Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2024-12-13 — TX
Operator
Coserv Gas, Ltd
Cause
Equipment Failure
Commodity
Other Gas
Program
GD
Damage and Injuries
1 fatality
0 injuries
Property damage (nominal)
$60,000
Incident datetime
2024-12-13 00:00 UTC
Report number
Location
TX, DENTON
Narrative
Coserv gas, ltd. Employees were performing a hot tap on an in-situ steel gas line at the above-described location of incident. They were using a mueller co. Manufactured hot tapping tool as a part of this work. The ratchet handle of the tool's mounted completion machine moved unexpectedly as a result of some yet-to-be-determined failure internal to the tool. A coserv gas, ltd. Employee was struck by the ratchet handle and suffered fatal injuries. There was no resulting gas leak.
Detailed record list
Report Received Date
2024-12-13 00:00:00
Iyear
2024.0
Report Number
20240070.0
Supplemental Number
41004.0
Report Type
Supplemental Final
Operator Id
31588
Name
Coserv Gas, Ltd
Operator Street Address
7701 South Stemmons
Operator City Name
Corinth
Operator State Abbreviation
TX
Operator Postal Code
76210.0
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
Cross Timbers Rd
Location City Name
Flower Mound
Location County Name
Denton
Location State Abbreviation
TX
Location Postal Code
75022.0
Location Latitude
33.04689
Location Longitude
-97.13293
Flow Cont Meter Reg Ind
Yes
Flow Cont Other Ind
Yes
Flow Cont Other Detail
Flow Shutoff Was Not Necessary, No Loss Of Gas At Time Of Incident.
Nrc Rpt Num
1416529.0
Additional Nrc Report Numbers
1416586.0
Commodity Released Type
Other Gas
Commodity Details
No Gas Release
Unintentional Release
0.0
Intentional Release
0.0
Fatality Ind
Yes
Num Emp Fatalities
1
Num Contr Fatalities
0
Num Er Fatalities
0
Num Worker Fatalities
0
Num Gp Fatalities
0
Fatal
1
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Aboveground
Incident Area Subtype
In Or Spanning An Open Ditch
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Other
System Part Details
Hot Tap Machine
Material Involved
Unknown
Release Type
Other
Release Type Details
No Release Of Gas At Time Of Incident.
Class Location Type
Class 1 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
60000.0
Est Cost Emergency
25820.0
Est Cost Other
0.0
Est Cost Other Details
2.b Operators Hot Tap Tooling Is Damaged; Repair Costs Are Estimated At 60,000
Gas Cost In Mcf
0.0
Est Cost Unintentional Release
0.0
Est Cost Intentional Release
0.0
Prpty
85820.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
0.0
Accident Psig
429.2
Normal Psig
429.2
Mop Psig
740.0
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2023-04-11 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Odorized By Others
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Accident had nothing to do with control room.
Employee Drug Test Ind
Yes
Num Employees Tested
9
Num Employees Failed
0
Contractor Drug Test Ind
Yes
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Eq Failure Details
Something Failed Internally, Analysis On Going.
Preparer Name
J*** S*******
Preparer Title
Compliance Manager
Preparer Email
J********@c*****.com
Preparer Telephone
3368488402
Authorizer Name
B** D******
Authorizer Title
Director Of Gas Operations
Authorizer Telephone
9037380983
Authorizer Email
B*******@c*****.com
Narrative
Coserv gas, ltd. Employees were performing a hot tap on an in-situ steel gas line at the above-described location of incident. They were using a mueller co. Manufactured hot tapping tool as a part of this work. The ratchet handle of the tool's mounted completion machine moved unexpectedly as a result of some yet-to-be-determined failure internal to the tool. A coserv gas, ltd. Employee was struck by the ratchet handle and suffered fatal injuries. There was no resulting gas leak.
Report Received Date | 2024-12-13 00:00:00 |
---|---|
Iyear | 2024.0 |
Report Number | 20240070.0 |
Supplemental Number | 41004.0 |
Report Type | Supplemental Final |
Operator Id | 31588 PHMSA Enforcement |
Name | Coserv Gas, Ltd |
Operator Street Address | 7701 South Stemmons |
Operator City Name | Corinth |
Operator State Abbreviation | TX |
Operator Postal Code | 76210.0 |
Time Zone | Central |
Daylight Savings Ind | Yes |
Location Street Address | Cross Timbers Rd |
Location City Name | Flower Mound |
Location County Name | Denton |
Location State Abbreviation | TX |
Location Postal Code | 75022.0 |
Location Latitude | 33.04689 Google Maps OpenStreetMap |
Location Longitude | -97.13293 Google Maps OpenStreetMap |
Flow Cont Meter Reg Ind | Yes |
Flow Cont Other Ind | Yes |
Flow Cont Other Detail | Flow Shutoff Was Not Necessary, No Loss Of Gas At Time Of Incident. |
Nrc Rpt Num | 1416529.0 NRC Report How to search |
Additional Nrc Report Numbers | 1416586.0 |
Commodity Released Type | Other Gas |
Commodity Details | No Gas Release |
Unintentional Release | 0.0 |
Intentional Release | 0.0 |
Fatality Ind | Yes |
Num Emp Fatalities | 1 |
Num Contr Fatalities | 0 |
Num Er Fatalities | 0 |
Num Worker Fatalities | 0 |
Num Gp Fatalities | 0 |
Fatal | 1 |
Injury Ind | No |
Injure | 0 |
Ignite Ind | No |
Num Pub Evacuated | 0.0 |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Federal | No |
Location Type | Utility Right-Of-Way / Easement |
Incident Area Type | Aboveground |
Incident Area Subtype | In Or Spanning An Open Ditch |
Crossing | No |
Pipe Facility Type | Privately Owned |
System Part Involved | Other |
System Part Details | Hot Tap Machine |
Material Involved | Unknown |
Release Type | Other |
Release Type Details | No Release Of Gas At Time Of Incident. |
Class Location Type | Class 1 Location |
Est Cost Oper Paid | 0.0 |
Est Cost Prop Damage | 60000.0 |
Est Cost Emergency | 25820.0 |
Est Cost Other | 0.0 |
Est Cost Other Details | 2.b Operators Hot Tap Tooling Is Damaged; Repair Costs Are Estimated At 60,000 |
Gas Cost In Mcf | 0.0 |
Est Cost Unintentional Release | 0.0 |
Est Cost Intentional Release | 0.0 |
Prpty | 85820.0 |
Commercial Affected | 0.0 |
Industrial Affected | 0.0 |
Residences Affected | 0.0 |
Num Persons Hosp Not Ovnght | 0.0 |
Num Injured Treated By Emt | 0.0 |
Num Resident Building Affctd | 0.0 |
Num Business Building Affctd | 0.0 |
Accident Psig | 429.2 |
Normal Psig | 429.2 |
Mop Psig | 740.0 |
Mop Cfr Section | 192.619(A)(1) View CFR 49 §192 |
Maop Established Date | 2023-04-11 00:00:00 |
Accident Pressure | Pressure Did Not Exceed Maop |
Gas Odorized System Type | Odorized By Others |
Gas Odorized Lvl Not Msrd Ind | Yes |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Accident had nothing to do with control room. |
Employee Drug Test Ind | Yes |
Num Employees Tested | 9 |
Num Employees Failed | 0 |
Contractor Drug Test Ind | Yes |
Num Contractors Tested | 1 |
Num Contractors Failed | 0 |
Cause | Equipment Failure |
Cause Details | Other Equipment Failure |
Eq Failure Type | Other Equipment Failure |
Eq Failure Details | Something Failed Internally, Analysis On Going. |
Preparer Name | J*** S******* |
Preparer Title | Compliance Manager |
Preparer Email | J********@c*****.com |
Preparer Telephone | 3368488402 |
Authorizer Name | B** D****** |
Authorizer Title | Director Of Gas Operations |
Authorizer Telephone | 9037380983 |
Authorizer Email | B*******@c*****.com |
Narrative | Coserv gas, ltd. Employees were performing a hot tap on an in-situ steel gas line at the above-described location of incident. They were using a mueller co. Manufactured hot tapping tool as a part of this work. The ratchet handle of the tool's mounted completion machine moved unexpectedly as a result of some yet-to-be-determined failure internal to the tool. A coserv gas, ltd. Employee was struck by the ratchet handle and suffered fatal injuries. There was no resulting gas leak. |
External Resources
PHMSA pipeline safety insights.
Product
Features
Company
All rights reserved. Copyright © by ClearPHMSA