HL incident on 2023-12-21 — TX

Operator
Energy Transfer Company
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2023-12-21 00:00 UTC
Report number
Location
TX
Narrative
On 12/01/2023 at 15:00, a local operator was performing a routine monthly tank inspection on tank 2725 at the corsicana tank farm and observed a small oil residue around the roof drain discharge valve and product on the ground where the drain valve discharges from the tank. Approximately, 30 gallons of crude oil was released on the ground. Free product was recovered with a vacuum truck. Contaminated soil was removed for onsite remediation. Supplemental: the failure was determined to have been caused by a failure of the external floating roof tank drain hose which is utilized to drain water from the roof. The hose is comprised of an external thermoplastic sheath extruded over a spiral wound stainless steel internal carcass. The analysis determined the hose had experienced mechanical damage suspected to have occurred due to a missing guard on a tank leg. The contact abraded the external surface, and eventually punctured the thermoplastic sheath. The hose has been replaced with a new design and the tank leg guards have been inspected to prevent reoccurrence
Detailed record list
Report Received Date
2023-12-21 00:00:00
Iyear
2023
Report Number
20230306
Supplemental Number
40180
Report Type
Supplemental Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.7
Recovered Bbls
0.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Tank 2725 Was Isolated.
Communication State Fed Ind
No
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Corsicana Tank Farm
Segment Name
Corsicana Tank 2725
Onshore State Abbreviation
Tx
Onshore Postal Code
75110
Onshore City Name
Corsicana
Onshore County Name
Navarro
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Roof Drain System
Tank Type
Atmospheric
Safe Fill Level
56
Safe Fill Level Exceeded Ind
No
Api Std Out Of Service Year
2019
Api Std In Service Year
2019
Installation Year
2019
Manufactured Year
2019
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Puncture
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
21
Est Cost Prop Damage
1500
Est Cost Emergency
1500
Est Cost Environmental
5000
Est Cost Other
0
Prpty
8021
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
15
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
External Floating Roof Tank Drain Hose
Additional Installation Ind
Yes
Additional Erosion Wear Ind
Yes
Preparer Name
T*** N*******
Preparer Title
Director - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2024-10-30 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 12/01/2023 at 15:00, a local operator was performing a routine monthly tank inspection on tank 2725 at the corsicana tank farm and observed a small oil residue around the roof drain discharge valve and product on the ground where the drain valve discharges from the tank. Approximately, 30 gallons of crude oil was released on the ground. Free product was recovered with a vacuum truck. Contaminated soil was removed for onsite remediation. Supplemental: the failure was determined to have been caused by a failure of the external floating roof tank drain hose which is utilized to drain water from the roof. The hose is comprised of an external thermoplastic sheath extruded over a spiral wound stainless steel internal carcass. The analysis determined the hose had experienced mechanical damage suspected to have occurred due to a missing guard on a tank leg. The contact abraded the external surface, and eventually punctured the thermoplastic sheath. The hose has been replaced with a new design and the tank leg guards have been inspected to prevent reoccurrence
Report Received Date 2023-12-21 00:00:00
Iyear 2023
Report Number 20230306
Supplemental Number 40180
Report Type Supplemental Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Time Zone Central
Daylight Savings Ind No
Location Latitude 32.067561 Google Maps OpenStreetMap
Location Longitude -96.478837 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.7
Recovered Bbls 0.7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Tank 2725 Was Isolated.
Communication State Fed Ind No
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Corsicana Tank Farm
Segment Name Corsicana Tank 2725
Onshore State Abbreviation Tx
Onshore Postal Code 75110
Onshore City Name Corsicana
Onshore County Name Navarro
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Roof Drain System
Tank Type Atmospheric
Safe Fill Level 56
Safe Fill Level Exceeded Ind No
Api Std Out Of Service Year 2019
Api Std In Service Year 2019
Installation Year 2019
Manufactured Year 2019
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Puncture
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 21
Est Cost Prop Damage 1500
Est Cost Emergency 1500
Est Cost Environmental 5000
Est Cost Other 0
Prpty 8021
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 15
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details External Floating Roof Tank Drain Hose
Additional Installation Ind Yes
Additional Erosion Wear Ind Yes
Preparer Name T*** N*******
Preparer Title Director - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Prepared Date 2024-10-30 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Director - Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 12/01/2023 at 15:00, a local operator was performing a routine monthly tank inspection on tank 2725 at the corsicana tank farm and observed a small oil residue around the roof drain discharge valve and product on the ground where the drain valve discharges from the tank. Approximately, 30 gallons of crude oil was released on the ground. Free product was recovered with a vacuum truck. Contaminated soil was removed for onsite remediation. Supplemental: the failure was determined to have been caused by a failure of the external floating roof tank drain hose which is utilized to drain water from the roof. The hose is comprised of an external thermoplastic sheath extruded over a spiral wound stainless steel internal carcass. The analysis determined the hose had experienced mechanical damage suspected to have occurred due to a missing guard on a tank leg. The contact abraded the external surface, and eventually punctured the thermoplastic sheath. The hose has been replaced with a new design and the tank leg guards have been inspected to prevent reoccurrence

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