HL incident on 2023-12-08 — WY

Operator
Bridger Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2023-12-08 00:00 UTC
Report number
Location
WY
Narrative
On the morning of november 9th, an operator employee was preparing the 12-inch four bears south receiver for an incoming routine cleaning pig. The employee was in contact with the casper control center and asked the controller to operate a mov on the receiver barrel. As the employee monitored activity on the four bears south receiver, the controller asked if the employee wanted to prepare the adjacent 12-inch four bears north receiver for a separate incoming cleaning pig. The onsite employee agreed to proceed with those preparations, and completed checking on four bears south receiver, while the controller sent the command to operate the mov on four bears north receiver. The onsite employee walked 30 feet to four bears north receiver to monitor activity and found oil flowing from the sump connected to it. This employee quickly identified that a 2-inch manual drain valve had been left in the open position, which allowed the sump to overfill and release approximately 55 barrels of crude oil into the containment area. The employee closed the 2-inch valve and immediately initiated a cleanup response. The employee notified his supervisor of the release, who subsequently notified operations management. Hydrovac crews were called to the site and were able to remove approximately 45 barrels of free product, which was injected back into the system. The contaminated soil was removed and is being managed as required by nd deq. No water or wildlife was impacted by this release.
Detailed record list
Report Received Date
2023-12-08 00:00:00
Iyear
2023
Report Number
20230291
Supplemental Number
39380
Report Type
Supplemental Final
Operator Id
Name
Bridger Pipeline Llc
Operator Street Address
455 N. Poplar St.
Operator City Name
Casper
Operator State Abbreviation
WY
Operator Postal Code
82602
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
55
Recovered Bbls
45
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Rapid Onsite Response Did Not Require Line Shut Down
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Nrc Rpt Num
Additional Nrc Report Numbers
1385212
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Johnson's Corner Terminal
Segment Name
Four Bears At Johnson's Corner
Onshore State Abbreviation
Nd
Onshore Postal Code
58847
Onshore City Name
Not Within A Municipality
Onshore County Name
Mckenzie County
Designated Location
Survey Station No.
Designated Name
713+20
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
2023
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
750
Est Cost Prop Damage
0
Est Cost Emergency
38412
Est Cost Environmental
0
Est Cost Other
0
Prpty
39162
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
150
Mop Psig
1440
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2023-06-14 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Immediate onsite response to the release identified that it was caused by field operator error, and controller actions were not a contributing factor to the incident.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
K**** P***
Preparer Title
Pipeline Compliance Coordinator
Preparer Email
K*********@t******.com
Preparer Telephone
4069393133
Prepared Date
2024-03-28 00:00:00
Authorizer Name
K** D*********
Authorizer Telephone
13072660275
Authorizer Title
Director Of Government And Control Center
Authorizer Email
K*************@t******.com
Narrative
On the morning of november 9th, an operator employee was preparing the 12-inch four bears south receiver for an incoming routine cleaning pig. The employee was in contact with the casper control center and asked the controller to operate a mov on the receiver barrel. As the employee monitored activity on the four bears south receiver, the controller asked if the employee wanted to prepare the adjacent 12-inch four bears north receiver for a separate incoming cleaning pig. The onsite employee agreed to proceed with those preparations, and completed checking on four bears south receiver, while the controller sent the command to operate the mov on four bears north receiver. The onsite employee walked 30 feet to four bears north receiver to monitor activity and found oil flowing from the sump connected to it. This employee quickly identified that a 2-inch manual drain valve had been left in the open position, which allowed the sump to overfill and release approximately 55 barrels of crude oil into the containment area. The employee closed the 2-inch valve and immediately initiated a cleanup response. The employee notified his supervisor of the release, who subsequently notified operations management. Hydrovac crews were called to the site and were able to remove approximately 45 barrels of free product, which was injected back into the system. The contaminated soil was removed and is being managed as required by nd deq. No water or wildlife was impacted by this release.
Report Received Date 2023-12-08 00:00:00
Iyear 2023
Report Number 20230291
Supplemental Number 39380
Report Type Supplemental Final
Operator Id 31878 PHMSA Enforcement
Name Bridger Pipeline Llc
Operator Street Address 455 N. Poplar St.
Operator City Name Casper
Operator State Abbreviation WY
Operator Postal Code 82602
Time Zone Central
Daylight Savings Ind No
Location Latitude 47.80189 Google Maps OpenStreetMap
Location Longitude -102.8909 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 55
Recovered Bbls 45
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Rapid Onsite Response Did Not Require Line Shut Down
Communication State Fed Ind Yes
Party Initiated Communication Operator
Nrc Rpt Num 1384461 NRC Report How to search
Additional Nrc Report Numbers 1385212
Ignite Ind No
Notify Qualified Indiv Ind Yes
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Johnson's Corner Terminal
Segment Name Four Bears At Johnson's Corner
Onshore State Abbreviation Nd
Onshore Postal Code 58847
Onshore City Name Not Within A Municipality
Onshore County Name Mckenzie County
Designated Location Survey Station No.
Designated Name 713+20
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Sump
Installation Year 2023
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 750
Est Cost Prop Damage 0
Est Cost Emergency 38412
Est Cost Environmental 0
Est Cost Other 0
Prpty 39162
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 150
Mop Psig 1440
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2023-06-14 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Immediate onsite response to the release identified that it was caused by field operator error, and controller actions were not a contributing factor to the incident.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Valve Misalignment
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name K**** P***
Preparer Title Pipeline Compliance Coordinator
Preparer Email K*********@t******.com
Preparer Telephone 4069393133
Prepared Date 2024-03-28 00:00:00
Authorizer Name K** D*********
Authorizer Telephone 13072660275
Authorizer Title Director Of Government And Control Center
Authorizer Email K*************@t******.com
Narrative On the morning of november 9th, an operator employee was preparing the 12-inch four bears south receiver for an incoming routine cleaning pig. The employee was in contact with the casper control center and asked the controller to operate a mov on the receiver barrel. As the employee monitored activity on the four bears south receiver, the controller asked if the employee wanted to prepare the adjacent 12-inch four bears north receiver for a separate incoming cleaning pig. The onsite employee agreed to proceed with those preparations, and completed checking on four bears south receiver, while the controller sent the command to operate the mov on four bears north receiver. The onsite employee walked 30 feet to four bears north receiver to monitor activity and found oil flowing from the sump connected to it. This employee quickly identified that a 2-inch manual drain valve had been left in the open position, which allowed the sump to overfill and release approximately 55 barrels of crude oil into the containment area. The employee closed the 2-inch valve and immediately initiated a cleanup response. The employee notified his supervisor of the release, who subsequently notified operations management. Hydrovac crews were called to the site and were able to remove approximately 45 barrels of free product, which was injected back into the system. The contaminated soil was removed and is being managed as required by nd deq. No water or wildlife was impacted by this release.

All rights reserved. Copyright © by ClearPHMSA