMSA Enforcement
Name Bbt Sigco Intrastate, Llc
Operator Street Address Black Bear Transmission, Llc 1501 Mckinney, Suite 800
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77010
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.8680278 Google Maps OpenStreetMap
Location Longitude -89.7434167 Google Maps OpenStreetMap
Nrc Rpt Num 1403238 NRC Report How to search
Additional Nrc Report Numbers 1403477
Commodity Released Type Natural Gas
Unintentional Release 1900
Intentional Release 2570
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Valve Closure
Downstream Action Taken Valve Closure
Num Pub Evacuated 0
On Off Shore Onshore
Onshore State Abbreviation La
Onshore Postal Code 70043
Onshore City Name Not Within A Municipality
Onshore County Name St. Bernard Parish
Designated Location Not Applicable
Pipe Fac Name Bbt Sigco Intrastate, Llc - 31424
Segment Name 16" Pipeline
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Other
Incident Area Details Marsh
Other Underground Facilities No
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 16
Puddle Weld Ind No
Pipe Wall Thickness 0.25
Pipe Smys 42000
Pipe Specification Api 5l X42
Pipe Seam Type Longitudinal Erw - Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Other
Pipe Coating Details Coal Tar
Coating Applied Ind Unknown
Installation Year 1958
Manufactured Year 1958
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 340
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 746
Est Cost Intentional Release 1009
Est Cost Prop Damage 389000
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 0.3928
Prpty 390755
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 730
Gas Flow In Pipe In Mcf 15
Mop Psig 945
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1958-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 76612
Internal Inspection Ind No
Unsuitable Mainline Ind Yes
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Pig Traps Needed For An Ili Run
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Public
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was elevated to be an incident only due to the cost of the repair. Initially treated as a src.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Other Corrosion Ind Yes
Corrosion Type Details Corrosion Was In-Between The Concrete Coatings Near The Seam Where Coal Tar Is The Coating (Localized Pitting).
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Shielding Evident No
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2023
Prior Damage No
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name J**** K*********
Preparer Title Director - Compliance Engineering And Operations
Preparer Email J**********@c******.com
Preparer Telephone 8325817806
Local Contact Name T*** S******
Local Contact Email T*******@b***********.com
Local Contact Telephone 3183553439
Authorizer Name W****** K*********
Authorizer Title Director - Compliance Engineering And Operations
Authorizer Telephone 8325817806
Authorizer Email J**********@c******.com
Narrative On 6/17/2024 bubbling was seen from a third-party helicopter pilot. The pilot reported the situation to bbt which they investigated and confirmed on 6/18/2024 to be the 16" bbt pipeline. Bbt initially treated it as a src due to the nature of the event (slow leak) and the vicinity (in the marsh, 1.5 miles from the nearest building), but was elevated to an incident within an hour when it was determined it was going to exceed the regulatory requirement in becoming an incident on 6/28/2024 (due to the mobilization cost and equipment needed in the marsh) . The leak was isolated immediately, and discussions were made to minimize fugitive emissions. As a result, customers burned down the gas to the regulator set point (200psi). The remaining gas was blown down to initiate repairs. Repairs started on 6/24/2024 (weld-on sleeve) and the pipeline was returned to service on 7/1/2024. Localized pitting was determined to be the cause in-between the concrete coatings near the seams where coal tar is the coating.

All rights reserved. Copyright © by ClearPHMSA