GTG incident on 2024-06-06 — TX

Operator
Enable Gas Transmission, Llc
Cause
Notification Issue
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$95,055
Incident datetime
2024-06-06 00:00 UTC
Report number
Location
TX
Narrative
On thursday, may 9th at approximately 1:25pm central time, emmet operations received a call from a third party about a possible line strike with a gas release. At 1:38pm, operations personnel confirmed that a third party had struck line sm-23 with a bulldozer causing a gas release. No one was injured and the gas did not ignite. An operations technician remained on site to monitor the release while one technician went to the upstream valve site and another technician mobilized to the downstream valve site. Pressure at the time of the strike was 550psig; pressure was lowered to 350psig and monitored. The decision to monitor pressure was made to avoid significant outages to residential customers. Once customer notifications were finalized, the pipeline was shunt in and blown down. A type b sleeve was installed over the defect and the pipeline was purged and returned to service on friday may 10th at approximately 4:40pm central time. The pipeline was struck by a third party logging company. The contractors working for the logging company did not complete a one call and were not authorized to perform work on the sm-23 right of way.
Detailed record list
Report Received Date
2024-06-06 00:00:00
Iyear
2024
Report Number
20240079
Supplemental Number
39651
Report Type
Original Final
Operator Id
Name
Enable Gas Transmission, Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Additional Nrc Report Numbers
1398644
Commodity Released Type
Natural Gas
Unintentional Release
13000
Intentional Release
1758
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Downstream Action Taken
Valve Closure
Num Pub Evacuated
0
On Off Shore
Onshore
Onshore State Abbreviation
Ar
Onshore Postal Code
71701
Onshore City Name
Not Within A Municipality
Onshore County Name
Ouachita
Designated Location
Not Applicable
Pipe Fac Name
Sm-23
Segment Name
Sm-23
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
20
Puddle Weld Ind
No
Pipe Wall Thickness
0.25
Pipe Smys
46000
Pipe Specification
Api 5l
Pipe Seam Type
Longitudinal Erw - Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Coating Applied Ind
No
Installation Year
1967
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
3.6
Puncture Circum
1.2
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
390
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
26390
Est Cost Intentional Release
3569
Est Cost Prop Damage
95055
Est Cost Emergency
20353
Est Cost Other
0
Gas Cost In Mcf
2.03
Prpty
145367
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
550
Gas Flow In Pipe In Mcf
10
Mop Psig
800
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1967-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
Yes
Gas Odorized Ind
Yes
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
32736
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No scada on this particular pipeline segment. Incident was called in by third party.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
State Law Exempt Ind
No
Notify Cga Dirt
Yes
Pipeline Easement Row Ind
Yes
Joint Trench Ind
No
Cross Bore Ind
No
Depth Of Grade
18� � 36�
Excavator Type
Contractor
Excavator Equipment
Bulldozer
Work Performed
Grading
One Call Notified Ind
No
Locator Type
Unknown/other
Visible Marks
No
Service Interruption
Yes
Service Interruption Hours
24
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
D***** A******
Preparer Title
Sr. Dot Specialist
Preparer Email
D*************@e*************.com
Preparer Telephone
501-351-8513
Local Contact Name
M*** G*****
Local Contact Email
M*************@e*************.com
Local Contact Telephone
870-703-0482
Authorizer Name
S**** S*****
Authorizer Title
Director Regulatory Compliance
Authorizer Telephone
405-557-5271
Authorizer Email
S***********@e*************.com
Narrative
On thursday, may 9th at approximately 1:25pm central time, emmet operations received a call from a third party about a possible line strike with a gas release. At 1:38pm, operations personnel confirmed that a third party had struck line sm-23 with a bulldozer causing a gas release. No one was injured and the gas did not ignite. An operations technician remained on site to monitor the release while one technician went to the upstream valve site and another technician mobilized to the downstream valve site. Pressure at the time of the strike was 550psig; pressure was lowered to 350psig and monitored. The decision to monitor pressure was made to avoid significant outages to residential customers. Once customer notifications were finalized, the pipeline was shunt in and blown down. A type b sleeve was installed over the defect and the pipeline was purged and returned to service on friday may 10th at approximately 4:40pm central time. The pipeline was struck by a third party logging company. The contractors working for the logging company did not complete a one call and were not authorized to perform work on the sm-23 right of way.
Report Received Date 2024-06-06 00:00:00
Iyear 2024
Report Number 20240079
Supplemental Number 39651
Report Type Original Final
Operator Id 602 PHMSA Enforcement
Name Enable Gas Transmission, Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 33.49613 Google Maps OpenStreetMap
Location Longitude -92.91935 Google Maps OpenStreetMap
Nrc Rpt Num 1398499 NRC Report How to search
Additional Nrc Report Numbers 1398644
Commodity Released Type Natural Gas
Unintentional Release 13000
Intentional Release 1758
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Valve Closure
Downstream Action Taken Valve Closure
Num Pub Evacuated 0
On Off Shore Onshore
Onshore State Abbreviation Ar
Onshore Postal Code 71701
Onshore City Name Not Within A Municipality
Onshore County Name Ouachita
Designated Location Not Applicable
Pipe Fac Name Sm-23
Segment Name Sm-23
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Other Underground Facilities No
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 20
Puddle Weld Ind No
Pipe Wall Thickness 0.25
Pipe Smys 46000
Pipe Specification Api 5l
Pipe Seam Type Longitudinal Erw - Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Coating Applied Ind No
Installation Year 1967
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 3.6
Puncture Circum 1.2
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 390
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 26390
Est Cost Intentional Release 3569
Est Cost Prop Damage 95055
Est Cost Emergency 20353
Est Cost Other 0
Gas Cost In Mcf 2.03
Prpty 145367
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 550
Gas Flow In Pipe In Mcf 10
Mop Psig 800
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1967-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind Yes
Gas Odorized Ind Yes
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 32736
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No scada on this particular pipeline segment. Incident was called in by third party.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
State Law Exempt Ind No
Notify Cga Dirt Yes
Pipeline Easement Row Ind Yes
Joint Trench Ind No
Cross Bore Ind No
Depth Of Grade 18� � 36�
Excavator Type Contractor
Excavator Equipment Bulldozer
Work Performed Grading
One Call Notified Ind No
Locator Type Unknown/other
Visible Marks No
Service Interruption Yes
Service Interruption Hours 24
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name D***** A******
Preparer Title Sr. Dot Specialist
Preparer Email D*************@e*************.com
Preparer Telephone 501-351-8513
Local Contact Name M*** G*****
Local Contact Email M*************@e*************.com
Local Contact Telephone 870-703-0482
Authorizer Name S**** S*****
Authorizer Title Director Regulatory Compliance
Authorizer Telephone 405-557-5271
Authorizer Email S***********@e*************.com
Narrative On thursday, may 9th at approximately 1:25pm central time, emmet operations received a call from a third party about a possible line strike with a gas release. At 1:38pm, operations personnel confirmed that a third party had struck line sm-23 with a bulldozer causing a gas release. No one was injured and the gas did not ignite. An operations technician remained on site to monitor the release while one technician went to the upstream valve site and another technician mobilized to the downstream valve site. Pressure at the time of the strike was 550psig; pressure was lowered to 350psig and monitored. The decision to monitor pressure was made to avoid significant outages to residential customers. Once customer notifications were finalized, the pipeline was shunt in and blown down. A type b sleeve was installed over the defect and the pipeline was purged and returned to service on friday may 10th at approximately 4:40pm central time. The pipeline was struck by a third party logging company. The contractors working for the logging company did not complete a one call and were not authorized to perform work on the sm-23 right of way.

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