Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-12-29 — TX
Operator
Plains Pipeline, L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$250
Incident datetime
2023-12-29 00:00 UTC
Report number
Location
TX
Narrative
Approximately three barrels of crude oil were released from the gardendale to three rivers loop line 20inch coupon at three rivers terminal. The date and time of the release (part a q4) is indicative of the earliest possible time the release could have started based on pressure trends. The cause of the release is attributed to incorrect operation as a result of improper installation of the coupon plug. To prevent future incidents, plains suspended the oq qualification of the third-party individual that performed the installation, and new fittings and plug for the coupon were installed.
Detailed record list
Report Received Date
2023-12-29 00:00:00
Iyear
2023
Report Number
20230310
Supplemental Number
39027
Report Type
Original Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
28.46192043
Location Longitude
-98.22423601
Commodity Released Type
Crude Oil
Unintentional Release Bbls
3
Recovered Bbls
3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Not Shutdown; Isolated The Coupon Only.
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Type Ind
Manual
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
No Action Needed; Isolation Occurred From A Valve Associated With The Coupon.
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Three Rivers Terminal
Segment Name
Gardendale To Three Rivers Loop Line 20in Coupon
Onshore State Abbreviation
Tx
Onshore Postal Code
78071
Onshore City Name
Three Rivers
Onshore County Name
Live Oak
Designated Location
Milepost
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Coupon Plug
Installation Year
2023
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
225
Est Cost Prop Damage
250
Est Cost Emergency
15000
Est Cost Environmental
0
Est Cost Other
0
Prpty
15475
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
898
Mop Psig
1440
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2016-05-26 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was below detectable limits.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
N****** A G*******
Preparer Title
Hse Regulatory Compliance Supervisor
Preparer Email
N***************@p*****.com
Preparer Telephone
7136464376
Prepared Date
2023-12-29 00:00:00
Local Contact Name
N****** A G*******
Local Contact Email
N***************@p*****.com
Local Contact Telephone
7136464376
Authorizer Name
S***** A*****
Authorizer Telephone
713-993-5676
Authorizer Title
Senior Manager Hse-Integrity-And-Phmsa
Authorizer Email
S************@p*****.com
Narrative
Approximately three barrels of crude oil were released from the gardendale to three rivers loop line 20inch coupon at three rivers terminal. The date and time of the release (part a q4) is indicative of the earliest possible time the release could have started based on pressure trends. The cause of the release is attributed to incorrect operation as a result of improper installation of the coupon plug. To prevent future incidents, plains suspended the oq qualification of the third-party individual that performed the installation, and new fittings and plug for the coupon were installed.
Report Received Date | 2023-12-29 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230310 |
Supplemental Number | 39027 |
Report Type | Original Final |
Operator Id | 300 PHMSA Enforcement |
Name | Plains Pipeline, L.p. |
Operator Street Address | 333 Clay Street, Suite 1900 |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Central |
Daylight Savings Ind | No |
Location Latitude | 28.46192043 Google Maps OpenStreetMap |
Location Longitude | -98.22423601 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 3 |
Recovered Bbls | 3 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Pipeline, Including Valve Sites |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | No |
Shutdown Explain | Pipeline Was Not Shutdown; Isolated The Coupon Only. |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
Ignite Ind | No |
Upstream Action Taken | Valve Closure |
Upstream Valve Type Ind | Manual |
Downstream Action Taken | Operational Control |
Downstream Oprtnl Cntrl Detail | No Action Needed; Isolation Occurred From A Valve Associated With The Coupon. |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Three Rivers Terminal |
Segment Name | Gardendale To Three Rivers Loop Line 20in Coupon |
Onshore State Abbreviation | Tx |
Onshore Postal Code | 78071 |
Onshore City Name | Three Rivers |
Onshore County Name | Live Oak |
Designated Location | Milepost |
Designated Name | 0+00 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Intrastate |
Item Involved | Other |
Item Involved Details | Coupon Plug |
Installation Year | 2023 |
Manufactured Year | Unknown |
Material Involved | Material Other Than Carbon Steel |
Material Details | Stainless Steel |
Release Type | Leak |
Leak Type | Connection Failure |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 225 |
Est Cost Prop Damage | 250 |
Est Cost Emergency | 15000 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 15475 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 898 |
Mop Psig | 1440 |
Mop Cfr Section | Component Design Pressure �195.406(A)(2) View CFR 49 §192 |
Maop Established Date | 2016-05-26 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Internal Inspection Ind | Yes |
Operation Complications Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | Yes |
Cpm Operating Ind | Yes |
Cpm Functional Ind | Yes |
Cpm Detection Ind | No |
Cpm Conf Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | The release was below detectable limits. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Incorrect Operation |
Cause Details | Equipment Not Installed Properly |
Operation Type | Equipment Not Installed Properly |
Related Failure Follow Ind | Yes |
Category Type | Routine Maintenance |
Operator Qualification Ind | Yes |
Qualified Individuals | Yes, They Were Qualified For The Task(S) |
Preparer Name | N****** A G******* |
Preparer Title | Hse Regulatory Compliance Supervisor |
Preparer Email | N***************@p*****.com |
Preparer Telephone | 7136464376 |
Prepared Date | 2023-12-29 00:00:00 |
Local Contact Name | N****** A G******* |
Local Contact Email | N***************@p*****.com |
Local Contact Telephone | 7136464376 |
Authorizer Name | S***** A***** |
Authorizer Telephone | 713-993-5676 |
Authorizer Title | Senior Manager Hse-Integrity-And-Phmsa |
Authorizer Email | S************@p*****.com |
Narrative | Approximately three barrels of crude oil were released from the gardendale to three rivers loop line 20inch coupon at three rivers terminal. The date and time of the release (part a q4) is indicative of the earliest possible time the release could have started based on pressure trends. The cause of the release is attributed to incorrect operation as a result of improper installation of the coupon plug. To prevent future incidents, plains suspended the oq qualification of the third-party individual that performed the installation, and new fittings and plug for the coupon were installed. |
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