Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2023-12-04 — TX
Operator
Products (Se) Pipe Line Corporation
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$447,000
Incident datetime
2023-12-04 00:00 UTC
Report number
Location
TX
Narrative
At 11:30 on 11/17/23, a leak from greensboro station tank 145 was discovered by local operations personnel. The leak originated from under the tank. By 12:00, the release was confirmed to meet nrc reportability requirements. The nrc was called at 12:15, and the initial nrc report was completed by 12:41 under nrc report #1384562. The PHMSA 48-hour update was made to the nrc at 13:32 on 11/18/2023 under nrc report #1384637. At 13:05, local operations began transferring the product into another tank onsite. An osro was activated and arrived onsite at 15:00 on 11/17/2023 and began gravel remediation. By 11:30 on 11/18/2023, tank 145 was emptied, and the flow of product has stopped. Contractors removed contaminated gravel and dug a trench against the ring wall. The area was surrounded by hay bales and absorbent boom. On 11/19/2023, tank 145 was cleaned and degassed. During an initial internal investigation of the tank on 11/20/2023, a 24-inch crack was found on the bottom plate of the tank floor near the area of release. Tank 145 remains out of service pending repair and internal coating. The cause of the release is under investigation. 1/30/2024 update: kinder morgan has elected to replace the floor of tank 145. The estimated cost of repairs has been updated to include the floor replacement and coating. 4/23/2024 update: kinder morgan completed repairs of tank 145, and the tank was returned to service on april 17, 2024. The cause of the release was determined to be a crack that resulted from combination of external corrosion on the soil-side of the tank bottom and flexing of the tank bottom during filling and emptying.
Detailed record list
Report Received Date
2023-12-04 00:00:00
Iyear
2023
Report Number
20230289
Supplemental Number
39547
Report Type
Supplemental Final
Operator Id
15674
Name
Products (Se) Pipe Line Corporation
Operator Street Address
1001 Louisiana St Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Time Zone
Eastern
Daylight Savings Ind
No
Location Latitude
36.075116
Location Longitude
-79.925256
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
5.36
Recovered Bbls
5.36
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Communication State Fed Ind
No
Nrc Rpt Num
1384562
Additional Nrc Report Numbers
1384637
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Oil Spill Removal Org Ind
Yes
Osro Arrived On Site Dt
11/17/2023 15:00
Num Pub Evacuated
0
Pipe Fac Name
Greensboro Station
Segment Name
Tank 145
Onshore State Abbreviation
Nc
Onshore Postal Code
27409
Onshore City Name
Greensboro
Onshore County Name
Guilford
Designated Location
Milepost
Designated Name
359
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Single Bottom System
Tank Type
Atmospheric
Safe Fill Level
42.7
Safe Fill Level Exceeded Ind
No
Api Std Out Of Service Year
2016
Api Std In Service Year
2021
Installation Year
1972
Manufactured Year
1972
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
900
Est Cost Prop Damage
447000
Est Cost Emergency
87933
Est Cost Environmental
50000
Est Cost Other
0
Prpty
585833
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
13
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release resulted from a crack in the tank floor. The controller's actions did not contribute to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
General Corrosion
Other Corrosion Ind
Yes
Corrosion Type Details
Soil-Side Corrosion Of Tank Bottom
Field Exam Basis Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1996
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2023
Prior Damage
N/a Bare/ineffectively Coated Pipe
Preparer Name
M****** P****
Preparer Title
Manager - Codes And Standards
Preparer Email
M************@k***********.com
Preparer Telephone
2052130226
Prepared Date
2024-05-14 00:00:00
Local Contact Name
J**** S*****
Local Contact Email
J***********@k***********.com
Local Contact Telephone
3365473661
Authorizer Name
Z*** R*****
Authorizer Telephone
7134202609
Authorizer Title
Director - Codes And Standards
Authorizer Email
Z**********@k***********.com
Narrative
At 11:30 on 11/17/23, a leak from greensboro station tank 145 was discovered by local operations personnel. The leak originated from under the tank. By 12:00, the release was confirmed to meet nrc reportability requirements. The nrc was called at 12:15, and the initial nrc report was completed by 12:41 under nrc report #1384562. The PHMSA 48-hour update was made to the nrc at 13:32 on 11/18/2023 under nrc report #1384637. At 13:05, local operations began transferring the product into another tank onsite. An osro was activated and arrived onsite at 15:00 on 11/17/2023 and began gravel remediation. By 11:30 on 11/18/2023, tank 145 was emptied, and the flow of product has stopped. Contractors removed contaminated gravel and dug a trench against the ring wall. The area was surrounded by hay bales and absorbent boom. On 11/19/2023, tank 145 was cleaned and degassed. During an initial internal investigation of the tank on 11/20/2023, a 24-inch crack was found on the bottom plate of the tank floor near the area of release. Tank 145 remains out of service pending repair and internal coating. The cause of the release is under investigation. 1/30/2024 update: kinder morgan has elected to replace the floor of tank 145. The estimated cost of repairs has been updated to include the floor replacement and coating. 4/23/2024 update: kinder morgan completed repairs of tank 145, and the tank was returned to service on april 17, 2024. The cause of the release was determined to be a crack that resulted from combination of external corrosion on the soil-side of the tank bottom and flexing of the tank bottom during filling and emptying.
Report Received Date | 2023-12-04 00:00:00 |
---|---|
Iyear | 2023 |
Report Number | 20230289 |
Supplemental Number | 39547 |
Report Type | Supplemental Final |
Operator Id | 15674 PHMSA Enforcement |
Name | Products (Se) Pipe Line Corporation |
Operator Street Address | 1001 Louisiana St Suite 1000 |
Operator City Name | Houston |
Operator State Abbreviation | TX |
Operator Postal Code | 77002 |
Time Zone | Eastern |
Daylight Savings Ind | No |
Location Latitude | 36.075116 Google Maps OpenStreetMap |
Location Longitude | -79.925256 Google Maps OpenStreetMap |
Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
Commodity Subtype | Gasoline (Non-Ethanol) |
Unintentional Release Bbls | 5.36 |
Recovered Bbls | 5.36 |
Fatality Ind | No |
Fatal | 0 |
Injury Ind | No |
Injure | 0 |
Accident Identifier | Local Operating Personnel, Including Contractors |
Operator Type | Operator Employee |
System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
On Off Shore | Onshore |
Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
Shutdown Due Accident Ind | Yes |
Communication State Fed Ind | No |
Nrc Rpt Num | 1384562 NRC Report How to search |
Additional Nrc Report Numbers | 1384637 |
Ignite Ind | No |
Notify Qualified Indiv Ind | Yes |
Oil Spill Removal Org Ind | Yes |
Osro Arrived On Site Dt | 11/17/2023 15:00 |
Num Pub Evacuated | 0 |
Pipe Fac Name | Greensboro Station |
Segment Name | Tank 145 |
Onshore State Abbreviation | Nc |
Onshore Postal Code | 27409 |
Onshore City Name | Greensboro |
Onshore County Name | Guilford |
Designated Location | Milepost |
Designated Name | 359 |
Federal | No |
Location Type | Totally Contained On Operator-Controlled Property |
Incident Area Type | Tank, Including Attached Appurtenances |
Crossing | No |
Pipe Facility Type | Interstate |
Item Involved | Tank/vessel |
Tank Vessel Subtype | Single Bottom System |
Tank Type | Atmospheric |
Safe Fill Level | 42.7 |
Safe Fill Level Exceeded Ind | No |
Api Std Out Of Service Year | 2016 |
Api Std In Service Year | 2021 |
Installation Year | 1972 |
Manufactured Year | 1972 |
Material Involved | Carbon Steel |
Release Type | Leak |
Leak Type | Crack |
Wildlife Impact Ind | No |
Soil Contamination | Yes |
Long Term Assessment | No |
Remediation Ind | Yes |
Soil Remed Ind | Yes |
Water Contam Ind | No |
Could Be Hca | Yes |
Commodity Reached Hca | No |
Est Cost Oper Paid | 0 |
Est Cost Gas Released | 900 |
Est Cost Prop Damage | 447000 |
Est Cost Emergency | 87933 |
Est Cost Environmental | 50000 |
Est Cost Other | 0 |
Prpty | 585833 |
Num Persons Hosp Not Ovnght | 0 |
Num Injured Treated By Emt | 0 |
Num Resident Building Affctd | 0 |
Num Business Building Affctd | 0 |
Accident Psig | 13 |
Pressure Restriction Ind | No |
Pipeline Function | > 20% Smys Regulated Transmission |
Scada In Place Ind | Yes |
Scada Operating Ind | Yes |
Scada Functional Ind | Yes |
Scada Detection Ind | No |
Scada Conf Ind | No |
Cpm In Place Ind | No |
Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
Investigation Status Details | The release resulted from a crack in the tank floor. The controller's actions did not contribute to the incident. |
Employee Drug Test Ind | No |
Contractor Drug Test Ind | No |
Cause | Corrosion Failure |
Cause Details | External Corrosion |
Internal External | External Corrosion |
Visual Exam Results | General Corrosion |
Other Corrosion Ind | Yes |
Corrosion Type Details | Soil-Side Corrosion Of Tank Bottom |
Field Exam Basis Ind | Yes |
Metallurgical Basis Ind | Yes |
Underground Location | Yes |
Under Cathodic Protection Ind | Yes |
Cathodic Pro Start Year | 1996 |
Shielding Evident | No |
Cathodic Survey Type | Yes |
Cp Annual Survey Ind | Yes |
Cp Annual Survey Year | 2023 |
Prior Damage | N/a Bare/ineffectively Coated Pipe |
Preparer Name | M****** P**** |
Preparer Title | Manager - Codes And Standards |
Preparer Email | M************@k***********.com |
Preparer Telephone | 2052130226 |
Prepared Date | 2024-05-14 00:00:00 |
Local Contact Name | J**** S***** |
Local Contact Email | J***********@k***********.com |
Local Contact Telephone | 3365473661 |
Authorizer Name | Z*** R***** |
Authorizer Telephone | 7134202609 |
Authorizer Title | Director - Codes And Standards |
Authorizer Email | Z**********@k***********.com |
Narrative | At 11:30 on 11/17/23, a leak from greensboro station tank 145 was discovered by local operations personnel. The leak originated from under the tank. By 12:00, the release was confirmed to meet nrc reportability requirements. The nrc was called at 12:15, and the initial nrc report was completed by 12:41 under nrc report #1384562. The PHMSA 48-hour update was made to the nrc at 13:32 on 11/18/2023 under nrc report #1384637. At 13:05, local operations began transferring the product into another tank onsite. An osro was activated and arrived onsite at 15:00 on 11/17/2023 and began gravel remediation. By 11:30 on 11/18/2023, tank 145 was emptied, and the flow of product has stopped. Contractors removed contaminated gravel and dug a trench against the ring wall. The area was surrounded by hay bales and absorbent boom. On 11/19/2023, tank 145 was cleaned and degassed. During an initial internal investigation of the tank on 11/20/2023, a 24-inch crack was found on the bottom plate of the tank floor near the area of release. Tank 145 remains out of service pending repair and internal coating. The cause of the release is under investigation. 1/30/2024 update: kinder morgan has elected to replace the floor of tank 145. The estimated cost of repairs has been updated to include the floor replacement and coating. 4/23/2024 update: kinder morgan completed repairs of tank 145, and the tank was returned to service on april 17, 2024. The cause of the release was determined to be a crack that resulted from combination of external corrosion on the soil-side of the tank bottom and flexing of the tank bottom during filling and emptying. |
External Resources
PHMSA pipeline safety insights.
Product
Features
Company
All rights reserved. Copyright © by ClearPHMSA