Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-12-08 — WY
Operator
Bridger Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2023-12-08 00:00 UTC
Report number
Location
WY
Narrative
On the morning of november 9th, an operator employee was preparing the 12-inch four bears south receiver for an incoming routine cleaning pig. The employee was in contact with the casper control center and asked the controller to operate a mov on the receiver barrel. As the employee monitored activity on the four bears south receiver, the controller asked if the employee wanted to prepare the adjacent 12-inch four bears north receiver for a separate incoming cleaning pig. The onsite employee agreed to proceed with those preparations, and completed checking on four bears south receiver, while the controller sent the command to operate the mov on four bears north receiver. The onsite employee walked 30 feet to four bears north receiver to monitor activity and found oil flowing from the sump connected to it. This employee quickly identified that a 2-inch manual drain valve had been left in the open position, which allowed the sump to overfill and release approximately 55 barrels of crude oil into the containment area. The employee closed the 2-inch valve and immediately initiated a cleanup response. The employee notified his supervisor of the release, who subsequently notified operations management. Hydrovac crews were called to the site and were able to remove approximately 45 barrels of free product, which was injected back into the system. The contaminated soil was removed and is being managed as required by nd deq. No water or wildlife was impacted by this release.
Detailed record list
Report Received Date
2023-12-08 00:00:00
Iyear
2023
Report Number
20230291
Supplemental Number
39380
Report Type
Supplemental Final
Operator Id
31878
Name
Bridger Pipeline Llc
Operator Street Address
455 N. Poplar St.
Operator City Name
Casper
Operator State Abbreviation
WY
Operator Postal Code
82602
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
47.80189
Location Longitude
-102.8909
Commodity Released Type
Crude Oil
Unintentional Release Bbls
55
Recovered Bbls
45
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Rapid Onsite Response Did Not Require Line Shut Down
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
1384461
Additional Nrc Report Numbers
1385212
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Johnson's Corner Terminal
Segment Name
Four Bears At Johnson's Corner
Onshore State Abbreviation
Nd
Onshore Postal Code
58847
Onshore City Name
Not Within A Municipality
Onshore County Name
Mckenzie County
Designated Location
Survey Station No.
Designated Name
713+20
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
2023
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
750
Est Cost Prop Damage
0
Est Cost Emergency
38412
Est Cost Environmental
0
Est Cost Other
0
Prpty
39162
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
150
Mop Psig
1440
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2023-06-14 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Immediate onsite response to the release identified that it was caused by field operator error, and controller actions were not a contributing factor to the incident.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
K**** P***
Preparer Title
Pipeline Compliance Coordinator
Preparer Email
K*********@t******.com
Preparer Telephone
4069393133
Prepared Date
2024-03-28 00:00:00
Authorizer Name
K** D*********
Authorizer Telephone
13072660275
Authorizer Title
Director Of Government And Control Center
Authorizer Email
K*************@t******.com
Narrative
On the morning of november 9th, an operator employee was preparing the 12-inch four bears south receiver for an incoming routine cleaning pig. The employee was in contact with the casper control center and asked the controller to operate a mov on the receiver barrel. As the employee monitored activity on the four bears south receiver, the controller asked if the employee wanted to prepare the adjacent 12-inch four bears north receiver for a separate incoming cleaning pig. The onsite employee agreed to proceed with those preparations, and completed checking on four bears south receiver, while the controller sent the command to operate the mov on four bears north receiver. The onsite employee walked 30 feet to four bears north receiver to monitor activity and found oil flowing from the sump connected to it. This employee quickly identified that a 2-inch manual drain valve had been left in the open position, which allowed the sump to overfill and release approximately 55 barrels of crude oil into the containment area. The employee closed the 2-inch valve and immediately initiated a cleanup response. The employee notified his supervisor of the release, who subsequently notified operations management. Hydrovac crews were called to the site and were able to remove approximately 45 barrels of free product, which was injected back into the system. The contaminated soil was removed and is being managed as required by nd deq. No water or wildlife was impacted by this release.
Report Received Date | 2023-12-08 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230291 |
Supplemental Number | 39380 |
Report Type | Supplemental Final |
Operator Id | 31878 PHMSA Enforcement |
Name | Bridger Pipeline Llc |
Operator Street Address | 455 N. Poplar St. |
Operator City Name | Casper |
Operator State Abbreviation | WY |
Operator Postal Code | 82602 |
Time Zone | Central |
Daylight Savings Ind | No |
Location Latitude | 47.80189 Google Maps OpenStreetMap |
Location Longitude | -102.8909 Google Maps OpenStreetMap |
Commodity Released Type | Crude Oil |
Unintentional Release Bbls | 55 |
Recovered Bbls | 45 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | No |
Shutdown Explain | Rapid Onsite Response Did Not Require Line Shut Down |
Communication State Fed Ind | Yes |
Party Initiated Communication | Operator |
Nrc Rpt Num | 1384461 NRC Report How to search |
Additional Nrc Report Numbers | 1385212 |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | No |
Num Pub Evacuated | 0 |
Pipe Fac Name | Johnson's Corner Terminal |
Segment Name | Four Bears At Johnson's Corner |
Onshore State Abbreviation | Nd |
Onshore Postal Code | 58847 |
Onshore City Name | Not Within A Municipality |
Onshore County Name | Mckenzie County |
Designated Location | Survey Station No. |
Designated Name | 713+20 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Aboveground |
Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Sump |
Installation Year | 2023 |
Manufactured Year | Unknown |
Material Involved | Carbon Steel |
Release Type | Overfill Or Overflow |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | No |
Water Contam Ind | No |
Could Be Hca | No |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 750 |
Est Cost Prop Damage | 0 |
Est Cost Emergency | 38412 |
Est Cost Environmental | 0 |
Est Cost Other | 0 |
Prpty | 39162 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 150 |
Mop Psig | 1440 |
Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
Maop Established Date | 2023-06-14 00:00:00 |
Maop Reversal Flow Ind | No |
Accident Pressure | Pressure Did Not Exceed Mop |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | Immediate onsite response to the release identified that it was caused by field operator error, and controller actions were not a contributing factor to the incident. |
Employee Drug Test Ind | Yes |
Contractor Drug Test Ind | No |
Num Employees Tested | 1 |
Num Employees Failed | 0 |
Cause | Incorrect Operation |
Cause Details | Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow |
Operation Type | Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow |
Overflow Other Ind | Valve Misalignment |
Related Failure Follow Ind | Yes |
Category Type | Routine Maintenance |
Operator Qualification Ind | Yes |
Qualified Individuals | Yes, They Were Qualified For The Task(S) |
Preparer Name | K**** P*** |
Preparer Title | Pipeline Compliance Coordinator |
Preparer Email | K*********@t******.com |
Preparer Telephone | 4069393133 |
Prepared Date | 2024-03-28 00:00:00 |
Authorizer Name | K** D********* |
Authorizer Telephone | 13072660275 |
Authorizer Title | Director Of Government And Control Center |
Authorizer Email | K*************@t******.com |
Narrative | On the morning of november 9th, an operator employee was preparing the 12-inch four bears south receiver for an incoming routine cleaning pig. The employee was in contact with the casper control center and asked the controller to operate a mov on the receiver barrel. As the employee monitored activity on the four bears south receiver, the controller asked if the employee wanted to prepare the adjacent 12-inch four bears north receiver for a separate incoming cleaning pig. The onsite employee agreed to proceed with those preparations, and completed checking on four bears south receiver, while the controller sent the command to operate the mov on four bears north receiver. The onsite employee walked 30 feet to four bears north receiver to monitor activity and found oil flowing from the sump connected to it. This employee quickly identified that a 2-inch manual drain valve had been left in the open position, which allowed the sump to overfill and release approximately 55 barrels of crude oil into the containment area. The employee closed the 2-inch valve and immediately initiated a cleanup response. The employee notified his supervisor of the release, who subsequently notified operations management. Hydrovac crews were called to the site and were able to remove approximately 45 barrels of free product, which was injected back into the system. The contaminated soil was removed and is being managed as required by nd deq. No water or wildlife was impacted by this release. |
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